[October 16, 2024]
My casual prediction that at the rate I was going the last couple of hose replacements should take me through the fall proved to be correct. I finally finished that project today. The final step was the most complicated, and involved removing the inboard flap actuator cylinders and replacing the hydraulic lines coming from the far aft ends, which were simply lengths of nylon tubing secured to the cylinder with tie wraps, with hard tubing terminating in an AN bulkhead fitting. The bulkhead fitting is secured to a flange that protrudes from the side of the cylinder at a right angle, and is bonded to it with silicone caulk to allow the cylinder to expand under pressure. Now the tie wraps pass under the hydraulic tubing, to keep it from rubbing against the cylinders. Whether this whole operation was worthwhile is questionable, but at least it looks better than it used to, and will certainly not be subject to connections popping loose under intense solar heating of the hydraulic fluid, as happened twice with the nylon plumbing.[June 20, 2024]
After being away most of the month of May and half of June, I finally finished the installation of the lidar gear warning system and flew the plane for the first time in 3 months. It started instantly and seemed none the worse for the long period of idleness. I found that I had by now forgotten which color wire I needed to disconnect to override the gear position signal and test the lidar portion of the system, but that can wait. Ironically, returning to Whiteman, when I was a mile or so out, I ran the landing checklist and found that I had failed to put the gear down. I attribute that oversight to my approaching fast straight in, so as not to inconvenience the airplane turning base behind me. I slowed from 130 to 100 knots rapidly with the airbrake, then put down half flaps. This was a deviation from my normal practice, which is to put the gear down before the flaps. Perhaps I unconsciously consider the flaps a confirmation that the gear is already down. If so, I had better make it my unvarying practice to do gear first, then flaps.[April 13, 2024]
Yesterday I began installing the gear warning system. The first step was to track down the wires going to the up and down lights on the panel, and I discovered that my recollection of the system, which I installed several years ago, was all wrong. I had mixed up the microswitch that enables the landing lights to operate (they are on a gear leg, and so don't light when the gear is retracted), with the switches -- it turns out there are two -- that trigger the gear position lights. So I actually have a "gear down" signal available, not just a "gear up" signal, and the ambiguity of a null "gear up" signal, which could mean gear down or gear in transit, is removed.[April 11, 2024]
I finally assembled the lidar rangefinder gear warning system, but have not yet installed it. It consists of a lidar rangefinder, an Arduino computer and a relay. When the rangefinder tells the computer that the distance to something below the airplane is less than 30 feet, the computer energizes the relay. The relay in turn completes a circuit that gets power from the "gear is up" branch of the gear position microswitch. If the gear is not up, that circuit is not energized and so nothing happens. If the gear is up, the circuit is hot and an alarm sounds. There is an LED that lights whenever the rangefinder says the plane is below 30 feet agl, whether or not the gear is down, and a press-to-test button to check, from time to time, whether the beeper is working.[February 13, 2024]
I have replaced all but two of the nylon lines with proper aluminum and a small fortune in AN fittings, and am now having a hard time bleeding the system. I realize now that certain components could have been better designed to avoid trapping bubbles; unfortunately it is unlikely that I will ever get to apply that knowledge. In the meanwhile I have also begun working on a landing gear warning system using a lidar sensor to trigger an alarm when the airplane is less than, say, 30 feet from the surface and the landing gear is not down. I have never done much with electronics before, but with the help of Peter Lert and YouTube, anything is possible.[December 15, 2023]
Having rehearsed the procedure in my mind a great many times, I set out to replace just one of the nylon hoses in the flap synchronizer with an armored hose with AN flare fittings, etc. It turned out to go more smoothly than I had expected, and in a couple of hours I did all four of the main feed/vent connections. Luckily my visualizations had forewarned me to partly lower the flap before making the change; that way the air that got into the system would be flushed back to the reservoir when the flap was retracted. I will not be able to attempt the next step until after Christmas, the time between now and then being consecrated to making cookies for our annual Christmas party which, after two years of Covid and one of Nancy's broken hip, is resuming its otherwise uninterruped 35-year run. The next step will be to connect the master cylinder outlets to the bubble catchers, four little towers that are supposed to collect any air that finds its way into the lines between the master and slave cylinders. I anticipate that stage being simpler than the first, which required partly dismantling the synchronizer frame; all of the fittings for the second phase are accessible from outside the frame.[September 28, 2023]
After some floundering around I learned that you can buy the plastic breakable link for a Rapco vacuum pump. It came today. The chief mechanic at Able Air told me that once one of these things has failed you might as well get a new pump, because it's friction in the pump that caused it to fail. However, I can't discern any friction in the pump, so I'm going to give it a try. The worst that can happen is that the pump fails again, which won't matter, since I no longer fly IFR. In the course of removing the pump I discovered that a steel bracket, whose intended purpose was to stabilize the throttle body, had fatigued and broken. The break could not be seen, I have no idea when it failed; I installed it in 2014.[September 6, 2023]
A while ago I received a card inviting me to join the octogenarian pilots' association. I have not yet acted upon it; the reality takes time to sink in.[March 5, 2023]
The trim system is pleasantly smooth now, demonstrating that lubricants are not all they're cracked up to be. I checked compressions; three were 80/80, none lower than 77/80, surprisingly good for an engine that qualifies, on time flown alone, as run out. Spectroscopic oil analysis after changing the oil found no ill omens. The radios -- Collins MicroLine dating from the 1970s -- are getting a bit weak; I may need to stop using earplugs under my headset. The airplane's main problem now is hydraulic leaks. I keep toying with the possibiity of replacing all of the nylon lines I now use with a combination of hard aluminum lines and a bunch of short Aeroquip hoses to accommodate cylinder movement. As I mentioned last June, it's a project that would cost quite a bit of money and might yield little or no improvement, since the leaks may be principally in the cylinder seals.The
reason for
the peculiar position of my right arm is that the gear is in transit.
The gear handle must be held in the "up" (or "down") position
while the gear is cycling; it is returned to the center detent once the
gear is up or down. The flaps work the same way. Both flap and gear
handles are connected by cables to closed-center hydraulic
valves, and directly actuate microswitches to energize the
hydraulic
pump.
[January 17, 2023]
Having gotten the trim system back into shape, I noticed that there seemed to be some friction in the elevator circuit, so I pulled out the hinge pins and cleaned and dry-lubed them, one with Molykote and the other, when the Molykote spray can clogged, with some stuff from Home Depot called Blaster. The elevator is still not exactly frictionless, but at least the friction is more or less constant throughout its travel, not variable as it was before.[January 3, 2023]
Nancy being at last sufficiently mobile that I can leave her alone in the house, I was at the airport yesterday and today trying to track down the cause of the extreme stiffness, indeed virtual inoperability, of the pitch trim. After exonerating the trim jackscrew, whch I originally assumed was the culprit, I finally homed in on the sprocket that converts the linear movement of the trim cables, via a length of bicycle chain, to rotary motion in the jackscrew. Apparently, long ago, in an effort to gild the lily (or, as the bard actually put it, to gild refinèd gold and paint the lily), I greased the bushing that supports the sprocket. In the course of (much) time the grease dried out, and now the sprocket would barely turn. I was kicking myself for the inaccessibility of the assembly, and had already taken a bunch of stuff apart (including removing the rudder), when I realized that all I really needed to do was take out the elevator bellcrank and I could remove the sprocket and its supporting bushing easily. I cleaned up the bushing, put the assembly back together dry -- aluminum is a perfectly good low-speed bearing surface for a steel shaft, even without lubricant -- and re-installed it. Now I just have to undo all the unnecessary disassembly of the surrounding structure. Actually, it has not been a complete waste of time; I was able to inspect a lot of hidden pieces and confirm that everything is holding up. I was impressed by the ingenuity with which I (not I who am writing, but an I of many years ago, practically a stranger to me now) had modified and cobbled together various pieces of a much longer linear actuator to make the current trim system. It really isn't bad at all.[December 7, 2022]
I flew today for the first time since September 22. My long absence from the upper air was not voluntary. Nancy and I spent the month of October in Ojai, with only occasion brief returns to Los Angeles, helping our son manage his two kids while their mother was doing a 30-day yoga program in Bali. No sooner did we get back than Nancy fell and broke her hip. She was in the hospital for three weeks, two of them in rehab getting physical therapy. I was with her most of the time. Now we're back home at last, and a day finally arrived when our daughter Lily, who came out here from New York between jobs to help, could hang out with Nancy while I went flying. Too much information, I admit. Anyway, the plane still flies, although now that colder weather (actually, standard atmosphere) is here the grease that I foolishly put on the pitch trim jackscrew has stiffened up and made the trim practically inoperable. I have to take the assembly apart, clean the screw and nut, and lubricate them either with dry graphite or not at all.[September 22, 2022]
I did a speed check today at 10,500 ft. The density altitude was 13,000. Speed seems to be a little off the expected numbers; at 25/2300, 25 LOP with a fuel burn of 9.9 gph, I got a true airspeed of 184 knots, versus an expected 189; or, to put it differently, versus an expected 9.5 gph. My engine is around TBO, and while I believe even an old engine will develop rated power, I'm not sure it will develop rated sfc. Since I use a curve-fitted sfc model to determine power for purposes of performance calculation, if the actual sfc is higher than I am assuming then the engine is developing less power at a given fuel flow, and so speed would be below the predicted value.[August 2, 2022]
Sure enough, the problem with the landing/taxi light was a broken ground wire, which I found and fixed. I seem to have suffered an unusual number (two) of broken ground wires lately; the reason is probably related to the fact that a composite airplane does not have the convenience of airframe ground, and so uses a great many more ground conductors than a metal airframe would. In many instances I used shielded conductors with the shield as the ground return, but not in the case of the landing light.[August 1, 2022]
Today I revised the wiring connections for the switch panel, and in so doing I found the broken ground wire that was the reason for the anticollision lights not working. Now they work, and, collaterally, that particular patch of wiring is a little better organized than it was before. Tomorrow I will tackle the problem of the inoperative landing lights. It will probably turn out to be something similar. I always imagine electrical gremlins to be more devious and subtle than they really are.[July 29, 2022]
The persistent refusal of the so-called strobes (they are actually halogen lamps) to work continues to baffle me. I have tried to troubleshoot the problem armed with a digital multimeter and almost zero understanding of electricity, and gotten about as far as I deserve to. The wiring behind the panel is not so well organized and labeled as one would wish, to put it mildly. Generally, my wiring resembles that of a Delhi slum. I decided to do some housekeeping there on the assumption that I would stumble on a solution to the strobe problem in the process. Actually, what I have stumbled on so far is that the landing/taxi light is not working either. They have nothing in common other than a 15-pin Molex connector that I've decided is too crowded with wires, so I'm dividing its occupants between two smaller connectors, one for the nav/panel/landing lights and another for the strobes. The flasher circuit was designed by the late Paul Lipps, who also made me the little board that operates it. It incorporates some ingenuity to increase bulb life; in the words of a caption, "This unusual dual-bulb flasher eliminates high inrush currents by using one bulb's heated filament to limit the starting current for the other bulb." This refinement may be superfluous, since the small halogen bulbs I use are practically given away and I don't fly at night anyway.[May 5, 2022]
Cinco de Mayo! And with it --- well, nothing, actually. Yesterday I flew around for an hour, going, as usual, nowhere. I noticed that the left main strut was a little low, which is surprising, since with warmed weather you'd think it would get a little higher. It's been years since I've added air to the struts; they hold air well. I dipsticked the fuel, and found that it perfectly matched the totalizer. This seems always to be the case, although I never set the totalizer by the dipstick value, only by the gallons added. The totalizer is an old Alcor that Mike Melvill gave me; the company, whose employees are all younger than the totalizer, now denies any knowledge of its existence. The so-called strobes still aren't working, I don't know why, and the Lowrance GPS is increasingly demented, but who isn't?After I finished that chore, I was lying under the plane trying to figure out where a hydraulic fluid drip was coming from and to decide whether it was even serious enough to bother tracking down. I suspect the airbrake actuator; its O-rings are about 20 years old. My main gear actuator is also a possible culprit. It came from an Aztec, I think, and I can't remember now whether I overhauled it before I installed it, which was maybe 25 years ago. If either of those is the source of the leak, I won't be surprised. Maybe both are. But I couldn't summon the energy to pull either actuator, so I just lay there looking up into the well where all the hydraulics are and thinking, "God, I did this?"
At some point recently my "strobes" -- they're really blinking halogen lights -- stopped working. I have tried to track the A+ and ground wires through the maze behind the panel to find the problem; so far no luck. On a more cheerful note, I got a comm radio (Collins MicroLine VHF-251) on eBay for $150 to replace the one that quit. It works reasonably well -- well enough for a backup.
[January 3, 2022]
My anxiety about the apparent inaccessibility of my oil screens turned out to be a case of hypochondria by proxy. Though I could not recall having inspected the oil screens -- there are two, a suction screen and a pressure screen -- I probably had done it at some point in the past 19 years. And, although it took a little fancy wiggling to extricate them, it was not necessary to make a hole in the engine mount to do so. And both screens were perfectly clean; washing them with acetone liberated exactly nothing. So my concern about oil starvation due to a clogged screen turns out to have been unnecessary. The time and trouble were not wasted, however, because knowing that the screens are clean is roughly equal in importance to their actually being clean. Incidentally, it's not surprising that the "pressure screen", through which oil returns to the sump, is clean, since oil passes through the oil filter before reaching it. As for the "suction screen", it is very coarse and is apparently intended to prevent large fragments of a disintegrating engine, or perhaps nuts or bits of safety wire inadvertently abandoned by a careless overhauler, from getting to the oil pump.[November 23, 2021]
Nancy and I and three other couples went to Hawaii for a couple of weeks. We spent three days at Hilo and then went to Hanalei on Kauai for the duration. It was fun. I came back with a pair of flipflops called "Locals" which to my surprise were immediately recognized by a passerby as a sign of my having recently been to Hawaii. You never know what people are looking at. When I flew after coming back I found that the fuel totalizer had apparently regained its long term memory and was again retaining the fuel remaining from flight to flight. My next job is going to be to cut an access hole into the engine-mount-cum-nosewheel-box so that I can get the oil screen out of the crankcase. It has been blocked in there lo these 20 years, but I just read an NTSB report about somebody's engine quitting and the oil screen being found half full of schmutz. Apparently it hadn't been inspected in 11 years. I am a little skeptical of the attribution of a sudden engine failure to a partial obstruction that must have accumulated very gradually, and I put faith in my oil filter, but as a matter of principle I guess the oil screen should be accessible.[October 7, 2021]
I finally finished installing the new tailBeacon. The first couple of PAPRs I got reported NIC and NACp discrepancies, but I think those may have been due to the mountainous route I flew from WHP to Santa Paula and back, so I am not panicking yet. There has, however, been a series of other unfortunate, if minor, annoyances. One cushion of my David Clarks began oozing silicone gel down my neck. (This is the second time this has happened, by the way. The first time I had just landed at Kendallville, Indiana when I dicovered the reason my neck felt so greasy. By chance, a Blanik landed soon after me, and its pilot turned out to be a manufacturer of silicone gel. I remarked that I hoped it did not have flesh-eating properties. "If it's okay for breasts, it's okay for necks," was his reply. Actually, breast implants have had a checkered history, but my neck seems okay so far.) Then my fuel totalizer stopped remembering the fuel remaining from one flight to the next. Most likely the problem is failure of an internal battery, but it could be something more dire: the eventual decay of semiconductors, which has rendered both of my Lowrance GPSs mere shadows of their former selves. Finally, the new direction of Flying threatens to make of me that rarest of rarae aves: an airplane owner with an income below the poverty line.[August 25, 2021]
After many delays the tailBeacon went to uAvionix for repair. Nancy and I are going to the East Coast for two or three weeks, so it will not be back on the airplane until mid-September. In the meantime I have accomplished nothing besides adding the stout ground wire -- 14 gauge, as it turned out -- linking the aluminum frame on the aftmost bulkhead to the nearest airframe ground, which is the instrument panel. I was about to cut a hole in the afterbody of the engine/intercooler airscoop for a dedicated flush air inlet for the pilot, but I began to wonder whether putting a NACA scoop on a narrow raised surface was such a good idea. I could put it above the afterbody, but I have been discouraged from doing that by concern that hot air from the various top-surface cowling outlets might get to it. I doubt that could actually happen, but by the time I make up my mind the weather will have cooled off and an extra airscoop will seem less desirable, so the whole project may drag on until next summer. In the meantime Flying Magazine has been sold yet again, with what consequences for me remains to be seen. Flying has been the reason I have been able to spend my life messing about with airplanes; I hope that doesn't change.[July 30, 2021]
At the beginning of July, I got a stern letter from the FAA telling me that my ADS-B performance was not up to snuff, and giving me 45 days to shape up. My NIC was out of tolerance. Don't ask. I got in touch with uAvionix support, and they said it was probably a matter of the ground resistance, which should be less than half an ohm. This was the first I knew of that requirement; I don't know whether I overlooked it when I first installed the tailBeacon or they did not think it worth mentioning. Low ground resistance is easy to accomplish in an airframe made of metal, but takes more attention in a composite airplane, especially when the nearest ground plane -- the instrument panel frame -- is 18 feet away. I had supplied a rather fine ground wire, 20 or 22 gauge, and its resistance was around 1.5 ohms. Apparently it was right on the edge of okay, because I've been flying for more than a year and a half with the tailBeacon and this is the first time the FAA has complained.[June 24, 2021]
Nancy finally finished proofreading Aloft yesterday. She found a bunch of typos and scanning errors, so my rashly publishing the ebook on June 1 was obviously a mistake. If anyone rashly bought it (Rule 1 of software: never buy v.1.0) and would like a copy with the errors fixed, let me know and I will PayPal or otherwise send the $8 so that you don't need to pay for it twice. The paperback version should be available on Amazon in a couple of days. Incidentally, some guy who writes fantasy fiction has chosen to do so under my name, heaven knows why. I am not the author of The Magic Dead (Changeling Saga #3).[June 3, 2021]
A couple of days ago I had a bad runup: big drop, rough, and didn't get any better after I ran up to high power and leaned. The problem occurred when I turned off the mag switch labeled 'L". Did 'L' mean I was checking the left mag, or turning off the left mag to check the right? I wired the system 20 years ago, and it's been so long since I've had a bad mag drop that I'd forgotten what I was thinking back around 2000. I also wasn't sure how the mags related to the plugs -- the leads are a confusing jumble of identical wires -- but I suspected that the right mag assocated with the upper right and lower left plugs. Just to be sure, I asked an A&P, who said there was no hard and fast rule, and that he had even seen systems in which the right mag fed the right cylinders and the left the left -- an arrangement that seems to violate common sense, as he readily agreed. Eventually, on the advice of a different A&P, I ran up to 2,000 rpm, leaned to bring up EGT indications, and checked each cylinder. Turning off one spark plug slows the burn within the cylinder, so that the exhaust gases are hotter when they leave it. When both plugs are healthy, the EGT will rise during the mag check. The effect was not subtle. The EGT on #1 was much higher than the others' with both mags on, and when I switched off the left mag -- that's what 'L' means, as I found by checking the P leads with a multimeter -- it dropped to the peg. No ignition whatever on #1 from the right mag. I replaced that spark plug and the engine ran up fine. The faulty plug looked okay; there was no external evidence of failure.[June 1, 2021]
In a second venture into self-publishing, I have assembled 50 or so articles from my Technicalities column into a book called Aloft, which is currently available from Amazon (mea culpa!) as a ebook and will emerge in paperback form just as soon as Nancy finishes finding typos in the manuscript. It looks like this:[April 2, 2021]
Yesterday the temperature hit 88, so, while it's still not exactly midsummer in the Rub al Khali, I did a quick oil temperature check using the digital system. The highest I saw was 193 F during a high power climb; cruising, it settled at 177. That is exactly the Vernatherm setting, so I guess the system has been working as expected all along, and my years of intermittent concern over high oil temperature readings were due to nothing more grave than a faulty panel instrument. The temperature did seem to be slightly affected by the cowl flap setting, so I will do some further tests to compare the current arrangement, where the oil cooler air vents into the upper plenum along with the cylinder cooling air, with the alternative, in which the oil cooler air shares a vent with the turbocharger intercooler air and is unaffected by the cowl flaps.[March 17, 2021]
I asked, rhetorically, in the current issue of Flying, whether, if you sliced an airfoil-shaped body of revolution transversely at its thickest point, the bullet-shaped forebody or the blunt-faced afterbody would have the greater drag. My friend Hans Kandlbauer ran some simulations using Solid Works' RANS code, with the following results:[February 17, 2021]
I did a cold compression check. All three cylinders on the right side of the engine were 80/80. the three on the left were 42, 64 and 71. This seemed odd, so I ran the engine for five minutes at 1,200 rpm, then shut down and repeated the check on #6, which was the lowest; it now showed 80/80. I don't understand compression checks; it seems as if you can get just about any result on any given day. The asymmetry is puzzling, however.[February 10, 2021]
A friend forwarded me a picture, taken by a friend of his, Elwood Schapansky, of the original Melmoth at Galena, Alaska, in July, 1976, a few days before Nancy and I flew over to Japan. I am surprised to see that 1) the airplane was so clean; and 2) the down jacket, which I still have, was once so puffy.[January 8, 2021]
Oddly, it has now happened twice that the new micro-camera stopped working as soon as I took off. Today, however, I did get a gratifying speed point at 14,000 ft DA, 181 ktas at 9.2 gph, 63% power, which is slightly better than the computer simulation predicts.[December 19, 2020]
Last week was notable for ridiculousness. I re-did the calibration of the MS-28034 induction air temperature probe, and checked a spare as well (I have three -- the third is the oil temp probe). Both returned horrible calibration curves, with a true 100 deg C reading as 125, and 40 reading as 55. Since it is unlikely that two probes are identically faulty (and the oil temp, which I did not test, also indicates unexpectedly high), it seems probable that, as a friend suggested a few weeks ago, the problem is the three-gauge panel display, which is probably coeval with the B-47. If this is the case, then all my worries about oil temperature have been unecessary, since it has actually been in a reasonable range all along.[November 30, 2020]
Before Thanksgiving I moved the IAT probe, which is about 1/4 inch thick and a couple of inches long, from its position at the entry to the throttle body to one in the middle of the intercooler outlet tank. I did this in the hope that the asymmetry it created in the throttle body flow, which it entered from one side, might be responsible for the odd difference between EGTs between the right and left cylinder banks. The change turned out to have no appreciable effect. CHTs have always been very inconsistent front-to-back, but they do not show the same right-left imbalance as EGTs do. Yesterday at 12,500 ft d.a. I recorded these CHTs (Celsius) with partially open cowl flaps, ordered front-to-back:[November 14, 2020]
I added a heat shield to the portion of the duct leading air to the oil cooler. The result -- with the not negligible help of cooler weather -- was that the oil temps are now in the green. The temperature of air entering the cooler is now about 4 deg. F above ambient, so there is still some heating taking place on the way from the cowl intake, but it's slight. The temperature rise in the air passing through the oil cooler is around 75-80 degrees F. It was apparent that the vernatherm was working as intended, since there was no temperature rise in the air passing through the cooler until the oil temperature hit 160 F.
The oil temperature turns out to be quite sensitive to the position of the cowl flaps, which regulate the pressure drop across the cooler and the amount of air passing through it. This was the reason I originally provided the oil cooler with its own exhaust duct, separate from the cylinder cooling air. With cowl flaps open, oil temp was 185, fully closed 215.
I finally got a speed point -- 178 ktas at 9.6 gph at 12,500 ft -- that more or less matched predictions for an equivalent flat plate area of 2.35 sq. ft, so the intercooler and the pitot-style scoop on the side of the cowling have not added a huge amount of drag. They've added some, however. Maybe I should have a way to shut off the intercooler when I don't need it.
[November 2, 2020]
The duct is now installed.[October 21, 2020]
I see that it was just shy of three years ago that I contemplated providing a direct duct from the cowling air inlet to the oil cooler, to avoid an admixture of exhaust-warmed air. I have now almost finished the mold for this duct:[October 13, 2020]
The oil and air temperature probes, which share the same indicator via a toggle switch, both read high on the ground (on a 38 deg C day. they read 50 C) but say 100 C when immersed in a can of boiling water; so they're okay. I decided finally to provide a separate supply of cold air to the oil cooler, and I am making tooling for that duct now. Now that the oil cooler will no longer be sharing an outlet with the intercooler, I can probably replace the hood over the opening with shark gills.[September 24, 2020]
No peace unto the wicked. I took out the nice oil cooling air outlet plenum and duct that I was so pleased with, closed up the holes it left, and moved the pressure probe line to the top of the (now intercooler only) outlet pan. The OAT was slightly higher than yesterday's: 94 F on the ground and 71 at 8,500 feet, or 42 degrees F above standard. Despite the change in the oil cooler arrangements, during the climb the oil temp went up to 240 F, same as before, and settled back to 230 in cruise.[September 23, 2020]
I collected a few pressure points from the plenum immediately above the oil cooler. To my surprise, the pressures there were quite high, even though the outside world is 12 inches away through a 10 sq. in. duct. Two representative values were 3.8 in. H2O at 120 kias and 5.1 at 140 kias. These correspond to delta-p's of 3.5 and 5.4 inches respectively. What is surprising about this is that the delta-p's across the engine are 6.5 at 120 and 7.9 at 140. In other words, I would get better delta-p across the oil cooler if I closed the external duct and simply let the oil cooling air spill into the upper plenum. This was the original arrangement, before I started messing with it about 10 years ago. I now intend to try reverting to it.[September 22, 2020]
I finally managed to get some video of the scoop tufts, but now I can't figure out how to download the video from my iPhone. However, I did some screen grabs, of which this is one:[September 12, 2020]
I tufted the scoop and then made two attempts to record video of the tufts in flight. Neither was successful. I belatedly realized that the camera rig I was using had no on-off switch, and was activated simply by connecting the battery to the camera. The charging port is on the camera, however, and so to charge the battery one must connect it to the camera. I had not done so, and when I turned it on before flying the camera would work for just long enough to persuade me that it was okay, but, once I was airborne, quit. I can see some of the tufts from the cockpit, and they were lying down nicely. Tufts are typically made of a loosely woven yarn, and one telltale sign of flow separation is tufts that are unravelled after flight. Tufts in smooth flow are undamaged. The only frayed tuft I had was one right in front of the center of the boundary layer channel; I suppose it may have been whipping back and forth across the stagnation zone.
In the course of the last three flights I noted unusually high oil temperatures. The ambient temps have been around 40 degree F above standard -- that is, in the high 90s -- but even so the oil temp is higher than expected. I checked the pressure in the lower plenum and got the impression that it's down a bit, perhaps because of leakage into the collector pan from which the intercooler and oil cooler air are vented. The pan is stationary -- it does not move with the engine -- and so I am removing its flexible perimeter seals and replacing them with a rigid barrier that will press into a rubber sealing strip on the inside surface of the cowling. There could be other reasons for the increased oil temperature, but since all are potentially more dire or difficult to deal with than this one, I might as well start with this.
Last Tuesday I climbed through smoke to 5,000 feet, hoping to get on top, but with restricted forward visibility -- impossible to tell whether it was three miles or half a mile -- and with the ground disappearing below me, I turned back to the airport. Yesterday and today the smoke has been dense, down to the ground, its campfire smell pervasive, the sun a faint orange disk or entirely invisible, all around an infernal and shadowless scene.
September 2, 2020]
[August 7, 2020]
The outer form of the scoop is now complete; only the afterbody behind the cowling parting line remains to be laminated, and then the whole thing needs to be smoothed and finished. The ivory paint with which I originally painted the plane 17 years ago, and of which I still have a serviceable can, now seems to cure with a faint purplish hue, so the repainted areas around the new inlet and outlet will be rather conspicuous; but no one has ever accused me of being overly fastidious about paint. Call it Murano.[July 30, 2020]
I finished the inner liner of the new airscoop today. (When I flew the other day, the front 4.5-inch duct and the boundary layer channel were not yet installed.) This will now be covered with a layer of foam, which will be sanded to a streamlined shape and glassed over. The inlet is 7 inches wide and 1.25 inches deep, and the boundary-layer channel is 3/8 inch deep. The afterbody will extend a little past the firewall along the side of the cabin and will incorporate a small flush scoop for the pilot's ventilator.[July 24, 2020]
I flew today with the new air inlets partly installed. At present only the inner surfaces are in place; the outer fairing is yet to come. I was curious to see what speed penalty the sharp-edged, lipless excrescence would exact. At 10,500 ft, where the density altitude was 12,500, 9 gph gave an indicated airspeed of 143 for a true of 172. This is about three knots shy of what the computer model predicts. On the other hand, at 7.8 gph it was 138 kias (166 ktas) which coincides exactly with the model. So I suppose things won't be noticeably worse once I have the smooth fairing built.[July 21, 2020]
I've been spending a couple of hours a weekday on the seemingly endless task of replacing the air inlets for the engine (NACA flush, very pretty) and intercooler (crude metal kludge) with a single pitot-style scoop. I am very sorry to lose the NACA inlet, the look of which I have always liked, but regret, as both Chief Seattle and Marlon Brando have said, is useless. I intend to incorporate into the afterbody of the scoop a smaller NACA inlet, a sort of consolation prize, to provide air directly to the pilot's ventilator. In the present arrangement, a single inlet on the right side supplies both pilot and front-seat passenger, and it is not too satisfactory for the pilot on hot days if the passenger-side vent is open. The two back seats share a single ventilator, but it produces a surprisingly powerful blast of air, as Russ Hardwick and I discovered to our sorrow when flying at a frigid 15,500 feet a few years ago. I resolved then to provide the pilot with the ability to shut off that ventilator, but have not yet done so.[May 27, 2020]
I found a nice picture online of M2 leaving Oshkosh in 2011. Takeoff flaps have not yet been retracted. This reminded me that there are still some bits that need paint. I wrote to the copyright holder asking for permission to post the picture on this site. I have not yet heard back -- it's been a couple of weeks -- but if he refuses I'll take it down. So study it carefully now.[May 2, 2020]
To convert the geyser emerging from the top of the cowling into a more-or-less aft-facing plume, I removed the hood from the now-disused oil cooler outlet with an oscillating saw -- marvellous tool! -- cut it in half lengthwise, made it an inch wider, and tacked it over the new outlet with some fancy turning vanes added. I am now laminating this into place, and in the process am revisiting my long-neglected epoxy-metering equipment. My ratio pump is too gummed up to use without a thorough cleaning, but I find that a simple balance beam is almost as fast. In the past I used this method, when I used it, quite stupidly, piling up certain number of washers, moving them right or left to balance, and then increasing their number as needed to achieve the desired ratio when the second part was added. This time around it finally dawned on me to make a mark 10 inches from the balance point, and other marks at 12 inches and 14.4 inches, representing respectively the mix ratios for West System and EZ-Poxy. You put your empty mixing cup into the ragged-looking cup at the right-hand end and balance it with the big nut. You then pour resin into the mixing cup, balance it with washers at the 10-inch index -- you can precisely match the washers with a few extra drops of resin, if need be -- and then move the stack of washers to the appropriate index and add hardener to balance. I can't believe how long it took me to figure this out. Not so smart after all.
[April 17, 2020]
Initial test flights produced mixed results. Induction air temperature dropped by 30 deg C, from 65 to 35, with an OAT of 19 C. I'm not sure how good that is, but anyway it's going in the right direction. On the other hand, the oil temperature, which I optimistically expected to be lower than with the previous arrangement, initially settled at the top of the green, but then started creeping upward. Suspecting that this might be related to the fact that air from the oil cooler and air from the intercooler approach the outlet from opposite directions, I landed, taped over the intercooler air inlet and took off again. The oil temperature got even higher, which made no sense at all. On landing and removing the cowling side panel, I found that the neoprene gland at the bottom of the oil cooler duct had partially prolapsed, probably because of the large pressure difference across it. I'm not sure how that would affect oil temperature, but at any rate it's something that needs to be fixed. At the moment it's held in place by friction; I'll try a hose clamp. The tufts that I had affixed around the outlet on top of the cowling resembled the scene when a car collides with a fire hydrant; I began work on a hood.
Here at last is the finished ducting for the intercooler and the oil cooler. Spent oil cooling air now goes into a box that protrudes through the rear baffle, and thence through a 3.5-inch duct into a plenum shared with the intercooler. The plenum vents through the top of the cowling; I am bandaging that wound now, and I hope to be able to test-fly the system by the end of this week. If all goes well, I will then turn my attention to the airscoop on the side of the cowling. It will replace the odd pairing of a crude temporary metal scoop and a slick NACA flush inlet (see below) and will provide air to both intercooler and engine. I shall draw my inspiration from the scoops on top of the cowlings of the DC-7 in which I took my first plane ride at the age of 10.
[March 25, 2020]
Today I added the flexible baffles to the air outlet box; tomorrow I'll cut the dreaded hole in the top of the cowling. Yesterday I flew with a temporary airscoop feeding cooling air to the intercooler. The air, having passed through the intercooler, merely flowed into the cowling. Nevertheless, the induction air temperature was lower than usual. The scoop is homely, but at least it has its own boundary-layer channel:
Progress on the intercooler project, which began two years ago, has sped up markedly. One of the reasons for this -- not, I'm sure, a very sensible one -- is that I would like to get the system finished, along with the oil cooler ducting to the new hot-air cloaca on top of the cowling, so that the plane is at least complete, if not clean, in case I contract COVID-19 and die.
[March 13, 2020]
The intercooler is now equipped with its inlet and outlet ducts. The inlet is the upper of the two rectangular openings below the intercooler; the lower one is the engine induction air filter box. The outlet is the tray on top, which is eventually intended to receive both intercooler and oil cooler air and send them out a louvered vent on top of the cowling. The current protruding outlet for the oil cooler will disappear. I've partially built the duct in the side panel of the cowling that will bring cooling air to the intercooler, but I haven't cut the hole in the cowl side yet -- I hate cutting into these pristine surfaces. Also, I have been busy lately with an apparatus from which the ashes of an old friend will soon be scattered into the Pacific Ocean.
[January 22, 2020]
The Christmas season is hopeless for getting any work done on the airplane, as I have regularly complained before. Early January does not seem much better. I did collect some rough data on EGTs, and found that while messing with the induction did not noticeably affect the synchronization of peak EGTs, it did somehow or other cause the right-side cylinders to collectively run at higher EGTs than the left-side ones. I asked George Braly at GAMI about this, and after offering various comments and suggestions he added a quotation from Richard Feynman about the easiest person to fool being yourself. I have often fooled myself in the past, and am prepared to believe that I am doing so again now. After I have the intercooler plumbing completed I will do a careful survey of EGTs and possibly add a flow straightener or an adjustable vane just ahead of the throttle inlet in order to equalize the flow to the two intake-manifold logs.
In my previous entry I bashfully admitted to having made a really beautiful landing on a particular flight. Well, I am about to do so again. My landing yesterday was perfect. I feel free to say this because while Melmoth 2 is not a difficult airplane to land well, I seldom manage to get all aspects of the landing to work out perfectly, and so I either land at a slightly higher airspeed than ideal, or with more of a tap (or bang), or I don't put the nosewheel down as gently as I would like to because I run out of tail authority (being alone, and therefore noseheavy). There are some tall things sticking up just across the street from the approach end of Runway 12 at Whiteman, and, although you'd have to be awfully low to actually hit one, I tend to come in a bit high and chop the power just short of the end of the runway, with the displaced threshold still several hundred feet ahead. The glide steepens noticeably before I begin to flare. Ideally, the nose is still coming up as the tires get within a few inches of the surface. I like to get the nose really high, stall warning blaring, and on touchdown -- nearly imperceptible, of course -- lower it with sufficient control to arrest the wheel just before it touches and place it gently on the runway. At that point the speed is under 40 knots and I easily make the midfield turnoff. There is nothing extraordinary about any of this; it's really just a matter of chance to get all components right. But, as any pilot knows, it's a good feeling when you do.
[December 14, 2019]
The intercooler passed its first functional test, viz. it did not fall out of the airplane during its first two flights. After suitable delays for meleagricidal late-November activities, I got the outlet tank re-contoured, boldly sawed a 90-degree bend out of the existing duct, and put it all back together. At first it appeared that replacing the short elbow with a long one had made no difference, since on runup I found that the right-side EGTs were still much higher than the left-side ones. It then dawned on me that I had never established a baseline; I had merely assumed that since EGTs are pretty even in cruise, they must be in runup as well. For that matter, I never look at the EGT or CHT during takeoff, and so my impression, during the first test a couple of weeks ago, that CHTs were rising ominously may have been spurious.
I removed the intercooler again -- I've gotten pretty good at it -- re-installed the old duct and did a run-up, which revealed exactly the same behavior. It may be that even the short elbow was not having the enormously detrimental effect on mixture distribution that I thought, but the 6-inch radius aluminum duct looks a lot better. I put the intercooler back in, flew to Santa Paula, bought some relatively cheap gas ($4.35/gal vs $5.59 at Whiteman), and flew back to Whiteman, where I made, I must say (because I can't always), a really beautiful landing.
At present the intercooler is just a rest stop along the way from turbocharger to throttle body; I have not yet made any provision for cooling air to flow through it.
[November 23, 2019]
It turned out that the outlet "tank" could be shortened fairly easily to accommodate the same aluminum elbow of 6" radius as is now part of the pipe that runs from the turbocharger to the throttle body. I just need to do a little sculpting with filler -- a mixture of epoxy with plastic microspheres for lightening -- to smooth the internal contours of the tank. The intercooler will then be rigidly supported at its inboard end -- no more spring -- and sufficient (I hope) flexibility will be supplied by joints at both ends of the aluminum elbow. There is no guarantee that the flow distribution in the intake manifold will be entirely unaffected by a heat exchanger replacing a length of straight pipe; but I think the effect, if any, ought to be much less than that of the villainous blue elbow of yore.
Going back through this chronicle, I see that I never supplied a picture of the present plumbing connecting the turbo to the intake manifold. This is it:
The long duct consists of a bunch of pieces of .035 wall aluminum tubing spliced with bands of fiberglass cloth and epoxy. I don't know where I got the tubing, but I wish I had more of it. I will have to saw the 90-degree bend out of the top end. I would prefer to keep the old duct intact in case the new arrangement doesn't work; but there's no choice.
[November 15, 2019]
Physics 1, Hope 0.
At least I was not so naive as to be unaware that that short elbow might cause trouble. I just hoped it wouldn't, and told myself you never know with fluid flow, which is true, generally. However, by the time I was halfway to the runway for the first test flight, it was obvious that the right side of the engine was running much leaner than the left. I began a takeoff, but aborted it when after a few seconds the CHT I was monitoring (#3) hit 200 deg C (392 F). Normally, the engine does not get to that temperature until I am well established in the climb. I returned to the hangar, removed the intercooler, put the old duct back into place, and went flying.
I need to revise the shape of the duct on the outlet side of the intercooler to allow a bend with a radius of six or seven inches between it and the throttle body. That is the radius of the bend in the current pipe, and it works fine. But this puts me back in search of a 2.25-inch I.D. hose sufficiently strong to handle 1 atm. of overpressure at, say, 250 deg. F, and sufficiently flexible to 1) make a 6-inch radius bend without wrinkling on the inside and 2) allow some freedom of movement between the engine and the intercooler.
[November 7, 2019]
After much hesitation about how and where to mount the intercooler, I settled upon the above arrangement. The difficulty is that the intercooler is secured to the airframe, but connected to the engine, and the distance from the throttle body to the intercooler outlet is too short to allow for the full range of motion of the engine. The solution I am trying -- which may be no solution at all -- is to mount the outboard end of the intercooler to the firewall with a flexible shear clip made of .016 stainless steel sheet. A diagonal strap removes bending loads on the mounting lug, which is bonded directly to the honeycomb firewall and should, in principle, experience only shearing forces parallel to the firewall surface and a compressive force against the firewall. At the inboard end, a coil spring provides several pounds of lift, so that the flexible duct is not carrying the weight of that end of the intercooler. The inboard end of the intercooler does have some freedom of movement, however, to allow for the engine jumping around during startup and shut down. I'm not happy about the very tight elbow, but it was all I had room for even though I used the shorter of my two intercoolers. I started the engine today just to confirm that the assembly did not immediately fall apart. The next step will be to attach the fiberglass ducts to the intercooler and re-run the inflight EGT survey to see whether the elbow is affecting the mixture distribution. If the system passes that test and doesn't disintegrate in a few hours of flying, I will add the ducts for the cooling air.
[August 26, 2019]
The inlet and outlet ducts are finally, albeit temporarily, attached to the intercooler:
In the picture the intercooler is upside-down; the pipe on the left connects to the turbocharger, which is below it, and the one on the right goes to the throttle body. It actually fits into the airplane like this:
You can just see the turbo outlet as a dim red crescent at the bottom of the picture.
My present plan is to provide a pitot-type (i.e. non-flush) inlet for the cooling air, because flush NACA inlets are not effective unless there is a negative pressure gradient downstream. The cooling air will vent upward out of the top of the cowling. I plan to remove the present hooded outlet for oil cooler air and vent that air to the same outlet as the intercooler's.
[July 30 , 2019]
A week ago I finally took the intercooler to a welder to add the flanges to which the charge air ducts will be attached. I got it back yesterday. Since I changed my mind about which to use of the three intercoolers I have collected over the years, I had to saw about four inches off the outlet duct, which I had already made, and I will have to modify the inlet duct mould similarly before making that part. After lengthy mental calisthenics visualizing various ways in which the intercooler could be installed, I finally concluded, by dint of propping it up in place, that my first plan -- that of March 23, 2018-- was the best, or at any rate no worse than any other. Getting fast-moving induction air around the corner from the intercooler outlet to the throttle body inlet requires a 2 1/4" I.D. flexible elbow with a 7-inch radius of curvature. I found something at McMaster-Carr that should work. I also found ready-made aluminum tubing segments with beaded ends, which I will bond into the laminated ducts. So the design and materials of the induction air plumbing are more or less settled. As for the cooling air, I am leaning toward a pitot-style external scoop for both the intercooling and induction air, located where the NACA flush scoop is now, and some sort of louvered outlet on the top of the cowl, directly above the intercooler. I am also thinking of ducting the oil cooling air to that same outlet and dispensing with the hooded vent I am using now. The drag penalty of an external scoop and an additional heat exchanger is hard to foresee; if it represents an increment in F, the "equivalent flat plate area", equal to the frontal area of the inlets, it will be barely acceptable in exchange for cooler induction air and greater detonation margins.
[June 1 , 2019]
Nancy and I got back from a week-and-a-half trip to the east -- college reunion -- this morning at 2:00 a.m. I was planning to fly up to Paso Robles for Chuck Wentworth's annual Antique Aero BBQ, but LA has been socked in all day and I'm not remotely current, so I stayed home. This has given me time to think about all the things I need to do, mostly tedious. Having relieved the AT-50's 12-volt power supply of its duties, I now have to find another job for it. M2 has two of those Narco 24-to-12 converters, actually; I think the other powers a 12-volt outlet. Can I simply hook them together, in parallel, or would that engender inner conflicts? (Being ignorant of electronics, I have to launch queries like this into the ether, like Noah's dove.) Poking about back there also reminded me that I have never connected my pitot and AoA tab heat -- not that I will ever use those things in my ever-less-ambitious flying. Furthermore, installing the new transponder somehow caused my glideslope receiver to quit working; a loosened connection somewhere, no doubt. The intercooler, meanwhile -- like Hope, it is forever deferred, but never extinguished -- awaits the creation of the second "tank" and the addition to the heat exchanger of a couple of aluminum flanges to which the tanks will be secured.
While we were in the East, by the way, an unusual event occurred. Someone streamed Jaws, and, of the four people present, three -- Nancy, our daughter Lily and I -- had never seen it. A genetic thing, I guess.
[May 5, 2019]
A couple of days ago I did another evaluation flight and requested a PAPR report from the FAA. It came back with exactly the same fault as before I changed transponders, and not only the same fault, but almost exactly the same percentage of non-received Mode 3A squawks. This time, however, I heeded the advice on the FAA site to contact them before heading off to the radio shop. I got a very prompt and nice reply saying that the dropped squawks were due to being at low altitude or behind mountains or otherwise out of coverage, and my equipment appeared to be working fine. So I guess I can start thinking about something else for a change.
[April 24 , 2019]
Success! Today everything worked. Or let's say, at least, that I was unaware of the things that were not working.
[April 23 , 2019]
Installing the new transponder was more of a job than I anticipated, but after a day of fumbling around I got it and the wire harness installed. The Narco transponder used 12v power, and required a power converter; the Garmin is omnivorous, and so the connection between it and the bus had to be rewired. The power converter remains in service for a few other 12v things. Making the new connector for the Garmin turned out to be the simple part; I got a beautiful little crimping tool online for $30, and putting the right wire into the right hole was not much of a challenge, except in one instance where, in the twilight of my years and workshop, I mistook a dark brown wire for a black one and as a result deprived the altitude encoder of its ground. When I first powered up the transponder yesterday it was not displaying altitude -- this was due to the missing ground -- but appeared otherwise correct. When I got into the air, although the "reply"indicator was blinking in a realistic way the tower was seeing no return. Today I fixed the missing ground and re-installed the fitting on the transponder end of the antenna cable. The transponder now displays altitude -- correctly, to boot -- but I ran out of time and will test fly it tomorrow.
[April 12 , 2019]
One of the two intercooler tanks is now done. Unfortunately, I took a second look at the heat exchanger core that I had decided not to use, and I began to think that I might be better off with it than with the one I had first chosen. It's shorter, and will give me a little more freedom in arranging the parts of the system and their associated ducts. That means that the tank I have made is too long; but it will not be difficult to shorten it, and also the mold for the other, if that is what I decide to do. In the meanwhile, after what seemed to me a torturously long delay, I finally got the Garmin 327 transponder, which is supposed to be the solution to the Tailbeacon-related issues, and have been making up the wire loom for it and installing its remarkably stout steel rack in place of the AT-50A's aluminum one. I hope to be flying again by the end of next week. The airplane has not been in the air now for more than a month.
[March 22 , 2019]
I finally got back to the intercooler project after 10 months of idleness. The first of two layups of the outlet "tank" appears to have been a success, to the extent that 1) the epoxy hardened and 2) the part came off the mold without my having to destroy either. The part consists of four plies of glass with carbon fiber facings on the inner and outer surfaces of its relatively flat back. It's laminated with a high temperature Hysol epoxy. A second portion will be laid up covering the underside of the round tube, and overlapping, but not bonded to, the first. The final operation will be to bond the two parts together around a short length of aluminum tubing, without the male mold inside. The parts for the inlet tank are broadly similar.
Paul Lamar, the rotary engine advocate, gave me a bunch of books, including the classic Kuchemann and Weber text on internal flow systems. It reminded me of what I already knew -- because I made the oil cooler outlet duct that way -- but evidently forgot while I was designing the intercooler outlet tank, namely that while the inlet (that is, the high-pressure side) can be wedge-shaped, the outlet should be more like a rectangular box with equal clearance across the whole face of the heat exchanger. The effect will be to make one end of the intercooler less effective than the other. The whole thing is probably bigger than it needs to be, however, so the design is non-optimal from the start.
In the meantime, my transponder has been at High Desert Avionics at Fox Field for almost two weeks, waiting for an adjustment which I hope will allow the system to pass the FAA test. It almost passed on the second try, and what it did not do well was something that, if I understand it correctly, was due to the transponder, not the Tailbeacon.
[February 18 , 2019]
A correspondent who spoke with the Tailbeacon people told me that they pronounce it "you-Avionics", which is the least logical of the possibilities, unless they are trying to appeal to the "me generation". Another correspondent expressed concern over the thing being hard-wired on at all times, since that exposed it to voltage transients on engine start. He suggested putting it on the avionics master switch. There was no avionics master switch -- the first Melmoth didn't have one either -- but I decided to capitulate and add one. This turned out to be easy to do, since all of the avionics breakers are in a single row on the breaker panel. I used the old master switch from Melmoth 1, which is a somewhat bulky thing that you have to pull outward to toggle, and I put it over on the right side of the panel, beside the breakers, on the theory that if switching the avionics on and off involves a somewhat unusual group of motions, I'm more likely to remember to do it.
[January 29 , 2019]
First of all, it turns out, when you look closely, that the name of the company that makes the Tailbeacon is not actually uAvionix but mu - Avionix, that is, Greek letter mu, meaning micro. So I don't know how to pronounce it. Is it you-avionics, mew-avionics, or micro-avionics? In any case, I tried an FAA acceptance flight, which basically involves flying around for half an hour and making a few 360-degree standard-rate turns. You then get online and ask an FAA computer somewhere for a report on the quality of your ADS-B out returns, and in a minute or two you get an email, which said, in my case, that the system did not meet the requirements.
The next step is to use a cellphone app to adjust the sensitivity until the beacon and the transponder get into sync. It requires having regular transponder interrogations, so I have to find an airport around here where I can be on the ground (the app works only on the ground) and the transponder is blinking. I changed some wiring around so that the tailbeacon and its integral tail nav light are always on when the master switch is on; only the wingtip lights are switched from the panel. While I've been fiddling with this, two unrelated things went wrong: the attitude indicator tumbled (and would not untumble on subsequent flights) and the Lowrance GPS went dark. I sent the AH out for overhaul; the problem with the Lowrance turned out to be a blown fuse. I don't know why it even has a fuse, since it's on a breaker; but anyway, I put in a new fuse and it's working again.
This is what the beacon looks like (the thing next to it is a halogen flasher that I use in lieu of a strobe):
[January 17 , 2019]
In December I finally sprang for an ADS-B out transmitter. I selected the uAvionix Tailbeacon for a number of reasons, not least its price of $1,600. Still, only a diamond ring would cost more and come in a smaller box. Its installation, which I did a few days ago, involves an absolute minimum of alteration to the airplane. It simply replaces the tail light. When it is installed on a TC'd airplane the nav lights have to be kept on at all times; I intend to separate the tail light power supply and ground from those for the wing lights and run only the tail light/beacon continuously. I don't know how the thing works, but I assume that it just listens for a squawk from my extremely legacy Narco AT-50 transponder, and when it detects one it tacks on a few extra syllables of its own to report my ID, position and altitude. I am hoping that my Stratus 1, iPad, and the Tailbeacon will keep me flying in the ATC system for a few more years. I heard some dire grumblings about this being the first step toward user fees, which general aviation has been opposing for the past half century or so. Maybe, maybe not. I remember when the transponder requirement was denounced as the final nail in the coffin of our liberties.
One question that people ask about the Tailbeacon is, if it's entirely self-contained and just screws onto the taillight mount, what's to stop somebody with a screwdriver walking off with it. Well, first of all it's associated with a particular airplane -- you program it through your smartphone -- and you need a secret password to change that. Furthermore, the two #4 screws that hold its mounting plate in place end up behind the antenna, so you can't get at them with a screwdriver. The gadget itself locks into the base with two tiny allen screws, and unless I am mistaken they are either metric or of a strange intermediate size, because only the wrench that came with the beacon was able to engage with them.
It might be easier to steal the propeller.
[January 10 , 2019]
Looking through some old files, I came upon a letter that Mike Melvill wrote in 2002, when he was helping me fly off the 25 hours to get Melmoth 2 licensed. In it he reported the results of some speed tests. I thought it would be interesting to compare these to present performance, so yesterday I went up to duplicate at least part of his tests. I quickly realized that this could not be a very meaningful exercise, because at the time he did the tests the airplane did not yet have static ports, relying instead on cabin pressure for a static reference. Cabin pressure is generally below ambient because of leakage around the windows into the low pressure around the canopy, and so his results would be on the high side. Furthermore, at that time the airplane did not yet have a fuel flow meter, and so a direct comparison with the way I determine power setting today was not possible. Mike had recorded both fuel pressure and EGT, but much had changed about the engine since then, and I was now unable to duplicate his conditions. I gave up the intended comparison for a lost cause, but I did record a series of speeds at a density altitude of 11,000 feet, 2,500 rpm, and manifold pressures from 18 to 28 in. Hg. Not surprisingly, these coincided well with my computer model, which at this point does a pretty good job of impersonating Melmoth 2. Eleven gallons an hour, or about 75% power, produced 190 knots true airspeed. This would go up to around 197 ktas at 18,000 feet at the same fuel flow. Too bad; an even 200 would be nicer. Maybe if I ever get around to making the tires narrower. From the point of view of comparing 2002's performance with today's, the outing was a bust, but it proved fiscally fortunate: I stopped for fuel at Santa Paula, where I bought 30 gallons at $3.99 a gallon. I later ran into my hangar neighbor Claude Morgan refueling his exquisite 210-hp Swift at the Whiteman gas pit, where he had just had to pay $5.49 a gallon for the same stuff. A week's worth of visits to the local espresso joint!
[January 3 , 2019]
It's been a month since I last flew, owing in part to the Christmas holidays and in part to the failure of the batteries to hold a charge. I decided that rather than coax a little extra life out of the batteries by keeping them on a "battery tender," a supposedly useful practice that did not work out well for me when I tried it seven years ago, I would just replace them. This led to visits to four AutoZone stores, which have netted me so far one battery out of the required two. The hunt continues today. I contemplated switching from wet batteries to the sealed kind, which are more expensive ($100 each vs $60) but preferable in several respects. I was deterred by the sealed ones' not having exactly the same terminal geometry as the wet ones. Since my plane has solid connections in the battery box, it accepts only one style of battery. I may have to change that; I got the impression from the selection of batteries on display that sealed ones are more prevalent than the other kind, perhaps because motorcycles get laid down from time to time. One of the AutoZone guys said, by the way, that three and a half years was a good life to get out of these batteries; they usually last two. Hence the name "Duralast."
In the department of ludicrous blunders, I installed a microswitch to produce a bleat when the flap reached the takeoff setting, ie lots of area-increasing aft travel but little deflection. I thought I had the microswitch in the right location, but on the second flap retraction the roller went to the wrong side of the rod end over which it was supposed to ride, pretzelizing itself.
[December 19, 2018]
My Duralast motorcycle batteries have stopped holding a charge, at least for more than a few days. They're three and a half years old, so I suppose, since they cost about half what a 28-volt aircraft battery costs, I should not grumble. My previous Yuasas lasted just three years.
[December 5, 2018]
A couple of windstorms blew a lot of fine silty dust into the hangar, where it settled on the airplane. Today was showery, and I went flying in hope of getting some interesting streaks in the dust. I was lucky, in that there was enough rain to make streaks but not enough to wash the wings clean. After landing I took a number of pictures that reveal interesting details about the boundary layer flow. A few of them follow. The contrast has been exaggerated considerably to make the effects more visible; the airplane was not really covered with so much dirt that you could plant potatoes in it.
In the first picture, taken from the left wingtip looking toward the fuselage, the extent of laminar flow can be seen from the fact that the skin is clean from the leading edge back to around 40% of chord. This may not represent the true extent of laminar flow on the clean wing, however; the rain and dust themselves accelerate transition.
The next picture shows the right wingtip. The extent of laminar flow is much smaller, in part, at least, because leading edge sweep makes it more difficult to maintain. It's instructive that there is a pool of separated flow in the bend, where the pressure recoveries on the wing and the upturned tip form a mildly divergent channel.
The third picture shows another area of dead air, this time the upper surface of the aileron. The boundary layer evidently thickens significantly, or separates entirely, aft of the gap.
The next picture illustrates a curious phenomenon: spanwise flow near the trailing edge. The flow direction is inboard on the upper surface and outboard on the lower, and is related, I assume, to spillage at the tip and to formation of the tip vortex.
Finally, here is the flow around one of the flap track fairings. It's interesting that the flow does not hug the fairing, but seems to spread out away from it. There must be a pool of low-energy air close to the intersection. I don't know whether more of a fillet would improve the situation; I doubt it. In this picture, as in the first one, the transition from laminar to turbulent flow is visible.
[November 1, 2018]
It seems remarkable that this year had no October.
After making and breaking a number of appointments I finally got the propeller balanced per the recommendation of Art at Able Air back in June. I approached this operation skeptically, feeling that the idea that you ought to balance your prop every 500 hours was like the advice of shampoo manufacturers that you apply the stuff liberally and twice. But I tend to make the miser's assumption that everyone is out to swindle me. The traveling technician who performed the operation was named Leo Chrisostomo. Had I know this in advance I would have been even more suspicious, since the name, which means "golden-mouthed," suggests someone particularly persuasive and therefore potentially misleading. Leo connected a couple of what I thought looked like accelerometers, but he said were now called "velocimeters" (I think), to the front and back of the crankcase and had me run the engine at 1,700 and 2,000 rpm. An oscillograph made squiggly lines. Leo's expression suggested that he found the results a little startling. My engine, it seemed, was very far out of limits, registering 1.5 of some unit or other when the allowable value was 0.2. If this had been PSA, relatively speaking, I would be a goner. I was puzzled that the engine could be so far out of whack and yet feel so smooth, but he said it was all in the Lord mounts. Thanks be to thee, O Lord, as St. John Chrysostom probably used to say. He screwed a couple of weights onto the prop hub and we tried again; now the excess was merely half of what it had been. Another pair of weights and the engine was within limits, if just barely. We stopped there. I took the plane around the pattern and indeed it felt different -- silkier, as it were. Probably well worth the $300, especially if it prevents another alternator going to pieces on me.
After all the thinking about the flap position buzzer back in September, I decided to try the simplest of all options, namely a buzzer and a microswitch, nothing more, with the thought that in the time it takes me to react to the buzzer the flap will have continued past the microswitch anyway, and so there may be no need for additional ingenuity to keep it from buzzing interminably.
[September 14, 2018]
I dropped the plane at Able Air yesterday with trepidation, but Art called me a few hours later to report that the mag problem had simply been a plug "packed with carbon" on the #3 cylinder. Evidently my carbon-detecting skills are poor, since I had inspected all the plugs and not recognized this condition. I wish I had been there to see what it looked like. He suggested that I lean the mixture while taxiing, something that I know is desirable but have lazily neglected to do. The bill was $90, to my great relief.
[September 11, 2018]
A kindly correspondent pointed out that in original version of the circuit below the capacitor should have been in parallel with the Sonalert, not in series with it. Russ Hardwick was innocent of this error. It was sheer stupidity on my part, like thinking that you fill a bottle from the bottom and empty it from the top. I have now corrected the sketch.
[September 7, 2018]
Matters have been temporarily derailed by a 200-rpm drop on my right mag. I inspected all the plugs, found nothing remarkable, and put everything back together. No improvement. The shop I am currently annoying with my business, Able Air, can't look at the plane til next Thursday. Maybe that will encourage me to make some headway on the intercooler tanks.
Last week Russ Hardwick and I discussed how to design a circuit to produce a tone lasting one second or so any time the flap passes, or stops at, the takeoff position. I felt that I understood at the time, but now I have forgotten again. I think there's a microswitch or a reed switch, a relay, a capacitor and a Sonalert, and you just connect them in all possible ways, one after another, until you get the desired effect. Just kidding. Actually, I think this is the circuit. I just need to figure out the right size capacitor for the Sonalert. The behavior of the circuit relies on the capacitor filling up much faster than the relay actuates.
[August 15, 2018]
A simple audio tone to announce the arrival of the flap at the takeoff position would make it unnecessary to watch the flap going up or down.
[August 13, 2018]
I happened to see a professional test pilot's evaluation of a certain airplane whose flying qualities are generally admired. He roundly rejected it for a training role, judging a number of its traits UNACCEPTABLE. I began to think about how Melmoth 2 would fare under such unsparing scrutiny, and I concluded that there are many obvious faults which I had simply agreed with myself to overlook.
One is the way the flap operates. To raise or lower the flaps, you move the flap handle to the up or down position until reaching the desired flap setting, then re-center the handle. (The gear works the same way). The handle operates a cable loop that goes to a valve. It also carries a two-lobed cam that triggers a single microswitch to operate the hydraulic pump. There are, for practical purposes, only two flap settings, takeoff and landing. For takeoff, the flap extends aft but deflects only a few degrees, producing a large area increase but only a small change in drag and pitching moment. Because of the long distance traveled (15 inches at the wing root) the flap takes about 12 seconds to reach the takeoff setting. It takes only two more seconds to get to the full (30 degree) deflection. (You can see this here and here.) Because of the rapid increase in drag and pitching moment associated with flap deflection beyond the takeoff setting, the pilot's attention is diverted (most critically, while setting the flap to the takeoff position at the start of a landing approach) by the task of monitoring the flap travel. Also, after takeoff, while retracting the flap, I tend to watch it while waiting to shut off the hydraulic pump, even though it does no harm for the pump to run for a few seconds against its own bypass valve, which emits a faint but useful scream of protest. (I have an unfortunate tendency to anthropomorphize machines; for instance, I don't like to keep my computer waiting.)
Landing gear operation involves similar deflections of pilot attention, but for shorter periods; the gear cycles up in five seconds or so, and down in two.
Lying on my back on top of Mt. Wilson last night while watching the generally disappointing Perseid meteor shower (imagine the even greater disappointment of the fellow who installed a 100-inch telescope there, only to notice, too late, that Los Angeles was just below) I mulled over how to mitigate this situation. During the retraction cycle, I would like the hydraulic pump to automatically stop when the flap is fully retracted; during extension, I would like it to stop at the takeoff setting. But then what? The flap handle is already down. There could be a pushbutton next to the flap handle that would override the limit switch and let the flap run down to full deflection.
There is a problem implementing this seemingly simple arrangement, however. The same microswitch on the flap handle energizes the pump during both up and down cycles, so whatever happens on the trip down will happen on the trip back up. Do I want the flap to stop at the takeoff setting when I'm trying to retract it? Well, maybe yes. For a go-around, for instance, that would be desirable.
But there is a bigger problem. At present there exists a clear, unvarying relationship between the position of the flap or gear handle and the state of the hydraulic pump. But once you add "logic" to the system, in the form of a second microswitch overriding the first, you introduce weird new possibilities. For instance, suppose the flap handle is down, the flap is at the takeoff setting and that limit switch has turned the pump off. Now I lower the landing gear. The gear handle microswitch now energizes the pump; fluid goes to the gear and to the flap as well (because the handle is down), the flap moves past the limit switch and runs down to full. Or the inverse would occur if the flap handle were up. Either effect would be highly undesirable and potentially hazardous.
There are certainly ways around such difficulties, but they involve increasing complications, make the system harder to understand, and create new modes of failure. Maybe a better approach would be to not let any professional test pilots evaluate the airplane.
[July 31, 2018]
I have accomplished nothing at all lately. Most days have been sucked up by writing, kid transportation or hot-weather laziness. When an empty day presents itself Nancy and I drive up to Ojai to help our son Nick with his house, into which his family intends to move in less than three weeks. Nick and I did fly down to Jacumba, on the Mexican border, on the 20th, to look at his '68 Malibu, which is being refreshed there like Aphrodite at Paphos. The trip down was a bit crawly, but on the way back we had a 20-knot tailwind at 12,500 feet, it was very clear and smooth, and we crossed right over the top of the LAX Class B and had a long fast dive to Santa Paula, where Nick had left a car. A long time ago I wrote about the pleasure of descending from 20,000 feet in Melmoth 1 and seeing 220 knots on the DME while listening to a favorite piece of music, and I mused about whether the pleasure might have been further increased had I had a slice of sachertorte to eat at that moment. I have since concluded that pleasures do not always add arithmetically, but sometimes tend to subtract from one another.
Jacumba is an odd little place. There are hot springs there, and our friend said that it used to be a resort of Hollywood types, like, say, Two Bunch Palms in "The Player". The recently paved 2,500-foot runway is right next to the border fence, a not especially forbidding-looking palisade through which a sufficiently svelte person could probably slip without much difficulty. It would be still easier, however, just to stoll over to the 1,000-foot gap about half a mile east of the runway, which would give the Clown in Chief a well-deserved conniption.
[July 3, 2018]
Late in June I sent away an oil sample for spectroscopic analysis. The last time I did this was in 2003, shortly after Melmoth 2 began flying. It's interesting to compare the results from two analyses 15 years apart. With the sole exception of copper, which went from 4 ppm to 6, all of the wear metals are present in lower concentrations now than when the engine came out of 20 years of storage. Aluminum went from 12 ppm to 2, Iron from 53 to 37, Nickel from 7 to 6 and chrome from 3 to 2. The engine now has 1,800 hours. At this rate it will soon cease to wear altogether, except for its copper parts. The oil analysis firm does not provide tolerances, except implicitly, through the use of decimal digits, which I have rounded for the sake of simplicity. But it says that all values appear normal. That was a relief.
[June 23, 2018]
In case anyone is interested in this sort of thing, the so-called "tanks" that conduct air into and out of the intercooler have to sustain an internal pressure equal to the maximum boost, as well as, on the inlet side, a temperature of around 250 deg. F. So part of the design process is to decide what "maximum boost" is going to be. If I wanted to be able to get 41 inches at FL180, where the ambient pressure is about 15 in. Hg, max boost would be 26 in. Hg and the pressure would be (26/29.92) *14.7, or about 12.8 psi. Realistically, however, I think I would be satisfied with 30 inches at 18,000 feet, which would provide 75% power. Being more frugal than impatient, I never use even that much anyway. So, (15/29.92) *14.7 = 7.4 psi. The area of the intercooler face is about 47 sq. in., so we get 348 pounds of pressure trying to blow the tanks off the intercooler.
[June 19, 2018]
The latest on the alternator coupler is that it is both a vibration damper and a shearable link. So much for that.
I put the alternator back into the plane on Saturday. I had a hard time with the transverse exhaust pipe, which passes behind the alternator and has to be removed to allow the alternator to come out. The pipe, which has the heater shroud wrapped around it, is straight, with a tapered flange at each end; the mating parts also have flanges, and these flanges are drawn tightly against gaskets by circular clamps with a V-shaped cross-section. The pipe looks as though it ought to be able to be put in either way, but actually the flanges on the two ends are of different types, one thicker than the other, and the flanges on the mating parts are as well. It turns out that you have to mix, not match, to get the clamps to work; if you put the two thicker flanges together, the V-groove can't handle them. I suppose I may have known that once, but if I did, I forgot it, and it took me about half an hour, and some bloodshed, to figure it out anew. Once I got everything back together, the alternator checked out fine on a runup.
I then decided to do an oil change, and to get a spectroscopic oil analysis while I'm at it, something -- the analysis, not the oil change -- I haven't done for 15 years or so. Things went fairly smoothly this time, since after last time's flood I wrote "Aft end" at one end of the trough that conveys the used oil into the bucket.
[June 15, 2018]
My supposition about the function of the wildly expensive coupling between the alternator and its driving gear was apparently incorrect. According to the technician at Aero Accessories from whom I picked up the overhauled alternator this morning, it's just a plastic connection designed to avoid dropping metal fragments into the engine in case the link fails. That makes it even harder to understand why TC asks $1,500 for the thing. But I wonder whether he's right. In any case, he said that failure of the outer case of the alternator is something they see maybe once a year. He assumed it was due to vibration wearing the aluminum threads, so that the steel bolts and safety wire all remain intact, but the whole structure comes loose.
[June 12, 2018]
Lacking a belt to damp the torsional vibrations of the engine, the direct-drive alternator requires a flexible coupling between its shaft and the gear that engages the accessory drive. After some number of hours of use, this coupling wears out. It is no longer possible to secure it to the alternator shaft with the required torque, and it must be replaced. This was the case with mine. Unfortunately, the diminutive item comes new from Continental for a cool $1,500. Reconditioned, they're $575 from AC Spruce. I think I've found one for $350, but it remains to be seen whether it will pass the torque test. This experience has reminded me that I am not really in the airplane owner demographic, and my flying career will last only as long as not too many expensive parts of my plane break at once.
[June 6, 2018]
I took the plane to Able Air this morning. The problem with the alternator turned out to be the alternator. In the seven years since I installed t, it had shaken itself to pieces. This is a little hard to understand, because the engine is quite smooth and I feel that the vibration level in the plane as a whole is low, but, as the mechanic said, you can never tell about vibration. Tomorrow I will take it to Aero Accessories at Van Nuys, where I bought it in 2011, for repair. What was surprising, and instructive, about this was that I had inspected the alternator before taking the airplane to the mechanic, and noticed nothing; but my attention was directed to the wire connections, and since the alternator itself was ostensibly intact, with all its bolts and screws and safety wire in place, it never occurred to me to grab the end of it and shake it to see whether it was coming loose from the rest.
The mechanic asked when I had last had my prop balanced. Forty years ago, I said. He suggested that every 500 hours would be a better interval.
[June 2, 2018]
I took off for Paso Robles this morning to attend the annual Antique Aero barbecue, but turned back after 20 minutes with the ammeter indicating a continuous five-amp discharge and the voltage meter just 24 volts. I've seen flakey behavior in the charging system before, including on the previous flight, but always the system would pull itself together after a few minutes and do the expected thing, that is, initially indicate a charge as the battery recovers from starting the engine, then gradually drop to zero charge or close to it and maintain a steady 28 volts. I made an appointment with Able Air (where I used to hangar Melmoth 1 in the Bob Eeg days) to troubleshoot the system on Wednesday.
I tested my old epoxy a few days ago; it's still good. I don't have much graphite cloth, however; I have to decide whether to settle for glass or spend some money. I'm tempted to use glass just because it's so much more cooperative. Graphite is so stiff, it's a pain on small radii like these. Maybe I can use a little of each; that would seem high-tech.
[May 25, 2018]
The intercooler inlet and outlet tank molds are ready for laminating. I need to find out whether my out-of-date high temperature epoxy will still harden, and whether I have enough carbon cloth for the parts (I suppose I could use glass; it's a question of stiffness, not strength, and so carbon would be preferable). More important, I need to figure out how to split the parts in order to be able to get them free of the molds. The molds represent the inner surface of the parts; in other words, the parts themselves will be laid up over these molds.
[May 14, 2018]
When I am thinking about the airplane here at home, I often refer to photographs to refresh my memory of the arrangement of certain details, particularly ones inside the cowling. This morning I began to reflect that the ambient pressure source for the injectors and mags -- both of which are pressurized by the turbocharger -- and possibly also for the manifold pressure gauge, is a tap in the duct leading into the throttle body, and that this tap is at a right angle to the flow direction. Since the flow speed in that duct is around 100 mph, there might be some pressure drop, and so I may not be getting full pressure. I consulted my photos and found, first of all, that I was wrong about the MP source; it comes from the crotch of the Y downstream of the throttle body. At least I think it does; actually, every one of my photos manages to hide that area, which resembles the pudendum of a putto, as modestly as those fortuitous bits of foliage and fabric in paintings of yore do the corresponding parts of Venus, Mars or Jesus. But it stands to reason that the MP pickoff would be downstream of the throttle; I was silly to think otherwise, however briefly. At any rate, I shall go to the airport today and visit the scene in person. Fortunately, my manifold pressure gauge has two needles, one of which tracks ambient pressure and provides, for anyone who can subtract, a crude but reliable backup altimeter. I can temporarily hook that one up to the pressure tap that goes to the mags and injectors; the two needles will show the pressure drop, if any.
[April 12, 2018]
The story of the Lowrance GPS continues, and never fails to amuse and astonish. The last time I reported on its behavior, in December, I had replaced its internal battery and it was now remembering to send position data to the autopilot; but it had stopped offering airports, NDBs and such stuff as Go To options, and was confining itself to waypoints, of which, incidentally, none were programmed. In addition, its map would display road, airport, position and track data, but not airspace boundaries. I was pretty well resigned to this state of affairs when one day it suddenly remembered its airports and NDBs. Then it would not search properly; it would go up to about the middle of the alphabet and then jump back to the beginning. After a couple of restarts, however, it abandoned that annoying behavior and acknowledged the entire alphabet. A couple of flights later, airspace boundaries suddenly appeared. It was like a stroke victim slowly relearning how to speak and walk. I do not know enough about electronics to understand how a device like this, which must have about the neurological complexity of C. elegans, can behave so capriciously, but I am glad to see that its fundamental impulses still exist, and are sound.
[March 28, 2018]
The ghostly lineaments in the previous entry are taking (as yet unfinished) form as wooden molds. The intercooler tanks will be laid up, using carbon fiber, over these molds. The one on the left is the inlet.
A kindly reader expressed concern about my long silence. Actually, I am well and so is the airplane. (The nation, maybe not so much.) I have done very little work on the plane lately, for several reasons. One is simply that I am in a period of slackened interest in working on it; my interest in various projects -- improvements on the airplane, repairs on my son's newly purchased house in Ojai, adding capabilities to my lofting/CFD software, translating a German memoir of my father's and editing another, working on a Melmoth 1 memoir of my own, and of course the usual article-writing and its attendant research -- rises and falls, and at the moment a lot of my free time is going into trips to Ojai and the translating and editing work. Plus, although I feel I am getting closer to the correct solution, I am still uncertain about some details of the intercooler plumbing. I am pretty sure, at least, that I have the position right. Here is the palimpsest upon which my runes are inscribed:
I do not expect this to be comprehensible; I am including it just to show that I do occasionally pick up a pencil or, more often, an eraser, and inflict something upon a piece of paper. The process has been somewhat impeded by my stupid choice of some redwood that happened to be lying around here as the material from which to make molds for the two high-pressure "tanks" that bring air into the intercooler and conduct it thence to the throttle body. Redwood is a material of constantly varying density, and singularly ill suited to mold-making. However, once I have made a mistake I am determined to persist in it. I am pretty satisfied with the inlet and outlet paths for the induction air, although the very tight 90-degree turn to the throttle worries me a bit, just in terms of its effect on flow distribution in the log manifolds. The cooling air is a different story, but it, at least, I can defer thinking about until a later time.
[February 14, 2018]
I tried a different position for the intercooler, and I think it's better. The inlet path for cooling air is less obstructed, and the paths for the charge air both into the cooler and from the cooler to the throttle body (identifiable as an orange sleeve in the photo) are better aligned. But I am still waffling about the whole idea, in part because of the weight of the intercooler itself -- around six pounds. I think it's bigger than it needs to be. Someone cautioned me against sawing off one end of it, but I don't know what difference it would make if I did so and just bonded a new end plate to it with a mess of JB Weld. At any rate, the non-airplane aspects of my life have been more than usually complicated lately, and I've spent less time than usual on the plane. So between lack of time and uncertain motivation, the intercooler is making no headway at all.
[January 28, 2018]
Moving at a more than usually glacial pace, I mocked up the intercooler placement, using wood wedges in lieu of the eventual "tanks". I don't like the arrangement, now that I've seen it, and am going to try a different one, with the large face of the core horizontal rather than vertical.
After writing an Aftermath column in which the cause of the crash was the pilot's faulty handling of an aborted landing, I became curious about whether Melmoth 2 could climb with full flap and airbrake -- one of many things that I have never tested. I tried it, and found that at 70 kias I could climb at several hundred feet a minute at 26/2800, which is nowhere near full power. (The airplane was extremely light, however.) The only problem was heating; the CHTs rose rapidly because of the low airspeed. The proper technique for a go-around would be to maintain level flight initially while cleaning up and accelerating. The pitch changes with airbrake and flap retraction are quite marked, but easily managed if you're prepared for them.
[December 30, 2017]
I collected some temperature readings in the duct leading into the oil cooler, with and without the deflector. The temperatures were, on average, 20 degrees F above ambient with the deflector and 30 above without. This suggests that maybe I ought to look into making up some sort of duct that runs directly from the peripheral intake to the oil cooler; at present the oil cooler duct takes in a mixture of deflected cold air from the peripheral duct and warm air from the plenum. Incidentally, these data were collected while cruising at 4,500 feet at 144 ktas on 6.8 gph -- another example of the airplane doing better than expected at very low power settings -- 25/2100 and way LOP, in this case.
Today the unpredictable #1 Lowrance worked, to some extent. Now that I have replaced its internal battery, it remembers that it is supposed to be producing NMEA output for the autopilot coupler. On the other hand, it seems to have forgotten its airport and navaid data, and now offers only user waypoints in response to the "Goto" command. I suppose it would not be that much trouble to program the waypoints I use most often. But would it remember them?
[December 2, 2017]
On the theory that air directed along the bottom inner surface of the cowling by the splitters I installed in the inlet might be sticking to the surface for Coanda-like reasons and not getting into the oil cooler inlet duct, I installed an aluminum deflector on the floor of the plenum in such a way that it would steer this putative river of cold air into the duct. The first time I tested it in flight I got the impression that it had had a remarkable effect; but as time went on the effect appeared to vanish. The only way I will know for certain is by measuring the temperature in the duct with and without the deflector in place.
My seemingly successful installation of a new battery in the #1 Lowrance has resulted in a unit that remembers its settings, but refuses to lock onto a satellite, even though it passes its self-tests okay. Meanwhile, the #2 unit, which is currently installed in the airplane, has developed a new problem: it remains on for only a few seconds after startup, and then turns off. I suppose it is foolish of me -- perhaps I am a deranged US dotard -- to suppose that electronic devices almost 20 years old can be expected to function normally.
[November 19, 2017]
Here's another plot of the same data, this time temperature rise versus net boost pressure above (or below) ambient. Different altitudes produce scatter, but on the whole the points line up fairly well.
[November 18, 2017]
Yesterday I collected some baseline data that will allow me, at some future time, to assess the effectiveness of the putative intercooler. I recorded induction air temperature at 20, 25 and 30 in. Hg at 4,000, 8,000, 12,000 and 14,000 feet. I had intended to finish the series at 16,000 feet, but it became apparent that the temperatures were getting quite high and I did not want to venture past 200 deg. F.
Here are the data I collected:
The left-hand chart is simply the right-hand chart minus the OAT.
The astute viewer will wonder why the temperature rise is so large even at low manifold pressure and low altitude, where no compression at all should be taking place. The reason is the peculiar design of the Piper "fixed wastegate" system that I have modified to incorporate a manually adjustable wastegate. The bypass is only 3/4" in diameter, and so even at low power a significant amount of exhaust gas is going through the blower, which is pumping against a partially closed throttle. This is an inefficient arrangement, obviously, but by using low rpm (these tests were run at 2,300 rpm, but I often go lower) I can open the throttle fully at 8,000 feet or so. I seldom cruise lower than that -- more usually above 10,000 feet. It's evident, anyway, that there's a good deal of heat to be gotten rid of.
One question on my mind was whether I needed to provide a separate cold air intake for the intercooler, rather than use the air already in the "cold" plenum. The temperature near the firewall is about 45 deg F above ambient -- this due to heating by the exhaust pipes and the turbocharger. Assuming 50% efficiency (I think this is the wrong term; it should be 'effectiveness'; but it's the one they use, and simply means the temperature drop across the intercooler divided by the temperature difference between the charge air and the ambient air), that would mean 22 degrees less temperature reduction if cowl air were used. But it might be worth a try, nevertheless.
[November 16, 2017]
Goaded by Peter Lert, I broke the solder joints to the dead battery in the Lowrance and extracted it, a 3v Renata CR2450N valued at $2. Following his advice, I crammed a new battery in with padding to press the contacts against it, and voila, it remembers! But -- can it be TSO'd?
[November 15, 2017]
My design process has always involved obsessively thinking about the object to be designed. I remember, during the construction of Melmoth 1, intensely visualizing the retraction linkage for the main landing gear while meditating at the Cimarron Zen Center of Rinzai-ji. How, I pondered, is the gear koan to work? I am now at the same stage with the intercooler. My recollection of the details of the engine compartment is not so complete or exact that I can mentally map every attachment and duct path, but I have dozens of photographs of it to help me. A number of criteria must be met. The intercooler must be able to be built piecemeal, without having to ground the airplane for long at any stage. It must be easy to remove, with as few attachment points as possible, and have short, direct flow paths. It must require moving or damaging as few existing items as possible. My mental scheme is like a rapidly oscillating object that at first appears blurred, but, as it slows, acquires sharper outlines and at last halts in place.
The most suitable location for the heat exchanger seems to be on top of the present induction air box, rotated so that the aft inboard corner touches the firewall while the aft outboard edge is about an inch and a half from it. The firewall thus forms the roof of the wedge-shaped "tank" that feeds cooling air into the core. On the opposite side, a similar tank (for that is the name of the end housings through which air enters and leaves), also deepest at its outboard end, collects the heated air into a 3-inch SCAT hose that discharges forward into the upper plenum. A third tank, on the bottom surface of the core between it and the induction air box, is connected to the existing riser coming from the turbocharger; on top of the core, a fourth tank feeds the cooled air to the throttle. In this arrangement, the intercooler is attached to the airframe, not the engine, and three flexible segments are required to join it to the engine. (I am reluctant to attach such a large, relatively massive object to the engine.) I have not yet found out how much cooling air the intercooler requires. A turbonormalized Bonanza has a ram air intake about 3 or 3.5 inches in diameter, but unless the velocity ratio in the duct happens to be 1.0, that tells me little about the actual mass flow. I had thought about constructing a pitot-style inlet with a boundary layer channel, but I decided it would be rather complicated and possibly draggy, so my present thought is to replace the existing NACA scoop in the cowling side panel with one about three times larger. This would supply both induction and charge cooling air. I'm not sure what the politics of splitting the inner channel of a NACA scoop are, but I'll find out. The most difficult part of the whole project, I think, will be making the induction-air tanks, which have to withstand both heat and pressure.
In the meantime I attempted to break into one of my Lowrance GPSs, having learned from the company that they no longer support such ancient devices as mine. There are no external screws on the case, which seemed to be glued shut. I cracked the joint with a chisel and pulled the halves apart sufficiently to see the battery that maintains the device's memory. Unfortunately, it is soldered to the circuit board, and so there is no practical way to replace it.
Incidentally, Monday, 11/13/17, was the last day, until almost 90 years hence, whose date is written (in the US, at least) as three successive primes.
[November 8, 2017]
I talked with someone who knows something about intercoolers. The guidance I came away with was that 1) I should not try sawing off the end of an intercooler core; 2) small differences in size are not critical, since the original choice of a size was probably based on false assumptions in the first place; and 3) the cooling air flow requirement is about what fits in a 3-inch SCAT hose. Ah, the cool, fresh air of simplification!
[November 6, 2017]
The puzzle of the failure of the autopilot to couple to the GPS is solved. The problem seems to have been related to the Lowrance's having lost the memory that restored its previous state at each startup. One of the settings that were being lost on each shutdown was "NMEA On" -- that is, the command to send course deviation information to the autopilot. If I reset that selection on startup, the system works as expected. The failed memory is presumably sustained by an internal battery, and that battery has evidently lost its ability to hold a charge. I assume there is a way to replace it, but so far I have not even figured out how to split the case. I will.
My vague plan to install an intercooler has advanced to the point that I have more or less decided where it will go. The next step is to find out whether I can make one of the heat exchangers that I have smaller by sawing off one end of it. I have three cores, one of which was originally intended for a 250-hp engine, one for a 310-hp, and the third for a 72-hp McCulloch two-stroke. Obviously, the last is too small, so forget about it. The others are too big, and for reasons of weight, space and internal resistance it is probably not desirable to have excess intercooling capacity. At any rate, I need to figure out how big an intercooler is appropriate and what volume of cooling air it will require. Probably the 250-hp one (for example) was sized for 75% power at the critical altitude, say 18,000 feet. I never fly at 75% power (except for takeoff), but I suppose the airplane should be capable of meeting the needs of some other pilot, since it is likely to live longer than I. I have not located any strict rules for sizing intercoolers, so for the time being I am supposing that I would use 80% of the 250-hp one or 65% of the 310-hp one.
[October 11, 2017]
The borescope did not find anything obviously wrong with the #4 cylinder. It did make a nice portrait of the top ring gap reflected in the polished cylinder wall:
I ran the engine for a few minutes and then checked the compression of the #4 cylinder again. Now it was 72/80 rather than 40/80. I thought that 40 didn't seem likely.
[October 10, 2017]
At the end of the eclipse trip, which involved about eight hours of flying, there was a fine mist of oil on the right side of the windscreen, enough that I could not see clearly through it. The oil consumption had not been out of the ordinary -- about one quart in 10 hours. It was evident from that, and from the fact that the mist had not coalesced into large droplets or streaks, that the amount involved was small, but evidently from some new source, since I had not seen this problem before. I was thinking that I would carefully clean the right side of the engine and then check it after each flight to locate the leak; but it was became clear, as soon as I removed the cowling today -- various things had prevented me from getting to it sooner, though I had flown in the meantime -- that the leak was coming from loose joints in an elbow in the 3/4" pipe that conducts air from the oil separator overboard. Lengths of aluminum tubing were simpy slipped into the elbow without any kind of positive seal, because I had thought there would be very little pressure in that line. I now contemplated cutting O-ring grooves in the elbow, but settled for gluing the tubes into it with red silicone. I then did a compression check (for the first time since January, 2014 -- "If it ain't broke..."), and found that the #4 cylinder was holding only 40/80. This seemed odd, since the others were still in the mid-70's and one was 80/80. I suspect that there may be some little speck of carbon or something under a valve, and that if I fly and then check the cylinder again I will find it in line with the others. In the meantime, however, I will examine it with the digital borescope that I got some while ago for $18, and have never yet found an excuse to use.
I had the Porcine Smart Coupler benched checked by its maker, and he reported that it is okay, which, he said, was too bad in a way, because troubleshooting the rest of the system will be more difficult. I may have to give up the Lowrance GPS, whose behavior has grown increasingly flaky, and replace it with something newer. Unfortunately, the iPad, which provides a beautiful navigational display, does not provide the digital output required to link it to the autopilot.
In the meantime I have been toying with the idea of installing an intercooler. I have toyed with this idea before, but never gotten past the toying stage. I have several intercoolers lying around, none of which will be suitable for my 200-hp engine without modification. I don't think I have any practical need for an intercooler -- I seldom go above 14,500 feet -- but I would do it, if I do it, just to round out the tubosystem.
[September 25, 2017]
A highly compressed video of the eclipse trip is here.
[August 23, 2017]
The curious pattern of light on the instrument panel -- and everything else in the cabin -- was, I think, a schlieren image of density variations in the plexiglas of the canopy.
[August 22, 2017]
The universe was kind enough to schedule a solar eclipse on my birthday, so on the 20th my son Nick and I flew up to Winnemucca, Nevada, where we spent the night before continuing to above Weiser, Idaho. There we observed, or perhaps a better word is experienced, the event from a perch at 14,000 feet.
Enough has been written about this eclipse that I will not add my two cents, except, first, to explain that the tawny line along the horizon in the photo above, taken at 11:26 a.m. MDT from the middle of the umbra, was due to smoke from fires in Oregon, and, second, to note a curious optical phenomenon whose cause I do not know. I suppose it must have something to do with the plexiglas canopy, but for some reason the only time I have ever seen it was just before and after totality in this eclipse. All surfaces appeared pebbly or rumpled. The paper on my kneepad looked as if it had been soaked in water and then dried, and the instrument panel resembled the surface of a hilly, eroded landscape.
[August 14, 2017]
The house work goes on, but on Saturday I woke up early and slipped away to the airport. I was obsessed with wondering whether there was a way to get the leaky nosewheel hydraulic cylinder out of the airplane wihtout having to dismantle everything surrounding it, which requires jacking the airplane and is a big pain in the neck. The freeway was conveniently empty, the airport dim and silent. I quickly found that yes indeed, there was a way; and in ten minutes the cylinder was out. I opened it up and inspected the O rings; everything appeared okay. I left it on the workbench for further inspection. As I was leaving the airport I heard a plane heading down the runway, and I glimpsed it as it began to climb out. It was an airplane I always see parked, but had never before seen move: a Scottish Aviation Bulldog, quite a rarity in the US.
[August 8, 2017]
I flew today for the first time since June 27. I have been completely absorbed in house repairs, but they are finally coming to an end. I went up to Tehachapi, a bit less that half an hour away, where Mike Melvill has his hangar. I circled overhead but did not see his car; he is probably not yet back from Oshkosh and from visiting friends in Indiana, where he and Sally lived before they came to Mojave to join the then nascent Rutan Aircraft Factory. The Smart Coupler is still not working in spite of my having repaired a broken wire. On approach to Whiteman I found that the flaps would not work -- obviously low hydraulic fluid again, and on inspecting the usual leak sites I found that the nose gear hydraulic cylinder, which I thought I had repaired early in May, is again leaking copiously. I hope I can figure out a way to take it out without having to dismantle the entire nose gear retraction linkage again. This time the leak appears to be between the outer tube and the piston-end cap; last time I thought it was around the piston itself.
The one repaired thing that worked properly was the #2 radio.
[June 28, 2017]
It didn't take long to discover that the cause of the failure of the GPS to talk to the autopilot coupler was nothing more complicated than a broken wire. I fixed that. I then pulled the #2 comm radio, which I took home. Removing the fascia, I found that the plastic shaft connecting the Store/Select/Recall knob to its internal switch had failed where a shallow groove had been cut into it for a snap ring. Going by feel, I put, or at least I hope I put, the switch into the "Select" position, where it will henceforth remain. Another plastic knob, the tiny one that controls volume and squelch on the #1 comm, turned out to be cracked. I'll find a replacement for it.
[June 27, 2017]
I flew to Oakland yesterday, and there encountered an instance of the often forgotten fact that every feature entails a vulnerability. My comm radios are Collins Micro-Line dating back to 1975 or so. They're great radios and I have no complaint about them at all. One of their features, which was novel at the time (I think) but has since become standard, is a "Store-Select-Recall" switch that allows you to store a frequency for future use or to "remember" the current Center frequency before switching to the next one en route. In my radios, this is a rotary switch, and when I turned it something broke, leaving the radio in "Recall" mode and therefore incapable of selecting a frequency.
One interesting data point was that after climbing to 10,500 feet and cruising for a while, I decided to re-adjust the mixture. As usual I was running lean of peak, and I found that I had to enrich by 250 deg. F. to get to peak. So I now know that the engine will run smoothly at 250 LOP.
With reference to the June 16 entry regarding whether the iPad can talk to the Porcine Smart Coupler, which seems to be on the outs with the Lowrance GPS, as far as I can tell from discussions on line neither Apple nor ForeFlight provides an output of NMEA data to the autopilot coupler.
[June 16, 2017]
We returned on the 13th from Cape Cod, where we ended a trip that began in Mid-may with Nancy's 50th college reunion in South Hadley, Massachusetts. This was a three-day affair during which I met, among other people, a woman whose father, Charles d'Olive, scored five victories in Spads in World War I. Too late, sadly, to relate the encounter to my friend Javier Arango, who would have been delighted by it.
I flew for half an hour today after replacing my antediluvian Lowrance GPS with the spare that I got for $40 on eBay 18 months ago. I had been having two problems with the unit. One was that it often had to be restarted several times before it would show a complete map; initially it would leave out stuff like the boundaries of Class B or C airspace. The other was that it had stopped talking to the gadget that converts GPS course deviation information into autopilot commands. The replacement unit, once it had figured out that we were not in Tulsa, resolved the first problem but not the second. The second, however, is the more important, since the iPad provides a Technicolor map six times larger than the Lowrance's black and white one, but no autopilot output (at least that I know of).
[May 4, 2017]
Before leaving for the East on April 14, I overhauled my leaking left brake master cylinder. On returning, and after due delay for getting my affairs in order, I took the nosegear retraction apparatus out in order to fix a leaking hydraulic cylinder. While I was at it, I changed the oil. A couple of months ago I had made a permanent version of the temporary gutter that I hit upon in July, 2014 as a way to drain the oil without making a huge mess. Unfortunately, there are two ways to install it, and in obedience to Murphy's Law I unreflectingly picked the wrong one, with the result that two quarts of oil went into the bucket and six went onto the floor. Luckily I had a tub full of absorbent stuff, basically kitty litter I think, left over from the big fuel spill of January, 2015, as well as a pile of old clothes, sheets and towels that I had husbanded against just such an eventuality, and I was able to stanch the Stygian flood before it had advanced more than a few feet in several directions. The nose gear hydraulic cylinder turned out to have a prolapsed O-ring. I got everything put back together and cycled the gear today; no time to fly, however.
[April 12, 2017]
The iPad installation turned out quite well. On the first outing, it was free of reflections and perfectly visible as long as I did not look at it through my polarizing sunglasses, which make it appear completely dark. It's simply hanging from a hook and supported by one short leg, and can be removed as easily as a coat hanger from a rack.
I was taking a couple of visitors up for a short flight at the end of which the flaps would not go down. It turned out that the hydraulic fluid was exhausted, having leaked out of the nose gear auxiliary cylinder that I noticed dripping the other day. Fixing that will probably be a couple of days' work -- it will involve removing and replacing the whole nose gear retraction apparatus -- and I won't do it until we return from the East toward the end of April. Today, however, I did overhaul a leaking brake cylinder, apparently successfully. At a certain point there was a terrific racket outside the hangar; someone was running up a Stearman that appears, for the moment at least, to be my new neighbor.
[April 6, 2017]
In 1974, Gary Maker was a private pilot, an airplane enthusiast and a Flying reader. He lived in the San Fernando Valley, and one day was at Whiteman Airport -- "back when a person could just drive back there and watch the planes" -- where he saw the then much-publicized Melmoth 1 and snapped a picture of it. A few weeks ago he sent me this:
At that point the T tail and rear window mods had been done and the airplane was still unpainted. To judge from the clouds and the fact that the ground looks wet, this might have been taken in the late spring, but it appears to be of the same general vintage as another photo that was sent to me by Gino Barabani, and that has been in the "Melmoth 1, mostly pictures" section of this website for some time:
Recently Barabani wrote to me, "The date of this photo was 7-9-1974, it was a Tuesday. I flew my second solo cross country from Rialto to Whiteman Field in a Cherokee PA-128-140 N7303F just to see your aircraft. I read every article in Flying about your aircraft. This high school kid had to find out what kind of person could design and build their own aircraft, so I talked my flight instructor into letting me go to Whiteman field for my solo cross country. How sad that you where taxiing out just as I had arrived. The picture was taken with an old Polaroid camera; after the black and white picture was developed I had to run a clear liquid stick over the photo, so I never saw where you went."
[April 5, 2017]
I finally completed the iPad mount that I started thinking about in January. It looks good, but it remains to be seen how visible it will be; the transparent canopy is a powerful creator of reflections.
After landing the other day I noticed hydraulic fluid leaking -- what else is new? -- from the shaft O-ring on the small booster cylinder that is supposed to help the nosewheel along. I wonder whether that can be related in any way to the adjustment I made to get the nosewheel doors to close flush. It's hard to see how the two could be connected, since the leak is occurring when the gear is down, not up. At any rate, the change made the gas spring collide with the retracting arm, and so I have to revise the gas spring mount, which will require removing a bunch of stuff including the hydraulic actuator. I'll overhaul it then.
[April 3, 2017]
While I was away I formed the notion that I could make the main gear tire/fork assemblies narrower by machining some material off the half fork -- which is an aluminum forging that is stronger than my airplane requires -- and then moving the wheel a little closer to the fork. Unfortunately, it turns out that the brake caliper is already up against the inside of the door, so that is not an option. I suspect that the best solution would be a narrower tire. My original tires allowed the doors to close flush; I probably discarded them, but may have some carcasses lying around somewhere. Of course, there may be tires other than aviation ones that would fit these wheels. No doubt there is an All The World's Tires listing somewhere online. This has been a lesson, albeit one I am unlikely to have an occasion to employ: Leave some extra space around replaceable items, because the replacements may not be identical to the originals.
[March 10, 2017]
I flew to Santa Paula on Wednesday in hope of seeing a flight of the clipped-wing Harmon Rocket powered by a 650-hp turbocharged rotary engine that is supposed to make an assault, when conditions are right, on the time to climb record for propeller aircraft. The airplane was ready, but the pilot. who seems to lack confidence in the engine, was not. He wants 20 knots of west wind down the runway, and the day promised only 15. In fact, while I was there it was 10 out of the east. Paul Lamar, who is a huge advocate of rotary engines for airplanes and supervised the installation of this one, was just about tearing his hair out, since he has complete confidence in the engine, thinks the pilot's hesitancy is unwarranted, is certain that the airplane will easily better the current record, and can't wait for it to do so. I did take advantage of the trip to buy some fuel, which is a dollar a gallon cheaper there than at Whiteman, and to wander about a mile up for half an hour or so in perfectly smooth and perfectly clear air, admiring the scenery which, at the moment, is still a pleasing green after a period of unexpectedly heavy and persistent rainfall. After returning I peered into the wheel wells to see whether the idea of cutting holes in the floor to give the tires more clearance is practicable. It is not; the aft portion of the tire retracts against the upper cap of the rear spar.
[March 2, 2017]
I taped one of the wireless video cameras to the belly in order to see whether the nosewheel doors were closing properly. They weren't:
The odd-looking spike in the middle is a propeller blade. The object to the left is the exhaust pipe, and the one to the right is a fairing enclosing the engine breather and cloaca. The doors looked horrible, so today I jacked up the airplane and learned that the nose strut was not retracting fully and the tire was keeping the doors from closing. Fortunately, by shortening a certain link by a sixteenth of an inch I was able to get the wheel to retract fully and the doors to close perfectly flush. I noted, however, that the main gear doors were not closing fully either; they stick out a quarter-inch or more. That is a more difficult problem, because the tires are already touching the roof of the well and the doors are as close to the struts as they can be. The wheels retract under the seats, and there are already wells in the underside of the floor there to provide them with the greatest possible space. I believe that the back edges of the seats clear the floor by only a quarter-inch or so, so it may not be possible to raise the floor in the vicinity of the tires. Perhaps, however, I could cut two holes in the floor and seal them with rubber sheet.
[February 15, 2017]
A few days ago I replaced the paper filter element in the hydraulic system filter. I had expected this to be a troublesome job, because some time back in the 1990s an idiot using my body had installed the filter behind the instrument panel rather than in front of the firewall alongside the reservoir, where it obviously belonged. As it turned out, getting at the filter was not so difficult as I feared, and I managed to complete the job without spilling a drop of either hydraulic fluid or blood. The filter element was quite black. Here it is, like a patient etherized upon a table:
This is the sort of thing the NTSB has a field day with when it's found in a wreckage. The actual height of the strip is about 1.38 inches, and the spaces between the accordion pleats are about 1/4" wide. A closer look at about 20x magnification, its drama enhanced by Photoshop's "Auto levels" function:
To look at this you would suppose the hydraulic system would long since have failed, but it seems to work fine apart from occasional rebellions of the flap sequencer, which I pitilessly suppress. Where did all that finely-divided metal come from? There are 10 hydraulic cylinders of various sorts in the airplane, and a corresponding population of aluminum lines and flare fittings. I suppose the shiny debris represents the sum total of the fine metal dust that clings unnoticed to the insides of lines and cylinders fabricated and assembled under non-clean-room (to put it mildly) conditions. Or maybe the pump is disintegrating.
Apart from the eye-catching metal, the paper (originally a pale tan color) appears thoroughly clogged with black silt, which I take to be either extremely fine aluminum oxide dust or the wear products of Buna-N O-rings. Whatever the case may be, it appears that an inspection interval of less than 14 years -- well, 13.3, actually, no use being too hard on myself -- might be desirable.
[February 10, 2017]
Assuming that there must be some physical problem in the #2 (that is, left side, inboard) flap actuator, I removed first the actuator itself, then the master cylinder that drives it, and dismantled and inspected each of them. There were no problems that I could see; the O-rings were in good condition, as were the bores and the shaft surfaces. I put the system back together -- this whole cycle took about 8 hours -- and it worked correctly.
The problem was that the inboard end of the left flap had begun moving inward while the outboard end, as well as the entirely of the opposite-side flap, was going outward. This had to mean that back pressure in the exhaust side of the system was overcoming the pressure being delivered to the acuator by its master cylinder. This could happen only if there were a big leak -- and apparently there wasn't -- or if there were air, possibly at below-ambient pressure, in the line between the master cylinder and the actuator. There is a bypass in each master cylinder that is intended to restore the proper volume of fluid to the lines between the masters and their associated actuators, but for this action to occur the hydraulic pump must be allowed to run for a few seconds after the flaps are fully retracted. I have not been doing that, and I guess that may have been the root cause of the strange behavior. That, at least, is the straw at which I am now grasping, having had to discard the hypothesis of a faulty seal.
One thing that this adventure has brought to my mind is that the hydraulic fluid filter, which is in the exhaust side of the system just before fluid returns to the reservoir, has not been cleaned or even inspected -- note my self-exculpating use of the passive voice -- in 14 years.
[January 27, 2017]
Yesterday, after installing a new ELT battery, I went up for what was supposed to be a multi-purpose test flight. I had two cameras on the airplane, one under the left wing to check the closure of the main gear doors, the other on the canopy top looking down at tufts on the cowling top. It turned out to be rather choppy, in spite of being nearly calm on the ground, and so I didn't stay up long or do most of the things I had intended to do; it's a lot easier to fiddle with test equipment in smooth air. I did record an amusing but useless video of the landing gear retracting
and confirm that the main gear doors are reasonably flush (that's the airbrake to the left; this is on 3-mile final at Whiteman).
Now I need to point the camera at the nosewheel doors. I did not record the cowl top tufts, but I did observe them and noted that, as expected, they smooth out quite a lot when the cowl flaps are closed. I once measured a 2-knot speed difference between open and closed cowl flaps, but I don't have a lot of confidence in that number. In any case I think any speed difference would principally reflect the changing pressure drop across the engine rather than skin friction effects from turbulence on the cowling top.
There now seems to be a problem with my flaps. When I cycle them on the ground the inboard end of the left flap move inward when the flap is supposed to be going down. Hydraulics are inherently baffling, at least to me, but I think this must mean that there is a leak in either the master or the slave cylinder for the inboard end of the left flap. What is pushing the flap inward is the natural resistance in the vent lines. In flight, however, the behavior was different; the flaps went out in step, as expected, but halted before reaching full deflection; this could, I guess, be due to the aerodynamic resistance to flap extension (there is no resistance on the ground) causing the faulty O-ring to seat better. At least that is my hypothesis du jour. I at times wish I had operated the flaps with screw jacks and an electric motor, rather than hydraulically. I was concerned about the added weight of another electric motor, but I doubt it could have been any heavier than the synchronizer that controls the amount of fluid going to each of the four actuating cylinders.
Incidentally, it is interesting to compare two different presentations of the airspeed calibration curve from January 25. The left version looks pretty good; the right, awful. Same data, different first impressions.
[January 25, 2017]
Out of the blue Brian Gerdes, who has done my biennial pitot-static-altimeter certification for years but whom I was unable to reach earlier -- that's why I ended up going back to Vista in the first place -- called me yesterday and came to my hangar today. He has a beautiful RVSM-worthy all-digital testing rig that he said cost $25,000. He made a small adjustment to my altimeter -- basically just slightly shifting the 29.92 point -- and it passed the test fine. He affirmed that there is no connection between the 30-nm Class B veil and the IFR pitot-static cert; the latter is required only for IFR in controlled airspace. The VFR test is of the encoder-altimeter correspondence and accurate reporting by the transponder; the altitude tolerances are much larger than the IFR ones. Gerdes also mentioned that despite the name there is actually no pitot test; the reason the test plumbing hooks up to the pitot tube is that if it didn't, the ASI could be damaged by being driven against the high-speed peg by decreasing static pressure, which it would interpret as increasing airspeed. Of course, there is a leakage test for the entire system, which includes the pitot plumbing.
[January 22, 2017]
As far as I can tell, the authoritative-sounding old-timer and longtime A&P who told me that I could not fly VFR within the LAX 30-nm veil was probably wrong, as authoritative-sounding old-timers, including me, frequently are. I can find nothing in 91.411 that suggests that the altimeter cert is required for anything except IFR operations within controlled airspace, veil or no veil. I suppose the Los Angeles FSDO may have invented a rule of its own; I have emailed them to inquire. The irony of all this -- apart from the fact that I never fly at 1,000 feet below sea level, and don't know anybody who does -- is that I myself am incapable of holding altitude for any length of time within the tolerance required of my altimeter. In fact, if one may judge from several midair collisions that seem to have been the result of highly precise GPS navigation, too much precision can be a dangerous thing.
[January 19, 2017]
Turns out I can't settle for a VFR pitot-static certification, because Whiteman is within the 30-nm veil of LAX. I am now looking at a digital altimeter from MGL avionics, and, alternatively, the possibility of overhauling my Bendix. All this because it's off by 50 feet at 1,000 feet below sea level! While waiting for news on that topic, I am figuring out how to mount an iPad in the cockpit, to serve as the display for my Stratus. I think it will fit under the throttle quadrant, tilted toward the pilot. Reflections are likely to be a problem, however; they always are, with a transparent canopy.
[January 12, 2017]
Yesterday, after working two or three hours a day for three days, I finally got the wiring harness for the gear position indicator light finished. I can testify to what every child who received an electrical hookup kit for winter solstice knows: that there is a deep satisfaction, after stringing a bunch of wires and throwing a switch, in seeing a light go on.
My altimeter failed the bench test; as was the case in the airplane, it had zero error until it got below sea level, and by -1,000 ft got 30 feet out of tolerance. I am grateful that this discrepancy was detected before I attempted a CAT3A approach to Furnace Creek or Bar Yehuda. For the time being, I will settle for a VFR cert, which does not entail strict altimeter tolerances.
[January 8, 2017]
Well, at least the world is not quite so mysterious a place as I briefly thought. In fact, my external power socket is correctly wired; what was wrong was the A&P's statement, which I blindly accepted -- after all, he is an A&P -- that the middle pin is ground. Actually, in an AN2551 plug and socket the large end pin is ground and the other two are A+. And start carts probably don't have reverse polarity protection. Maybe airplanes do. So my stupidity consisted not in wiring the socket wrong, but in not being more sceptical of authority. It's my German blood that does it.
Incidentally, punctuation pedants like me will have paused over the sentence three back. The phrase "which I blindly accepted" would normally be set off by commas, but in this case it is immediately followed by another parenthetical phrase set off by dashes. What happened to the second comma? If I had used parentheses instead of dashes, the second comma would have followed the closing parenthesis. But it looks strange, I think, to place a comma immediately after an em dash. Style handbooks often differ about points like this; Flying's style book is not infrequently at odds with my opinions and preferences. It would be amusing to see what the copy editors there, sometimes nemeses, sometimes saviors, would do with that sentence.
[January 6, 2017]
The day before leaving for the East I did some static system tests, using a plastic syringe to draw down pressure, and satisfied myself that the leak was at the nipple on the blind encoder. The Tygon hose with which parts of the static system are plumbed makes a less tight fit with it than with the barbed nylon connectors used elsewhere. I trimmed half an inch off the tube and reinstalled it. That seemed to solve the problem. .
We returned from Cape Cod on Wednesday, shortly after midnight. Today, I took the plane back to Vista, confident that all would be well. But it wasn't. There was still a leak. The A&P and I spent quite a while hooking into the system at various points to ascertain where the leak was. I finally tried putting some Vaseline on the blind encoder nipple to seal it better. We ran through a few altitudes, and found that now the altimeter was out of tolerance at altitudes below the field elevation (the test protocol starts at 1,000 feet below sea level) but nearly perfect above it. This suggested to me that the flexible hose was expanding slightly, and therefore leaking, under pressure, and shrinking slightly under suction; but Dusty, the old-timer who owns Vista, said that it was because the altimeter never sees those low altitudes. I didn't understand his reasoning -- you overcome stiction by tapping on the instrument, and I didn't see how the frequency with which a mechanism visit this or that portion of its range would affect its accuracy. In the end, I removed the altimeter from the airplane and left it there for them to bench test.
In the process we checked the ASI against the one in the testing apparatus. I'm not sure how perfectly calibrated that one is, but at any rate I noted down a rough calibration curve for my ASI which suggested that it indicates 2 knots high around cruising speed and around 7 knots high at stalling speed. For various reasons I don't regard these numbers as definitive; for one thing, I didn't notice that the ASI on the testing device had a calibration card. It's hard to imagine that it's perfect at all speeds.
One startling discovery, which came about when we hooked up an external power supply to operate the transponder, was that I have the external power socket polarity reversed. This is astonishing for a couple of reasons. For one, it is a huge, and hugely inept, mistake to have made. But okay, I make some beauties. More surprising, however, I have had a number of start-cart starts in the 14 years I've been flying this airplane, and there has never been an indication of a problem. I can only surmise that start carts have protection systems that sense battery polarity and supply voltage accordingly. And even assuming anyone notices a warning light or whatever, once the engine is running and you're waving goodbye nobody runs after you to tell you your socket polarity is wrong.
[December 15, 2016]
The simulation below turned out to be accurate. I put the plane up on jacks and raised the gear, and the link cleared the repositioned down microswitch. I installed the up miscroswitch, and now just have to put in the LEDs and wire them. That will have to wait until next year, however; we're going to Connecticut and Truro for the holidays. Very few people, it should be noted, go to Cape Cod in December and January. Why could that be?
At the start of the week I took the plane over to Vista, one of the the local FBOs, for its biennial pitot/static/transponder certification. There appeared to be a leak somewhere in the static system, and the test had to be suspended until I find and fix it. I was stupid not to remove all of the test hoses that I've been using for measuring pressures; some of them were connected to the static line. After I got back to the hangar I pulled out all that plumbing; it had become a nuisance for passengers and was not providing any new information anyway. Tomorrow I'll see if I can find the static leak.
[November 30, 2016]
Providing gear position indicator lights has turned out to be more complicated in execution than in conception. In principle, it's quite simple. Since the three gear struts are mechanically interconnected, microswitches can be put anywhere in the system to report the state of the entire system. (Not, of course, if something breaks; but let us moderate our imagination of catastrophe.) For a designer, many options are an embarras des richesses, or, as we anglophones have it, too much of a good thing. The place I originally thought I would use turned out to be impractical; the three-lobed joint visible in the photo below is too far from the frame behind it to allow convenient mounting of microswitches, and the inner wall of the fuselage nearby is encumbered with plumbing and cables. Some other locations within the wings were disqualified by the comparative inconvenience of routing wires to them. I finally decided to use the bellcrank in the right wing root that drives the torque tube going to the nose gear, which has a convenient bracket for attaching the microswitch assembly. Over the space of two days -- which is to say about four hours' work -- I built the support for the "down" microswitch, only to realize that it might interfere with the rod linking the bellcrank to the right main gear retraction link when the gear is up. Fortunately, I have a digital model of the gear system and can incorporate objects in it to test for interferences. I found this:
The little rectangle in the middle is the microswitch; the diagonal line passing beneath it is the link axis. The actual link is half an inch in diameter (the microswitch, for comparison, is 5/8 x 1"). So obviously the microswitch has to move upward at least 3/8", and the bracket has to be made again. But that's no surprise. Projects like this always involve making a few parts several times. You could make another airplane, defective in every respect, from parts that I've discarded.
[November 17, 2016]
I flew to Catalina today with a 6-foot 5-inch passenger. The chronic problem of inability to see the main gear torque tube through the passenger's leg was particularly acute, since I have all sorts of experimental hoses and whatnot on the floor, and his legs were already bent like an unborn foal's. So here's a new project: gear position lights. This should be an extremely simple matter, since all three struts are mechanically interconnected, and so it is possible to know their position with reasonable assurance -- with as much assurance, at least, as I have now -- by consulting the position of the torque tube. Skimming through this document, I see that the last time I resolved to make this minor modification was in May, 2012, after I almost landed gear-up. Four and a half years' procrastination -- that's about par for me.
I find to my surprise that I do not have a very good photo of the torque tube as it runs along the right edge of the cabin floor, but in the picture below you can see the white tube, the two silvery isoceles triangles whose apexes meet when the gear is fully up or down, and, if you have extremely sharp eyes and/or a good imagination, a corner of the three-bolt hub joining two segments of the torque tube. This joint, right next to a fuselage frame, is a convenient place to attach a cam and two microswitches.
November 13, 2016]
Ah
love, let us be true
to one another! for the world, which seems
to lie before us like a land of dreams,
so various, so beautiful, so new,
hath really neither joy, nor love, nor light,
nor certitude, nor peace, nor help from pain;
and we are here as on a darkling plain
swept with confused alarms of terror and flight,
where ignorant armies clash by night.
[November 9, 2016]
Genesis 25:29
[October 18, 2016]
Yesterday I tried to record tufts on the upper surface of a cowl outlet vane with one of the two small video cameras -- the one that records to a chip. (Actually, both supposedly do, but I have only managed to get one to do it so far.) Unfortunately, the wifi connection quit as soon as I took off, and only resumed when I was back on the ground. I need to test its range; this camera has no antenna, unlike the other one. At any rate, I was reduced to attempting to photograph the tufted vane though the windshield with my phone camera. I also moved the wake rake to a position behind the right outlet and got a survey of velocities there. Here is the experimental setup; the camera is the tiny back dot at the apex of the triangle; the recorder-transmitter and battery are taped to the cowl top behind it. Although a few of the tufts appear somewhat aroused, the airplane is in fact standing still.
Here is the best picture I was able to get though the windshield:
And here is the velocity distribution at intervals of 0.5 in. behind the outlet, and next to it the scan of velocities on the upper surface of the vane; the values in the box on the right are the size of the opening at the aft edge of the cowl flap:
What to make of all this, I don't know. Evidently there is a layer of attached flow on the outer surface of the vane; the tufts there are lying down. It is not parallel to the direction of flght, however, but more nearly normal to the raked leading edge of the vane. This I already knew from oil streaks on the vane. Apparently there is an expanding plume of hot air behind the upper outlet, to judge from the longer tufts, which are taped to the upper lip of the outlet and appear to rise away from the cowling surface. They are waving around in a shear zone between the outlet flow and the free stream, however, and so a single snapshot does not tell the whole story. What is curious about the left-hand velocity scan is that the dynamic pressure at the test speed, 130 kias, is about 11 in Hg; the pressure observed 2 inches from the cowling surface is only half that, implying a velocity about 70% of free stream. One conclusion that can be drawn is that the discharged cooling air is not emerging at free stream velocity and is not making a seamless re-entry into the outer flow. It apparently forms a plume several inches thick.
The next experiment will be to tuft the top of the cowling and the windshield to see 1) how badly the flow there is disturbed by the cooling air outlets and 2) whether, as I optimistically suppose, the disturbance is damped by deceleration of the flow at the base of the windshield and acceleration over the canopy. We're going back to Greenwich for a week for a birthday party, however, and so I won't do that until early November.
[October 13, 2016]
I have been gradually, and more by accident than by design, unraveling the peculiarities of these tiny cameras. I have gotten to the point of downloading video from one of them to my computer; unfortunately, it is the 640x480 one (the $18 one) not the HD one, but I expect that sooner or later I will figure the HD one out too. Here is what the tuft array for the wing root test looked like standing still on the ground (left), and how the tufts lay at all speeds in flight:
[October 11, 2016]
The first thing I did with the remote camera was tuft the wing root intersection and fuselage side from about 70% of chord aft. My intent was to see whether any separation exists at climb speed that might require a fillet. There was none; the tufts were glued to the fuselage side at all speeds. This was the intent of the fuselage design; the maximum width is at the trailing edge of the wing, and the fuselage meets the upper surface of the wing at a right angle. There is a little weakness on the wing upper surface near the trailing edge, which I had previously observed, but it is not related to the wing-fuselage intersection; it extends out a couple of feet, and is simply a consequence of the root profile being of 18% thickness with the maximum thickness far aft. So that result was satisfactory, except for one disappointment: The camera's image was visible on the iPhone, but nothing was recorded on the TF chip. I have to figure out what went wrong there. The only files I found on the chip were a couple of 640x480 ones from the first camera; and they were large in bytes, but played as blackness on the screen; so there is still a problem with that camera too. If worse comes to worst, I can always use the phone's screen capture function to get still images, but I would much prefer video.
In addition to the root tufting, I repeated my wake survey of the upper surface of a cowl flap. The results were perplexing. I did not see any signs of kinking this time, but the two probes closest to the skin yielded no readings at all. The outer ones did, but I did not understand their behavior. The free stream dynamic pressure at the test speed was around 11 in Hg. I need to repeat this test once again, after making certain that the two lower probe lines are not kinking.
I had also tufted the left aileron to see whether the internal seal had eliminated any indication of weakness; it had. There is an interesting eddy at the inboard end, however, when the aileron is deflected downward. It is due to air flowing through the comparatively large gap between the aileron and the flap and upper wing surface. Only the innermost tuft on the aileron itself is disturbed; the one next to it, on the wing surface just inboard of the aileron, is straight. I could do a better job of sealing that gap, but the problem is minor and exists only during brief moments when the aileron has a large downward deflection. It's interesting to note that the gap between the cove lip and the aileron surface seems to be smaller near the center of the aileron, possibly because the aileron is supported at its ends and flexes under load, and the center tuft is also the one lying closest to the surface of the aileron.
[October 7, 2016]
For some time very small HD video cameras with the ability to connect wirelessly with a smartphone have been on offer on eBay at very low prices. This seemed like a promising tool for doing tuft studies without having to struggle with a festoon of wires from the camera to the cockpit. A couple of months ago I got one for $18 but was unable to get it to work; my phone never managed to hook up to its network address. I ordered a second, for $36, with equally little success. Thinking that I might be failing to properly follow the directions, which are inscribed on a slip of a paper in 0.5-point characters, Chinese on one side and a literal English translation on the other, I asked my son to have a go -- the septuagenarian's usual solution for digital bewilderment -- but he had no better luck than I. I returned that one and got my money back. After a period of mourning, I ordered a third camera, this time for $29. This one worked; or maybe I just finally understood how to work it. I mounted the camera and its associated circuit board, battery and antenna on an inverted aluminum T in order to be able to tape it securely to the skin of the plane.
The camera is the little thing peeking out of the field of orange tape. For scale, the tape is two inches wide and the mount two inches tall. An app on the phone turns recording on and off; the video is recorded on a chip that mounts in a socket on the edge of the circuit board.
Remarkably, after I got the third camera working, the first one started to work. Next thing you know, I'll be speaking Mandarin.
I also revised the mounting of the wake rake on the cowl outlet. I'm hoping for a big day of data gathering on Monday.
[September 28, 2016]
My first effort to measure cowl outlet velocities failed. The vinyl tubes kinked just in front of the aluminum tape when the cowl flap rotated to the fully-open position. Also, as I suspected might happen, the heat softened and loosened the duct tape. The metal tape was undisturbed, however, and when I get back from Post Angeles, Washington, where we are going tomorrow for a few days, I will replace the duct tape with metal tape and revise the routing of the vinyl tubes so that they will not kink.
[September 23, 2016]
Returned from the East yesterday. Today I installed the pressure rake that has been sitting around since last March but one. My plan is to collect measurements for four cowl flap settings for each of the two exit streams, one above and the other below the cowl flap, which doubles as a turning vane. I am hoping to learn something about the velocity of the exit stream. After collecting data with the rake on top of the flap, I will move the rake to a location just behind the flap and repeat the measurements. (In the picture below, the cowl flap is closed, but when it is opened there is a sepoarate outlet stream below its trailing edge.) I doubt that the results will be useful in any way, but they may be instructive.
The aluminum tape is there to be sure that the orange duct tape does not let go because of the heat. The four hoses go to four 1/8" steel tubes bonded into the firewall for this purpose; they are in turn plumbed to a four-valve manifold (from an aquarium supply shop) and to the inches-of-water gauge in the cockpit.
[August 26, 2016]
On the 18th I went to Santa Paula to see the Harmon Rocket (something like an RV-4) equipped with a 650-hp rotary engine that is preparing to challenge the absolute records for a propeller aircraft of record for time to climb from a standstill to 10,000 feet. What that record is, I don't know, but it may be 91 seconds in a Grumman Bearcat. Anyway, I figure the airplane, which will weigh less than 1,200 pounds with fuel and pilot, should get off the ground in less than 200 feet and climb at something more than 12,000 fpm. For some reason its wings have been clipped, which does not make sense to me; it must have been done to reduce weight, but I would have thought that in a climb the span would be worth more than the weight saving. The oddest thing about the airplane is that it has no cowling. The engine, with all of its plumbing, air and oil radiators and general clutter is left out in the breeze. The reasoning is that at 90 kias parasite drag will be a minor factor. Actually, this is not quite true; at best rate of climb speed, which is bound to be close to the best L/D speed, parasite drag is half the total drag. At any rate, I did some calculations, making various unfounded assumptions about the drag contribution of the engine, and found an impact of several hundred feet a minute. I did take into account the fact that a cowling would add weight at the same time as it reduced drag. The cooling drag, of course, would still be there. Anyway, the day after my visit the airplane made a couple of hops down Santa Paula's runway. The record attempt will be made at California City, near Mojave. Unfortunately, I will probably be on the east coast when it happens; we're leaving next Friday for an absence of three weeks or so.
[August 5, 2016]
Continuing in my new tradition of doing nothing of consequence, I added screws to secure the back-seat armrests, which have been held in place by the force of gravity for the past 12 years or so. I felt some hesitation about adding the weight of nine 3/8-inch-long 8-32 screws and their associated nutplates when they were so obviously unnecessary, but I overcame my scruples. Unfortunately I had the bright idea of using some Click Bond adhesive left over from a 2009 project to secure the nutplates. The two-part stuff completely failed to cure. I later looked up its shelf life, which is said to be one year. I then had to clean the horribly recalcitrant goop away before attaching the nutplates with a different adhesive, namely, Super Glue. Eventually I got the armrests secured, thus making the occasional inspection of certain cables, pushrods, tubing and wires somewhat more inconvenient and less likely to occur. Next big task: Velcro the carpets to the floor!
[July 21, 2016]
Two giant steps for mankind. First, I finally located the sheet of transfer lettering I bought a few months ago and promptly lost, and added the letters O (oil) and A (air) on either side of the temperature selector toggle switch. Second, on the suggestion of Russ Hardwick I added half of a 1/4" dowel to the back (ie uncalibrated) side of my carbon-fiber fuel dipstick. Russ pointed out, during one of our periodic lunch meetings, that a porous material like wood would hold visible fuel longer than the carbon fiber. It does. The suggestion was reinforced on the 9th when I observed Chuck Wentworth dipsticking the fuel in the Trimotor with what appeared to be part of an old broomstick.
[July 10, 2016]
Yesterday I parked, as I had determined was advisable, with the flaps out a few inches and the flap handle in the retract position. The plane sat in the hot sun for hours without ill effect. I described the problem I had had on June 4 to Chuck Wentworth, who said that he had experienced something similar with Javier's dark-blue Corsair. If it sits too long in hot sun with the wings folded, hydraulic fluid leaks out of the wings. The reason is the same: the fluid expands, raising pressures above the design values in the sealed-off parts of the system. This must have been a regular occurrence in the Pacific theater during World War II.
I have been meaning to show the checklists, to give a sense of the flavor of operating M2. Here they are:
Before start
Preflight
inspection complete
Sumps and gascolator drained
Chocks and tiedowns removed
Flight control locks removed
Pitot cover removed
Gear lowering ratchet, #2 Phillips screwdriver available
Seat belts fastened
Fuel shutoff valve open
Check visual gear-down indication
Cycle airbrake lever through retract position
Flap and gear handles centered
Check breakers
Pump brakes for feel
Start
Cowl
flaps
fully open
Radios off
Windows secure
Mixture rich
Master switch on (check voltage = 24)
Hold reset button on fuel totalizer until blinking stops
Check fuel quantity indication
Check total fuel on totalizer
Mags on
Clear area
Cold start:
Throttle open 1/2"
Fuel pump high for 8 seconds before cranking
Hot start:
Fuel pump high for four seconds, then off
Throttle open one inch
Begin cranking, then turn on fuel pump
Use full throttle/lean mixture if flooded
Check fuel and oil pressures
Before taxi
Turn
on GPS
Check gyro suction
Check stall warning
Check AH erect
Set DG
Set altimeter
Set clock
Check ammeter for indication
Check CHTs for indication
Select inboard fuel senders
Oil/air temp selector on oil (left)
Check parking brake released and safe
Radios as needed
XPDR on standby
Neutralize roll trim
Set pitch trim
Controls free and moving in correct directions
Select fuel tank on inside of turn onto runway
Obtain clearance if needed
Runup
RPM
to 1,700
Check mags for drop less than 100 rpm
RPM to 1,800
Cycle prop (first runup of day only)
Pre-takeoff
Flaps
set
for takeoff
Doors latched
Airbrake handle in detent, light off
Auto fuel switcher OFF
Autopilot OFF
Mixture rich
Prop fine pitch
Wastegate open
Lights as required
Transponder on Mode C
Cowl flaps to climb position
Climb
Retract
landing gear
Accelerate to climb speed/alpha
Retract flap
Set climb power (34/2500 for high performance, 28/2500 normal, 27/2300
and 50 LOP for economy climb)
Check fuel flow
Check oil pressure
Check XPDR reply light
Auto tank switcher on when balanced and roll trim neutral
Monitor CHT, EGT, OT during climb
Use wastegate after throttle is fully open
Cruise
Mixture
to
25-75 lean of peak (TIT)
Adjust cowl flaps as needed (CHT < 200 C)
Descent
Close
cowl
flaps
Open wastegate as appropriate
Before landing
Fuel
on
proper tank
Auto tank switcher OFF (not while cycling)
Park brake OFF
Mixture rich
Prop fine pitch
Wastegate open
Airbrake deployed
Landing gear down and locked (100 KIAS max)
Flap as required (90 kias max)
Open cowl flaps fully
After landing
Transponder
to standby or off
Retract airbrake
Retract flaps
Sufficient delay before shutdown to cool turbo
Manual landing gear operation
If the hydraulic pump does not work, perform the following steps:
1.
Pull
both landing gear breakers
2. Open the bypass (faucet handle below passenger's knees)
3. Trim to 90 KIAS and engage the autopilot to reduce workload
4. Put the gear handle in the DOWN position
5. Rotate the manual overcenter (large bolt head under pilot's knees)
with the ratchet. Place the ratchet handle to left of socket and lift,
moving the ratchet clockwise as viewed from the rear, until the gear
free-drops. Do not force the ratchet; little effort is required, and
only a few degrees of motion. If it does not rotate easily, check that
the gear handle is in the DOWN position.
6. Verify down-and-locked indication on torque tube
If
the gear
control valve does not respond to the
handle on
panel, you can either operate cables directly (right side of cockpit,
near floor) or remove the panel under passenger's knees and rotate the
valve pulley by hand. If necessary, move the flap and airbrake handles
in order to determine which cable pair controls the gear valve. The
spade fitting on the cable from the valve should move forward for gear
down.
[July 9, 2016]
Today I logged a few minutes at the controls of Javier Arango's 1929 Ford Trimotor. It is quite stable in smooth air, and very heavy on the controls, especially the rudder, considerable and well-timed doses of which must accompany every turn. The pedals feel as though they are welded in place. Chuck Wentworth said that to get the rating you have to demonstrate handling with one engine out; this involves placing both feet on one rudder pedal, pushing with all your might until the general principle has been demonstrated to the satisfaction of the examiner, and then calling for help. There are three fuel tanks whose contents are dipsticked by climbing up on top of the wing through a hatch in the cockpit ceiling. You're 12 feet in the air on a curved metal surface with few handholds -- far more dangerous, I think, than mere flying. Pan Am used to fly these cross-country, cruising at 100 mph at up to 10,000 feet, with 12 passengers. The engines are uncowled P&W 985s of 450 hp and 20 gph each. They set up an ungodly howl on takeoff -- supersonic prop tips -- but at 1,800 rpm in cruise the main noise is the hiss of wind. The designers seem not to have been overly concerned about drag; note the external control bellcranks.
[June 29, 2016]
Today I finally put in the right-hand aileron seal and flew for an hour. As far as I could tell, the seals made no difference to either roll rate or stick forces; at least whatever difference they made was too slight to notice. The temporary seals are made of a thin, porous polyester cloth that I normally use as peel ply. I doubt that an impervious material would be greatly different, but I guess, since it's not very difficult to install the seals, I will order some teflon tape and make permanent ones.
[June 26, 2016]
After I installed a temporary aileron seal on the left side, a series of obstacles prevented me from getting back to the airport to put in the other one and test fly them. Probably next week. In the meanwhile, I received through Javier Arango a photo that warbird photographer Frank Mormillo took of my plane as I was leaving Paso Robles on the 4th. It's a nice picture and the only decent in-flight shot of the plane in its presumably final configuration, so I put it in place of the now rather dusty old picture that has opened this site for the past dozen years.
[June 6, 2016]
The coefficient of thermal expansion of 5606 hydraulic fluid is 0.0005 per degree Fahrenheit. The fitting that failed was in a volume consisting of a couple of feet of 1/4" hose or tubing and an actuating cylinder with a 15.2 inch travel and an internal diameter of 0.91 inch. The volume of fluid in the cylinder when the flap is retracted is 9.9 cu. in. The volume of fluid in the lines is comparatively negligible, but let's say the total fluid volume involved is 10 cubic inches. If its temperature rises by 50 deg. F, its volume increases by 0.25 cu. in. The volume increase must be accommodated somehow. The flap is already up against its forward stop, so the accommodation has to come from expansion of the aluminum hydraulic cylinder and the nylon and aluminum lines.
It would be tedious to calculate how much each would have to grow, given their respective tensile moduli, and I'm not sure I would do it correctly anyway, but it's evident that it was easier for the nylon line to pop out of its compression fitting than it was for everything to expand. It's also evident that if the flap piston were free to move, a displacement of about .38 in. would relieve all of the excess pressure. Now, for the flap to move the fluid on the other side of the piston has to go somewhere. Where it goes is to the associated master cylinder in the synchonizer assembly, which in turn has to move about 1/16". That movement would get passed on to some more nylon and aluminum lines, and to the flap-extension side of the other three master cylinders. There is a pressure relief valve there, however, that would presumably protect the system. So the way to prevent fitting failures due to thermal expansion of the hydraulic fluid would seem to be to park with the flap extended an inch or two.
Now that I think about it a little more, an even better way would be to park with the flap handle in the retract position, rather than neutral. Then expanding fluid would be free to flow to the reservoir, and there would be no pressure build-up at all.
I'll try to remember that for the next barbecue.
[June 5, 2016]
Yesterday was the annual Antique Aero barbecue at Paso Robles. It was a hot day, as usual. When I was leaving, I taxied to the departure end and ... Well, never mind; you can read the whole story in the entry for June 6, 2015, because exactly the same things happened again -- partial flap extension, same hose blew off same fitting -- with the sole exception that this time all the hydraulic fluid ran out, and there was none left to retract the gear. I returned, and with the generous help of a couple of the guys who work at Antique Aero I got the flap hose reconnected and the hydraulic fluid replenished and flew back to LA without flaps or incident.
Since the fitting that failed both times is in a vent line, and therefore under very little pressure, when the flap is being extended, my current hypothesis is that both this year and last the fitting popped off while the airplane was parked, and that what made it pop off was simple expansion of the hydraulic fluid due to the right side of the airplane baking in the afternoon sun. I suppose this could be prevented by either 1) not going to the barbecue any more or 2) parking with the flap slightly extended or 3) revising the plumbing to replace some of the nylon lines with actual aircraft lines with flare fittings -- which I have avoided doing because of the expense -- or at least replacing the long, loose runs of nylon line with aluminum and using nylon only where the attachment fitting can be aligned in such a way that the nylon lines are loaded as short columns and would resist popping out by their own compressive strength.
[May 20, 2016]
I sketched out the design for the aileron seals.
If I were Leonardo da Vinci, this yellowed palimpsest would be valuable. There is, at any rate, some history to it. The date of 3/5/88 refers to when I initially drew the BL 140 aileron on an airfoil profile drawn by a Swee' P plotter. The blue profile is the operative one; I'm not sure what the green leading edge is doing there -- probably economising on paper. The white profile is the shape of the new ailerons; the circular-arc nose of the old aileron is visible behind it. The seal design requires a shelf, about 0.6" wide, protruding from the middle of the rear spar. The seal -- curved lines going to the two extremes of the aileron travel -- would be secured to it and to the underside of the porpoise-nose of the aileron with two-sided tape. It happens that I still have some of the wing spar cap material that I laid up long ago and that is about the right thickness and length. It's the same stuff as I used for the aileron spar caps. I'm planning to install a temporary seal first to be sure that handling is not adversely affected.
[May 16, 2016]
It was a great pleasure to fly again after an absence of several weeks. The engine started immediately, and it, the airplane and the air were all smooth and contented-seeming.
Casting about for some new project, I have settled upon that of sealing the ailerons. The original ailerons, which I replaced in 2013, had circular-arc leading edges, small gaps, no aerodynamic balance and no seals. The new ones have partial aerodynamic balance (that is, the nose of the aileron extends farther in front of the hinge line), no seals, and, because of their nose shape, larger gaps. I did not notice any change in speed when I switched ailerons, so the drag increment from the larger gaps was apparently small. Nevertheless, it is preferable to prevent crossflow from the high pressure side of the wing -- normally the underside -- to the low pressure side, and the aerodynamic balance is more effective if air is not allowed to leak around the nose of the aileron. External gap seals, consisting of flexible mylar blades that would touch the aileron surface, would prevent crossflow but would also reduce the effect of the the aerodynamic balance. The alternative is to install a fabric diaphragm between the aileron and the wing. That is what I think I will try to do. It's a little tricky, because the diaphragm must be short enough not to prolapse through the gap, but long enough to allow installation and removal of the aileron. Theoretically, a seal of this type should both increase aileron effectiveness and reduce stick forces. We shall see.
[April 18, 2016]
EBay delivered up a functioning CHT probe, which is now installed. Before I put it in I checked its continuity. Sure enough, it had a low but not negligible resistance, so my theory that at the very least a thermocouple should display electrical continuity received some support. I re-checked my two spares, which obstinately refused to let a single electron through. They ended up in the trash can, poor things. I flew for an hour; the CHT of the #5 cylinder was about the same as that of its counterpart on the other side. My CHTs go by pairs, with the rear cylinders being the coolest and middle ones the hottest. It would be nice to be able to boast that all are the same, but since they are all at or below the recommended 380 F, I guess it doesn't make much difference.
A number of people very kindly wrote, anent my gloomy reflections of March 31, that they like reading this stuff, no matter how trivial it is. So I guess I'll keep it up. Not for the next two or three weeks, however; Nancy and I are going to the east coast (not in Melmoth 2) for a grandkid's birthday and a little time on Cape Cod before the crowds arrive. Odi profanum vulgus et arceo, as Horace used to say.
[April 9, 2016]
More systematically this time, I checked continuity throughout the CHT wire harness. All good. So I went over to the biggest repair shop on the field, Able Air, and asked a mechanic, who happened to be working at the time on precisely this problem in a twin Cessna, if they had a way to test thermocouples. He said that they just swap them between cylinders and run the engine -- a real pain in the neck, since they tend to be pretty well secured, and if they fail you have to take them out twice. I don't understand why they don't just connect them to an old CHT gauge and warm them with a heat gun or a soldering iron. But anyway, he went on to say that any balky thermocouples over 15 years old they just replace. He seemed certain that both of my "spares" were bad -- as in fact the lack of electrical continuity across them suggests, at least to me. Mind you, all of my thermocouples are 1970s vintage, so the 15-year rule must be applied gently. Next stop, eBay.
[April 7, 2016]
Yesterday, in the vein of continuing minutia, I tried to do something about the inoperative CHT indication on the #5 cylinder.
The system consists of six bayonet-style thermocouples connected by a few feet of two-conductor iron-constantan wire to a 12-pin Molex connector. The other side of the connector is a short pigtail to a three-position rotary switch which selects cylinders in pairs -- front, middle, rear -- and sends the selected signal through a pair of trim potentiometers to a dual CHT gauge. The purpose of the trim pots is to correct for the various junctions in the system and for the fact that not all of the wire is the proper iron-constantan. The calibration system is the usual cup of boiling water.
The possible points of failure, therefore, are many. But since all of the other probes work, the problem cannot be between the selector switch and the instrument; it has to be between the thermocouple and the rotary switch. The connections to the selector are soldered and the wires are tightly tied to the switch body with lacing cord, so, unless I have a cold solder joint there -- and that is not particularly probable, since the #5 CHT used to work -- the fault is not likely to be at the switch.
Based on past experience, I would be inclined to suspect the Molex connector, because its connections are crimped. On the other hand, bundles of 12 wires, tied at close intervals, are very stiff, and so their connections are less likely to fatigue than single wire terminals are. In the past, however, I had a CHT problem that was due to a broken, albeit quite stout-looking, connection between the thermocouple pigtail and the iron-constantan wire, so you never know.
I decided that the place to start was to check continuity between the thermocouple and the rotary switch. So I opened the cowling and disconnected the thermocouple. At this point I went off the rails. Thinking that a thermocouple is a bimetallic junction and therefore ought to have a low resistance, I checked the thermocouple with an ohmmeter and found infinite resistance. (I know this is not the proper way to test a thermocouple. but all I was interested in was continuity.) Aha, I thought, there's the problem; the junction has failed. So I hunted up a spare bayonet, installed it, put the selector back into the panel, and zipped everything up without ever conducting my intended tests of continuity between the probe and the switch.
I started the engine. The #5 CHT did not indicate.
Tomorrow is another day.
[March 31, 2016]
Yesterday I wired the landing light and lit it up. It worked.
According to legend, Alexander the Great, having subjugated various tribes all the way from Macedonia to India, wept because there were no worlds left to conquer. Alexander considered himself quite a fellow, but it is noteworthy that in all the ancient annals of Indian history there is no mention of his arrival or departure. He was a raindrop in an ocean, gone without a trace. My illusions about my own grandeur are not on the scale of Alexander's, but I am beginning to get that no worlds left feeling myself. All the goals I have set for myself with Melmoth 2 have been either accomplished or discarded. I am reduced to nugatory stuff like adding an armrest or fixing a leak. This 14-year record of tests and modifications is in danger of degenerating into a mere maintenance logbook. Perhaps it is time to put it to rest.
[March 24, 2016]
Stopped at Luky's on the way to the airport to pick up an AN822-3D fitting. Arrived at the hangar, I found the flap actuator still dripping, ostensibly from the elbow under the trunnion. This is what the thing looks like (also here), and this is about the only angle from which you can see or approach it:
I took the actuator out for the third time -- I'm getting quite good at it -- and replaced the fitting. I then reinstalled the assembly and ran the flap -- and it leaked worse than ever. I could hardly believe it; even a damaged joint could not leak that badly. I was gazing at it in wonderment when I saw a drop of hydraulic fluid fall onto the fitting from above. At first I thought it might be coming from the seam between the trunnion and the cylinder, but that seam was dry. I realized then that it must be coming from a fitting behind the top of the trunnion, not visible in the photo or for that matter in real life either. So I took out the actuator yet again, and found that the B-nut on that top fitting was not even finger tight. So after all that the problem had been a stupid oversight of assembly when I last overhauled the actuator, a year or two ago! How it managed to pass yesterday's pressure test I cannot guess. I tightened the fitting, put everything back together again, and it worked without leaking.
[March 23, 2016]
The landing light is now in place on the right main gear door; not wired yet, however.
In the meantime I removed the left outboard flap actuator in an effort to discover the source of a persistent escape of hydraulic fluid. I have repeatedly put folded-up paper towels into the niche that the cylinder occupies in the wing in an effort to discover where the leak is, without success. This time I rigged up a testing apparatus that consisted of a second hydraulic cylinder that I could squeeze in a hydraulic press, ducting fluid from it to the actuator in question through one port while the other was capped. This had the effect of pressurizing both sides of the piston, and therefore of potentially revealing a leak anywhere in the cylinder. At 500 psi, which is about as much as this actuator ever sees, no fluid appeared. When I put the cylinder back into the wing, however, one of the connections to it leaked copiously. The flare fitting, on close examination, may be slightly damaged -- though I would not have thought so had it not leaked. The fault could also be in the hose fitting, though that seems less probable, since it is steel rather than aluminum and so more difficult to damage. It is also more difficult to inspect. I'll replace the aluminum AN fitting today and hope that solves the problem.
[March 16, 2016]
I had a couple of strokes of good luck. Rummaging in my piles of detritus I found the uplock assembly for Melmoth 1's nosewheel, and it happened to incorporate a precisely suitable type of microswitch for sensing when the gear is down and illuminating the landing light. This could be seen as an argument for never throwing anything away, which is not quite my policy, but almost. I thought I was going to have to bond a couple of tabs in the wheel well to which to secure the switch, but as luck would have it I had, some time in the 1980s, incorporated a gusset that happened to be in exactly the right position for mounting the switch, which I did this afternoon. I omitted this gusset on the other wing without apparent ill effect. I can no longer remember, in fact, what it was supposed to do; but when its time finally came, it performed nicely.
[March 11, 2016]
I amused myself during the final episode of Downton Abbey -- our long national nightmare is finally over -- by hand-stitching a leatherette cover for my armrest. In dim light, with peripheral vision, it doesn't look bad. The combination of moving the sidestick back 3 inches and adding the armrest has improved the consistency of my landings, since I now rely on wrist rather than upper-arm action to flare.
I have now turned my attention to the landing light, which has been lying around for a year since I machined a lot of material off its housing to lighten it. (It was intended for a dune buggy, where weight is apparently not a serious consideration.) I had provided it with two mounting holes for 10-32 screws. These did not provide a convenient way to adjust its aim, however, so today, during a furious rainstorm -- all rainstorms sound pretty furious, to be sure, when you're working in a metal hangar -- I made a mounting plate out of .100 aluminum with holes at four corners through which four countersunk 3/16" screws will secure the light to the inside of the right upper wheel cover. Shimming the two front holes will allow adjusting the azimuth. The elevation is a bit more of a puzzle. I suppose the light should be pointed more or less at the landing aim point. A few online sources of uncertain infallibility mention values like -4 or -5 degrees, which must represent the negative of the angle of attack at approach speed. I calculated my angle of attack at 70 knots and 2,200 pounds with full flap and it's around -2 degrees, so the landing light should be aimed up, not down. I guess I'll just point it straight ahead. It will have to double as a taxi light, but it will not be a very good one, since it will be just a few inches above the ground. My idea at the moment is to wire it in parallel with the nav lights, with a microswitch actuated by the landing gear, so that the landing light would be on at any time the nav lights are on and the gear is down.
[February 25, 2016]
Before leaving on February 14 for a week and a half in the East, I rebuilt the exit duct for the oil cooling air to make it less restrictive. On returning testerday, I tufted the oil cooler air outlet. I had done this previously, but then I had placed the central tuft a few inches behind the outlet, where it lay down smoothly enough. This time I put one row of tufts immediately behind the outlet, and found that the middle tufts were jumping around like mad. By the time I landed they were in shreds. Reasoning that this bubble of vorticity could not possibly be helping the exit flow, I added a couple of turning vanes made of .010 aluminum. The flow is now smooth. Whether this change had any effect on cooling or anythng else, I don't yet know, but at least it's nice to know that the flow is now orderly.
The pictures below show, respectively, the rebellious tufts, the turning vanes as seen from outside and inside (temporarily held in place with aluminum tape; now that I know they work, I'll epoxy them), and the tufts brought to heel. It's interesting that the flow at the second row of tufts in the first picture, which is 4 or 5 inches behind the first, appears to be quite smooth and attached in spite of the turbulence immediately ahead of it; the outer tufts indicate a converging flow. The fourth picture is not very clear -- it's a small portion of a larger one, and taken through an optically poor area of the windscreen -- but at least it's obvious that none of the tufts is standing up.
[February 3, 2016]
At least for the time being -- winter, that is -- I am resolving the oil temperature problem by declaring victory. The "desired" oil temperature range, according to the overhaul manual for my engine, is 150-200 deg. F. I have been aiming for 78 C, or 172 F. On line, however, I found a persuasive recommendation by Mike Busch, who is a pretty reliable authority, of 180-200. So I took a small piece of green tape and affixed it to the face of the oil temp gauge to mark a "desired" band of 80 to 93 deg C. I flew for an hour today, climbed to 10,500 feet, set up a 6.3 gph cruise at 22.5/2000 for a true airspeed of 156 knots, and the temp stayed within that band. That will do for the moment.
The picture was taken during the descent, so the oil temp has come down a bit; but it gives the general idea.
[February 1, 2016]
No further work done on the oil cooling, but I hard wired the GPS, thereby liberating the 12v outlet for the iPhone charger. Probably I can use that power, and a cell phone car charger, for the Stratus as well. No doubt Peter Lert will tell me, as soon as he reads this.
[January 16, 2016]
Alas, the new duct is scarcely better than the old. It got me perhaps 7 degrees C of improvement, not the 20 I was hoping for. It is still in rough form and may be slightly improved by adding a bellmouth (that is, rounding the edges at the inlet) and sealing the small holes along the riveted edges, but it is still not going to do the trick.
January 13, 2016]
The new oil cooler inlet duct is almost complete; only a couple of seams remain to be riveted. I am building it on the theory that the existing duct is too restrictive. The new duct's inlet area is about 2.5 times larger, and, possibly more important, it does not converge so rapidly toward the face of the oil cooler. The old inlet duct -- its purpose is to suck up air from low in the the high pressure plenum before it has been heated by the exhaust pipes, turbocharger, and so on -- used a straight, wedge-shaped hood over the cooler. According to Kuchemann and Weber, the authors of the canonical text on this subject and, incidentally, a married couple -- how nice that they had a shared interest -- a more voluminous and convex hood is desirable. My hope is that the oil temperature will settle at 78 C, as Continental says it should. If that does not happen, I will have to start thinking -- well, not start, because I have already thought -- about a protruding scoop to bring cold outside air to the cooler. Such a scoop would be located about where the NACA inlet for engine induction air is located now, and would replace it as well. The conventional wisdom -- not to mention common sense -- holds that inlets should not be multiplied, and that it is better to take in all air -- heating, ventilation, engine cooling, oil cooling, intercooling, accessory cooling, etc -- through one large well-designed inlet. It is not clear, however, how the penalty for each additional inlet might be balanced by its particular advantages. For example, because of the engine cooling being of the updraft persuasion, air getting to the oil cooler is being preheated as it swirls around in the lower plenum. I could run a duct from the front inlet back to the oil cooler, but it would be almost three feet long and would entail a pressure loss. Air brought in from the free stream close to the cooler would experience almost no pre-heating and would also have slightly better pressure recovery. Removing the oil cooling requirement from the nose inlet would allow closing the cowl flaps farther, thus reducing the cylinder cooling mass flow and drag. Likewise, a pitot-style induction air inlet would probably have slightly better pressure recovery than the flush inlet. In the end, there are too many uncertainties to allow a person like me, with limited practical experience, purely theoretical judgment. The only way to find out is to try it.
[January 4, 2016]
The period around Christmas and New Years brings work on the plane practically to a halt. I did squeeze in a few hours to reposition the oxygen on-off lever, which turned out to collide with the sidestick after I moved the latter a few inches aft. I also started cutting material for an armrest, which I think will make it easier to control pitch precisely while landing. The next serious project, however, is to refashion the oil cooler inlet duct. I hope to get started on that this week. A good deal of rain is forecast, so the plane may as well be gounded for a few days.
A piece of good news was that the Lowrance GPS I got for $40 from eBay works.
A piece of bad news was that Homer Knapp, whom I had known for 45 years or so, and who always let me use his machine shop and taught me how, died a week before Christmas. Homer was an eccentric character and a genius with machines. Somewhat reclusive, he was still saying "groovy" in 2010. He had been a motorcycle racer, and made a living as a motorcycle machinist. Racing teams turned to him for work that no one else could do. A bit of a hoarder, he lived in a warehouse alongside his shop, surrounded by pieces of various bikes and a couple of Swifts that he never got around to restoring. He typically rose at 2, finished breakfast at 4, and worked at night in order not to be interrupted by the telephone. You needed to pick your foot placements carefully to move around in his shop, which was piled high with tools, machines, parts and general debris, while plastic sheets and improvised gutters dangled from the leaky ceiling. Homer proved that clean work can come out of a dirty place -- a rule I live by. I don't know for sure what killed him, but it was almost certainly something dietary, if one may judge from the directions for a sandwich that he asked me to bring him from Subway a few weeks before he died:
Foot
long turkey breast on Italian herb & cheese bread
mayo
both sides
extra pepper jack cheese
lettuce
tomato
cucumber
black olives
vinegar & oil
salt & pepper
honey mustard dressing heavy on both sides
[December 17, 2015]
Yesterday I flew to Flabob, near Riverside, to visit Fred Culick, a retired Caltech aerodynamics professor who has been involved for many years in investigating the aerodynamics of the Wright Flyer and in building a couple of replicas, one of which is in his hangar awaiting FAA approval to fly. This one is slightly modified to make it easier to handle, and equipped with a VW engine of ample power. We had lunch at the airport cafe with several other codgers, one of whom had owned a Loving's Love, a Formula One single-seater with an inverted gull wing that impressed me quite a lot when I was, in the words of Joyce, "jung and easily freudened." He reported complaining to Loving that the flat seating position was hard on his legs. Loving, who as a youth had lost both of his lower legs in a gliding accident, explained that as soon as he got into his airplane he would take off his prosthetic legs. Having complete legs, he observed, was a handicap.
Afterwards we visited the Quiet Birdmen headquarters, a big new building that contains an impressive mural of the history of flight told in aircraft types, the character of each of which the artist had accurately captured -- no small feat. Flabob has always been a pretty scruffy airport -- I had not been there in decades, since the days of Art Scholl -- but it seems to be in an upswing now, with a lot of new hangars, general cleanup, and big plans for the future with which I will not bore myself.
It took four restarts this time to get the GPS to behave. The first couple of unplug-plug-restart cycles produced nothing, the screen displaying only the track of my last flight and a bunch of blinking non-data. On the next try the map came up, but it was for the wrong place, and the "Go To" function had forgotten its Airport/VOR/NDB database and demoted itself to displaying waypoints only, of which none were stored. The fourth restart finally brought full functionality back. In the meantime, the "spare" Lowrance was on the seat next to me, displaying a blinking "GPS Cold Start" message for the entirety of the flight. Maybe it wanted me to press the Enter button, now that I think about it. A correspondent let me know that the Lowrance accepts voltages between 6 and 34, so obviously the problem is not due to tired blood in the voltage converter.
Ever since I moved the sidestick back three inches I have been landing a bit prematurely, but yesterday I finally managed a fully-stalled greaser and made the first turnoff, 600 feet or so from touchdown. Muscles take a while to reprogram.
Oil temperatures have been down a bit -- we're having what passes in southern California for a chilly spell, with daytime temperatures in the 60s -- but not where I want them.
[December 14, 2015]
To clarify the matter of my Lowrance Airmap 300 GPS and why I do not simply get a newer one: The Lowrance is nicely integrated into my autopilot (which is actually a single-axis Century I wing leveler originally acquired some time in the 1970s) and I use it almost all the time while cruising. The autopilot can couple to the Lowrance or to either VOR, and the interface gadget, a "Smart Coupler" (www.porcine.com) that I installed in 2005, can also use the GPS to hold a heading, a capability that the Century I itself lacks. (There is even a back course swtich for reverse-tracking a localizer, but I haven't used that in about 40 years.) So the system is nicely integrated and has worked well for years, and I am loath to replace it with a different one if I can avoid it. The problem with my present GPS is not that it is completely broken but that it is intermittent. It no longer seems to want to initialize on the ground; but if I unplug it (it's plugged into a 12v lighter-style socket that's powered by a Narco 28v-to-14v converter) and then restart it in flight, it usually behaves normally. I need to check the voltage at the socket, but in the meantime I got the second Airmap 300, since they're so cheap on eBay, just in case the one in the plane really turns out to be dying.
[December 10, 2015]
My second eBay GPS arrived. It is more complete and in better external condition than the first, but I can't get it to lock on either. So far I have just tested it at home. I forgot to take it with me today when I flew around a little to get some baseline oil temperature data with the revised oil filter plumbing and with the oil cooler's exhaust duct removed. The oil temperature was down about 5 degrees C, which was gratifying but a little hard to explain. The oil temperature increase due to closing the cowl flaps was only about 2-3 deg. C, as opposed to 8 when I measured it six years ago. But the cowling outlet for the duct was open, so closing the cowl flaps did not restrict outflow as much as it had then. I am going to proceed on the assumption that the outlet duct is needed. The temperature in the duct leading into the oil cooler was 35 C, as usual. The next step will be to revise the oil cooler inlet duct to considerably increase its cross-section and make its curves more gradual.
[December 2, 2015]
My first attempt to get a replacement GPS from eBay was not successful; the device started up, like mine, but like mine it would not lock onto satellites or track movement. I returned it and bought another for about the same price. I guess it's possible that they all contain some semiconductor that fails after 15 years; we'll see. In the meantime, I removed the AN fittings from the oil diverter (which sends oil through the filter and then returns it to the cooler) and replaced them with ones differently arranged. The old fittings hung out over the cooler, limiting the height of the outlet duct; the new ones are completely clear of the cooler. First, however, I will fly with the outlet duct removed and the cowl flaps open to see how the oil cooler performs with maximum delta-p and how oil temperature is affected by cowl flap setting. I usually cruise with the cowl flaps fully closed and about 5 inches of water delta-p; I'm not sure that is adequate for the oil cooler.
[November 23, 2015]
We finally returned on the 20th after an absence of four weeks. Today I flew around for a while. At one point the radios all stopped being audible in the headset. I switched to the overhead cabin speaker -- a quaint feature scoffed at by Burt Rutan years ago -- and it worked. I was congratulating myself on ignoring Rutan and keeping the backup cabin speaker, but when I tried switching back to the headset it was working again as well. The electrical demons were having a field day; my Lowrance Airmap 300 GPS had been intermittent and then seemed to have quit locking onto satellites altogether; but today it worked. In the meantime I got another one on eBay for $40. At that price, actually, I thought I might get a couple. The advantage of that particular unit, for me, is that I have a mount for it and a special plug and harness that connects to the autopilot, so I'm not as interested in an up-to-date GPS as I otherwise might be.
[October 18, 2015]
In an effort to resolve the oil temperature problem once and for all, I am consulting with various people who know about such things and working up a plan for a series of modifications and tests that will, in theory, allow me to isolate the effect of each change and, eventually, figure out how to fix whatever is amiss. In the past I have operated on a series of hunches and impressions, often comically false, as when for a long time I confused the oil and induction air temperatures, which are displayed on the same gauge and selected with a toggle switch that I had unwisely left unlabeled, imagining, I suppose, that the difference would be obvious. Actually, as it happens, the induction air temperature (a.k.a. turbocharger discharge temperature) typically runs right around 78 C, which is supposed to be the regulated oil temperature, and so, with the help of confirmation bias, I had no trouble at all mixing them up. (The switch is still unlabeled, but at least now I have a clear idea of which position is which.) At any rate, the failure of the oil cooler, which was plumbed more or less identically in Melmoth1 and worked fine there, to bring the oil temperature down to 78 degrees in Melmoth 2 can be due to a number of causes, singly or in combination. When I get back from Connecticut around the middle of November, I intend to work methodically on this problem until it is fixed.
On September 2 I referred to checking delta p -- the pressure drop in the cooling air -- across the oil cooler, but as I was about to install some probes to do so I realized that since the air never comes to a halt in the duct it is actually impossible to measure delta p there. I have thoroughly documented delta p within the cowling, so I know that ample pressure difference is available; the pressure recovery is about 85% of q, the free stream dynamic pressure, at cruise, and 90-95% in climb. The fact that the oil is too warm means either that the pressure available is not getting converted into sufficient mass flow through the cooler -- because of faulty design of the inlet or outlet ducts, or both -- or the air going through the cooler is hotter than it should be. Or all three.
Another possibility is that insufficient oil is going through the cooler; but the cooler has been overhauled, there is a pressure bypass in the oil filter, which is plumbed in series with the cooler, and the oil pressure is 45 psi, which is pretty normal, so I do not suspect a mysterious problem within the engine. At least not yet.
[October 13, 2015]
The new position of the sidestick felt a little odd; it will take getting used to. I felt, in fact, that it was now too far back, but I had that impression only during the flare; the rest of the time it was fine. I have not put in an armrest yet, and during the flare I pressed my forearm against the upper longeron in an effort to mimic the stabilizing effect of an armrest. It will take a number of landings to decide whether I like the new location better than the old.
I examined the ducts leading into and out of my oil cooler, trying to imagine a reason for my persistently high (95 - 100 deg. C) oil temperature. It's possible that the ducting is distorting the flow at the oil cooler face, so that, in effect, not all of the cooler is getting an equal supply of air. There also may be a simple choking effect at the outlet; the inlet area is 10 square inches, but the outlet is only 7. I had some idea about accelerating the outgoing air to that of the surrounding flow, but the physics probably isn't sound: Most likely, not enough energy is added to the air in the form of heat to overcome the aerodynamic losses in the ducting and in the cooler itself. I can improve the outlet ducting and make the vent an inch wider, but I will have to move an oil line first. Since we're going back East again shortly, that will be a project for when we return.
[October 7, 2015]
We returned from the East on September 25th, and are going back there for another three weeks or so on the 19th. In the meantime I'm moving the sidestick back about 3 inches and adding an armrest for my left arm. The sidestick has always been a little too far away for my combination of arm and leg length. It's probably been better for people with shorter legs than mine. I doubt I will get much else done in the short time we will be here, though I have several other projects in mind.
[September 2, 2015]
Flew today -- first time since July 9. All went well; only sour note was the usual high oil temperature. I need to have another look at delta-p across the cooler. But not now; tomorrow, to Boston for two or three weeks..
[September 1, 2015]
Just to round out my compendium of tire information, my worn-out tires weigh about 80 ounces, which is 25 ounces, or 1.5 pounds, less than the new ones. And, incidentally, the nosewheel tire, which is a 500x5, is 13.75 inches in diameter, and one door bumps it slightly.
I finished putting the plane back together today. The most difficult part was getting the hinge pins into the airbrake. I made the same mistake with them as I did with the stabilizer-elevator piano hinge: I used hinge wire for jigging. The hinge wire is actually 8 thousandths undersize, and so it allows errors of alignment to develop. After trying unsuccessfully for some time to get the hinge pins in, I decided to try the super-long reamer I had made back when I was thinking about line-reaming the elevator hinge. It went in about a foot and then the brazed joint between the reamer and the long .098 wire broke. Luckily, it wasn't very difficult to back the reamer out, and I eventually found a way to get the hinges in. Despite the difficulty of inserting the pins, the hinge action is smooth and free of resistance.
Yesterday the gear doors closed flush and the actuating cranks went overcenter, as they should. Today the gear stopped a little short of fully retracted. The only thing that had changed was that I had connected the linkages that operate the inboard doors, so they must be out of adjustment. I am pretty sick of retraction hardware at this point, however, and we're leaving for the East on Thursday, so I'm just going to let it be out of adjustment for a while.
August 30, 2015]
Here's a data point: the retread tires (one Goodyear carcass, one Condor) are not only 1/2" larger in diameter than the McCrearys but they also weigh 4.5 pounds more (each!), 180 ounces vs 105. Yesterday I installed the smaller tires, adjusted and swung the gear, and everything seems to be working fine. I still have to hook up the inboard gear doors, but my hope that I would get the plane airborne again before we leave for a couple of weeks in the East looks as though it may be realized.
[August 28, 2015]
Went to Desser Tire this morning with an improvised caliper and asked to see several 600x6 tire models, no retreads. Sure enough, they were 16.75, 16.5, and 16.375 in diameter, vs 17.0 for the retreads. I bought two of the smallest, which are McCreary Aero Trainers.
[August 27, 2015]
Yesterday, after reassembling the retraction mechanism, I discovered that the right main tire would not retract because of interference with one point on the wheel well. On consulting my maintenence log, I found this:
The 7/3 entry, which was made retrospectively, is incorrectly dated; it should be 7/9. But the important entry is the one on 7/2. The order of items reported is random -- they were done over several days -- and the cycling of the gear to adjust the retracted position of the left main was done before the right main tire was replaced. In other words, I did not cycle the landing gear after replacing the right mail tire. I didn't fly between then and the 9th, so the flight on which the gear failed to retract and the mainshaft taper pins failed was the first one with the new right-side tire. It now appears pretty clear that my theories about the problems having begun with the failure of the rivets in the left inboard door bellcrank were incorrect; the problem was simply that the tire is too large; everything else followed from that.
The tire is a retread, and is 17 inches in diameter. My old tires, which are Air Tracs and are worn out, are 16 inches in diameter. The tread depth on the new tires is 1/4", so the old tires were presumably around 16.5 inches in diameter when new. The difference would be inconsequential on any factory airplane, since they have larger tolerances, but things on Melmoth 2 are tighter and it's apparent that I'm going to have to find smaller 600x6 tires. Or I suppose I could machine a bunch of the tread off my new tires.
[August 15, 2015]
The aluminum bar in the picture below has now become this. It's not quite ready yet, and it's taking forever, both because our grandchildren are in town and my airport time is therefore somewhat curtailed, and because I'm not a skilled machinist and am working with a quite primitive milling machine and a very limited array of cutting tools. Once I've put the finishing touches on this part, however, I will be able to put the mechanism back together and see how badly whatever dimensional drift has occurred has thrown the whole system out of rig.
[July 22, 2015]
This is where things stand, or lie, at the moment.
The partially deconstructed central actuator for the landing gear is in the upper center of the picture. The arms that retract the gear, and go overcenter to hold it up, can be seen, along with the rods that connect them to the retracting trusses. In the original design, each arm was bolted to a hub which was pinned, with one of the now infamous taper pins, to the 3/4" central shaft. The present scheme is to replace the two hubs and two arms with a single piece machined out of the 7075 bar in the foreground. Since the piece is asymmetrical in two axes, the most critical task is to ensure that I do not inadvertently make a mirror-image of what is needed, as I have done so many times before.
[July 16, 2015]
I got a chunk of aluminum of exactly the alloy I wanted -- 7075-T651 -- and exactly the size I wanted -- 2.5 x 2.5 x 8 -- for exactly the price I wanted -- $18 -- from the wonderful Burbank Metal Supply. From this billet I hope to carve a single piece that will replace four pieces in the earlier version. I have a new main shaft, this time 4130 rather than mild steel. I intend to replace the taper pins with 1/4" NAS close tolerance bolts. A couple of people have suggested that the taper pins, by failing, protected the rest of the system, like fuses; but I think I would prefer to have a system that the hydraulic actuator cannot break.
Here is an interesting plot of the loads, mostly tensile, on the links in the retraction system. The one labeled "Master" is the force from the hydraulic actuator, and suggests that an actuator force of less than 500 pounds (the analysis ignores friction), which corresponds to an hydraulic pressure of 400 psi, is needed to retract the gear. "R truss", "L truss" and "N truss" are the links from the main shaft cranks to the right, left and nose retraction arms respectively. The "trunnion" loads are in the links between the retraction trusses and the struts. The horizontal axis represents 120 degrees of rotation of the main shaft.
[July 13, 2015]
With six hours of work and the indispensable assistance of a mini gear puller that my neighbor John Biggs lent me, I managed to get the landing gear retraction main shaft out of the airplane. It turns out that the taper pins securing both the right and left actuator arm collars to the shaft had failed. not just the right one; in fact, the shaft was spun about 45 degrees with respect to both those parts. When I have freed those parts from the shaft I will work out a plan for repairing the damage. This experience has given me a poor impression of taper pins, and I am thinking about replacing them with close tolerance bolts. The main shaft may need to be replaced; I need to check the holes to see whether any plastic deformation took place. Here is the shaft with the two spun collars still in place; the two holes at the right end secure the crank to which the main hydraulic actuator is attached.
[July 10, 2015]
My understanding of what happened during yesterday's gear glitch was wrong. I still don't understand what really happened or why it happened. Some forensic engineering and stress analysis will be required to puzzle it out, and some ingenious disassembly work, the details of which I have yet to figure out, to repair it. Two 1/8" rivets in the bellcrank operating the left main gear inboard door had indeed failed, and so the door was not opening to allow the left main gear to retract. But the much more fundamental problem is that a steel taper pin, which connects the central driving shaft of the gear retraction system to the retraction linkage for the right (not left!) main gear and the nose gear, sheared. That was the loud bang that I heard.
This raises several questions. One, what caused it to fail? Was it a fault in the original machining and assembly? Or was the joint subjected to excessive stress? If the latter, what stress level was expected, and why was the pin not strong enough to withstand it, several times over? The second question, or class of questions, has to do with how to repair it. Because of the way the mechanism is assembled, the main shaft -- a 3/4" thick-wall steel tube -- has to be freed from the aluminum arm to which the failed taper pin attached it in order for the whole assembly to come apart. It's not yet clear whether or not the sheared surfaces are clean enough, and sufficiently flush with the outside of the steel shaft, to allow it to slide inside the aluminum arm. If not, the only option I see at the moment is to take a Sawzall to the shaft and then make a new one. Obviously, I don't want to do something hastily and later realize there was a better way, so I'll be thinking about this a lot during the weekend.
At the same time, I'm resurrecting the computer program that I wrote in 1991 to design the kinematics in the first place in order to study the torques and tensions in the various parts. I hope with it to be able to see what the stress levels in the failed pin should have been, and why they were evidently greater -- or the pin weaker -- than expected. The whole assembly is quite inconveniently situated in a six-inch-wide cavity between the main spar and a closed torque box. In the two pictures below, the missing large end of the taper pin is visible as an empty hole in the first image, and the threaded small end can be seen, from the opposite side, in the other.
[July 9, 2015]
The small adjustment that I made to the geometry of the left main gear retraction arm had the unexpected effect -- doubly unexpected because it had worked fine on jacks -- of making the inboard door interfere with the tire and prevent it from fully retracting. The tire jammed against the door today in flight, failing a bellcrank in the door's actuating linkage. Here is the geometry at approximately the point where the collision must be taking place:
It's apparent that the left door gets closer to the tire than the right one does. The linkage that controls it is quite complicated and while I can't remember why everything is just the way it is -- I designed it in 1991 -- I do remember that I could not find another way for it to be, although I was obviously interested in keeping the door as far from the tire as possible. There is already a relief in the door for tire clearance; I may be able to make it deeper. First, however, I have to repair that bellcrank, this time with four rivets rather than two. A rivet failing makes a noise like a gun going off. The first time it happened was in flight; I though some major part of the gear system might have failed, in which case one strut might collapse on landing. I landed as gently as I could, and it turned out everything was fine; none of the major components was damaged, and the gear went down and locked as it was supposed to. The second rivet failure took place on jacks, while I was trying to figure out what had happened the first time. Now I know. I need to make an external switch for cycling the gear from outside the airplane; when I cycle it from inside I can't see what it's doing.
[June 30, 2015]
Someone asked why the gear doors are not adjustable, like those on every other airplane. Actually, both the upper door, the one that hinges to the bottom skin of the wing, and the innermost door, which hinges on the underside of the fuselage near the centerline, are independently adjustable, as are the nosewheel doors. The only ones that aren't are the big semicircular doors that cover the upper half of the tires. The reason they aren't is that the wing is small (105 sq. ft.) and although the profile at the root is 18% thick it was impossible to fit the 600-6 tire and strut into it without the strut (which is on the outboard side of the tire) grazing the wing contour when retracted. Consequently, the semicircular doors sit right up against the strut and cannot be adjusted inward.
Another person asked whether it is not possible to make a nosegear free-drop into place. The answer is that it is, and would be highly desirable, but it is possible only if the wheel retracts forward. On a single-engine plane with a tight cowling, fitting the nose tire under the front of the engine is difficult. The Cessna 210 manages it with a somewhat deeper cowling than mine; I tried to find a way and failed. Actually, now that I have a new gas spring installed I think the gear will free drop and lock, provided the indicated airspeed is 90 knots or less. It certainly locks on the jacks.
[June 29, 2015]
One of the results of doing things in an unconventional way is that you learn why the conventional way is preferred. It was out of a desire to simplify my hydraulic system that I decided to use a single central hydraulic actuator and also a single central landing gear up-lock, and to connect all three gear legs mechanically. I have had to modify that system in some ways -- for instance, the nose gear has a gas spring and a hydraulic actuator of its own to help it go down against its own aerodynamic drag -- but the solid interconnection among the gear legs remains and has for an unintended consequence that it is very difficult to make small adjustments in the behavior of individual legs. For instance, the only way to adjust the height of the retracted wheel in the well, and therefore the fit of the wheel covers, is to move a hole in two small aluminum lugs on the retracting arm -- which is to say, make the lugs over again. The kinematics program that I wrote to design the retraction linkage in the first place said that to raise the left main wheel 3/8" I needed to move the hole in question .040", or 1 mm, upward. I made the new pieces last week and today installed them. To my surprise and great satisfaction, the left main is now in the proper position when retracted and the doors are flush. I decided, however, that the bolt that connects the gas spring to the retracting arm was not well enough supported, and so I took the system apart again and made an additional steel part that will have to be welded into place before I reassemble the nose gear and get the plane off the jacks.
[June 22, 2015]
I was wrong to say in the previous entry that the nose strut gas spring had been installed upside-down. As is apparent here, it was installed shaft-downward, as it should be. I was misled by the fact that it had a journal bearing at the bottom end and a self-aligning bearing at the top. It seemed to me after I dismantled it that the journal must have been at the top if it was anywhere, but I was mistaken. Today, at any rate, I decided it would be better with self-aligning bearings at both ends, so I modified a spherical-bearing rod end to replace the journal. Today I also re-installed the nose gear retraction linkage with shims made from some .0025 stainless steel sheet that Dick Rutan gave me years ago, and I mounted two new tires, the nose and the right main, on their respective wheels. It's remarkable how much heavier a new retread tire is than one whose tread is worn out. Now that the nose retract arm pivots are tight again, the linkage is going to have to be readjusted, along with that of the sagging left main gear. The new gas springs are supposed to arrive on Thursday, so I hope to have most of this stuff taken care of by the end of the week. I have not yet tried to cycle the flaps.
Peter Lert pointed out to me that McMaster-Carr sells a complete range of gas springs (or gas struts, as I gather they should be called; I keep calling them gas springs to distinguish them from the landing gear struts). I don't know why I didn't think to look there, other than that when I searched for the part numbers of my old springs on line McMaster-Carr was not among the vendors who popped up.
[June 19, 2015]
I put the airplane up on jacks to swing the landing gear and replace the gas strut in the nose gear, which did not do its job of forcing the gear down against the airstream during the double malfunction of June 6. Gas struts lose their moxie over time, and this one had been in there for 12 years. I had probably hastened its enfeeblement by mounting it upside down. The longevity of gas struts is enhanced by mounting them with the rod downward. I probably did what I did because the rod ends it came with worked best that way. At any rate, the gas strut, which is supposed to have a force of 100 pounds, now has only 45. Finding a replacement is going to be a problem, because I can't find its part number in any of the online catalogs; I guess I'll put the old one back in for the time being. I was able to find replacement parts for the gas struts that hold the windows open; they too are getting weak, and I'm getting nervous about a gust of wind slamming a window on my fingers.
I found that one of the pivot bolts securing the retracting arm to the airframe was somewhat loose, so I took the whole apparatus apart to inspect it. The 5/16" holes in the anchor weldments are oversize by several thousandths, I don't know why; I hope to be able to fix the problem by inserting some very thin shim stock.
Some time ago, when I recorded the cycling of the landing gear with a small camera attached to a boarding step, I noticed that the left-side gear doors hung down a bit, and I wondered about the right-side ones, which could not be seen. On the jacks, the right doors close more or less perfectly. Having all three gears mechanically interconnected has some advantages, but ease of adjustment is not one of them. Correcting the 1/4-inch sag of the left main gear requires making a minute adjustment to the geometry of the retracting linkage. In the past I have made these adjustments by remanufacturing certain parts, moving a hole by maybe 20 thousandths of an inch, because doing it the easy way, by screwing a rod end in or out, would have the unintended effect of setting that gear leg slightly off vertical when lowered. I am wondering, however, whether it really matters much whether the gear legs are perfectly vertical. It's really just a visual thing, and for that matter sometimes they don't look vertical even when they are.
I have not even gotten around to the flaps yet. I'm hoping that bleeding them again will not be as big a job as it was the first time, because the hard part, the fluid in the lines between the master and slave cylinders, would not have been affected by the massive leak.
[June 12, 2015]
I got two Duralast batteries at Autozone to replace the two Yuasas. I decided to try the Duralasts because they are readily available off the shelf. They are identical in size to the Yuasas, but the terminals are slightly different -- just enough so that I had to replace a couple of the copper fittings I use to connect the two batteries to one another and to the airplane. An irritating thing about them is the size of the openings at the tops of the cells. They are so small that it is impossible to tell the fluid level by eye or, for that matter, even to remove the plugs with anything less than a pair of pliers. I suppose I will have to get a glass pipette to check fluid levels. (I chose the open cell type because the sealed "maintenance-free" version, besides being more expensive, has a different terminal configuration. If I had known that I was going to have to re-do the connections anyway, I might have gotten sealed ones instead. They have about 25% more cold cranking amps.)
Incidentally, the failure of the Yuasa was my fault; I had let the fluid level get too low.
Once the new batteries were in place and charged, I tried to retract the flaps, which were still extended a few inches, as they were all during the return flight from Paso. Nothing, but the sound of the hydraulic pump was uncharacteristic. Checked the hydraulic fluid level. Empty reservoir. Looked under the wings and fuselage. No leaks. Removed the floor under the rear seats, knowing full well what I would find: a big pool of hydraulic fluid, and a line that had popped off its connection to the retract side of the right wing root actuating cylinder.
That explained the failure of the flaps to operate and the gear to lock down, even though I had 28 volts from the alternator. The gear initially retracted because there was still fluid in the reservoir and lines. The gear circuit is separate from the flap circuit, so the leak did not affect it. But then, when I tried to retract the flap, most of the fluid ran out. When I lowered the gear for landing there was evidently just enough fluid left to release the up locks, but not enough to push the nose gear all the way down against the airstream and lock it. Since all three gears are mechanically interconnected, if one does not lock, none do.
What is surprising to me about this sequence of events is that two significant failures could occur at essentially the same time but, as far as I can tell, independently of one another. I can't see what the batteries have to do with the hydraulic plumbing. Besides, the connection that came apart was not even in a high-pressure part of the flap system; it was a line that supplies pressure to push the flaps back up. That takes almost no force at all; in fact the air rather pulls the flap forward. There is, however, a pressure spike when the flap reaches its up stop; I suppose it's most likely that the hydraulic failure had already occurred earlier in the day, when I retracted the flaps after landing at Paso.
Like everything, this has been instructive. For one thing, it's evidently time to get a new gas spring for the nosewheel; the one that's in there is 12 years old and didn't do what it's supposed to do, namely help the gear lock down. For another, I learned to be cautious about saying, "But what's the chance that X and Y -- two improbable events -- will both happen at the same time?" The chance may be small, but it's not an impossibility.
June 6, 2015]
I went to Chuck Wentworth's annual Antique Aero invitational barbeque at Paso Robles today.
When I tried to start the engine for the return trip, there was a moderately loud pop and the starter ceased to turn over. At first I thought something had broken, but after some discussion with Mike Melvill, who was there too, suspicion moved to the batteries, since after the failure the aircraft voltmeter was reading just 8 volts. I checked the batteries separately with a handheld voltmeter; one read 12.4, which is expected, the other 10.4, so that was obviously the bad one. The sound I heard must have had something to do with the failure of that battery, but I don't know what. Do batteries make a sound when they short? Anyway, the problem's onset was sudden: voltage readings and cranking power had been normal when I started at Whiteman in the morning and the electrical system had been behaving well for a long time.
One of Chuck's employees, whom I know only as Shannon, brought over their start cart. The plane started normally. As I taxied toward the runway, however, the system voltage kept dropping. Evidently there was insufficient field voltage and so the alternator was not charging. I tried to operate the flaps and nothing happened, so I figured it was a lost cause and taxied back. When I was in the taxiway approaching Chuck's, however, the voltage began rising rapidly and soon was at 28; evidently the field kicked in or I was taxiing at higher rpm. At any rate, I decided the alternator should be able to support the electrical requirements in flight, so I taxied back.
I again tried to lower the flaps, but they stopped at about four inches extension, I don't know why. I decided I would just have to see how the landing gear did in flight; if it would not retract I would return.
The gear did retract fully after I took off. The flaps, on the other hand, would not budge. That was a puzzle; the flaps should take much less power to operate than the gear. At any rate, I flew back with the flaps partly extended. I lost a few knots, but not many. The radios and other low-power services worked normally.
When I was six miles or so out of WHP I slowed to 100 knots and lowered the landing gear. It dropped, but did not lock down.
As I discovered a few years ago, because the hydraulic valves are closed-center it is actually possible to land even without the sway braces and drag links being locked overcenter. But I didn't want to take a chance, so I removed the acrylic window from the nosegear viewing hole (it's held in place with aluminum tape), opened the hydraulic bypass valve, pulled the gear breakers, put the gear handle in the down position and then with the aluminum pole I've been carrying around for 12 years against this eventuality I pushed the nose gear down and locked, as verified by the position of the big torque tube in the cockpit that connects all the gears together. When the nosewheel locks, the mains automatically lock as well.
The landing was uneventful.
I do not understand why the flaps did not operate even though the gear did, sort of. I do not understand why the gear went up but not down. Possibly there was still some power stored in the batteries when I took off, but raising the gear depleted it and flying for an hour did not restore it. The indicated voltage in flight was 28, as expected from the alternator, but the ammeter read zero, which means that the batteries were not taking a charge.
Question of the day: Should I replace just the bad battery or both of them, even though the other seems perfectly good? They are nearly three years old.
[June 2, 2015]
In another setback for dipstick calibration, I ran a series of tank volume analyses in Loftsman for a fuel depth of 4.38 inches at the dipstick and for several pitch and roll angles. Here are the results; roll angle is the horizontal axis.
So, while the quantity would be 12.7 gallons with the airplane level, it could be as little as 10.6 gallons with the wings tilted 2 degrees toward the tank in question and as much as 15.6 gallons with the wings tilted 2 degrees the other way and the nose pitched up 2 degrees. This seems to put paid to any idea of making precise measurements with the dipstick in the field. But since the purpose of the dipstick is not to measure fuel quantity before each flight -- the totalizer is supposed to take care of that -- but to get a precise reading from time to time in order to re-calibrate the totalizer, I can use a jack to level the plane in the hangar if it does not want to level itself. The saving grace of the errors is that the effects of pitch angle are rather small, and while those of roll angle are much larger (~1.1 gal/deg) they are linear across zero, so that the sum of the two tanks remains accurate even though the measures for each tank are wrong.
[June 1, 2015]
I drained the left fuel tank, which I had run pretty low, and put the fuel from it into the right. I then pumped fuel into the left tank, initially a gallon at a time and then at progressively larger intervals, up to 20 gallons, noting the dipstick reading after each addition. It was about the worst possible day to do it, warm, with a stiff breeze blowing, so that the fuel evaporated from the dipstick more rapidly than usual. Nevertheless, I collected a bunch of numbers which looked pretty random and strange until I got home and compared them with the calculated values. It turned out that they matched nearly perfectly, except for one. Unfortunately, that was the one for which I had jacked the plane up to a perfectly level attitude after returning to the hangar. It should have been the best match of all; instead, it was off by half an inch, or four gallons. To confuse matters further, the slightly higher wing at the fuel pump had been the left wing, and so the fuel depths I was measuring should have been larger than with wings perfectly level rather than smaller. Using the calculated calibration, I concluded that there was now around 7 gallons of fuel in the right tank, which was just what the totalizer said; but that didn't mean much, since I had set the totalizer on the basis of dipstick readings after the fuel spill of January 16. Still, any crumb of consistency is welcome.
[May 28, 2015]
It occurred to me yesterday evening that I should look at the EGT differences in terms of temperature rather than fuel flow, so this morning I printed yesterday's graph, drew a vertical line through peak EGT on the TIT (which I use to set the mixture) and then measured the temperature difference between peak EGT on each cylinder and the point where its curve crosses the peak TIT line. Given the imprecise nature of the data, the three right-side cylinders, 1-3-5, are at or within a couple of degrees of peak EGT; the three left side cylinders, 2-4-6, are richer by 8, 10 and 2 degrees respectively. The differences are inconsequential.
I ran the fuel in the left wing down to a couple of gallons yesterday; now I can drain it and then add a gallon at a time to calibrate the dipstick. I also need to install the landing light, although I don't have too clear an idea of how it should be aimed.
[May 27, 2015]
We got back from Cape Cod last Thursday, but one thing after another prevented me from going to the airport until today. The first thing I did was fly for an hour and a half and take another set of EGT measurements. The new #2 and #5 injectors have brought those cylinders into closer alignment with the others. This is what the sweep looks like now:
All cylinders peak within 0.2 gph of the average except #4, which is now the outlier at 0.3 gph. The interesting thing is that the left side of the engine (cylinders 2-4-6) is richer than the right. I suspect that this could have something to do with the 90-degree bend in the induction pipe just before it reaches the throttle body, but it would be hard to be sure because the injector flows have been fiddled with so much. In any case, they are now much better than they were after the intake manifold modification, and the engine leans beyond 100 degrees lean of peak while remaining perfectly smooth. When I finished the test I left the fuel flow at 7 gph, which gave 157 ktas at 10,000 feet density altitude and 22.3 nmpg. This presented a gratifying contrast with the Comanche 250 in which I learned to fly; it cruised at the same speed using 14 gph.
[April 17, 2015]
Leaving for a month. Til we meet again...
[March 27, 2015]
The dipstick handle now has two tiny (.047 piano wire) prongs with which to unscrew the access caps. I have but to calibrate the dipstick itself. I have a table of fuel surface heights versus volume, but I need to fine tune the relationship of the table to the dipstick and, for that matter, verify empirically that my calculation of fuel volume is correct. It was done in Loftsman by the typical digital approach of dividing the wing up into 1-inch wide slices, and then slicing these airfoil-shaped slices again into 1-inch wide columns and finding the volume of each one from the bottom inner skin to the fuel surface, and finally summing up this Giants' Causeway of avgas into one portable and compendious ocean. The accuracy of the dipstick depends on the airplane being level, which I can assure with the spirit level app in my phone; the surface of the wing centersection, under the front seats, is nominally level. I guess I should also do the volume analysis for a couple of fuel heights and pitch and roll angles, to get an idea of how sensitive the dipstick reading is to airplane attitude. Obviously, this is of concern mainly at low fuel levels, but they are the ones that are mainly of concern.
GAMI send me a couple of replacement injectors for my #2 and #5 cylinders, which are still the outliers. I installed them -- I'm getting quite good at it -- and in the next few days I'll do another EGT survey.
Digging around in my midden heap today for some 1/8" I.D. thin-wall flexible tubing with which to plumb my wake rake -- I didn't find any -- I stumbled upon a 20-inch piece of 1/4" auminum tubing, which I needed to complete the re-routing of the fuel vent in the right wing. I knew I had some somewhere. The price at Vista is extortionate. Twenty inches wouldn't have come to much more than Nancy's and my morning coffees and scone (which we share) at Fix, the trendy local espresso joint, but I hate to pay for something I feel certain I will find on the floor if I just walk around long enough with my eyes cast down.
[March 25, 2015]
I installed the dipstick ports in both wings. Although I originally thought each plug would have a built-in dipstick, I decided today to use a single, separate dipstick combined with a tool for extracting the plugs by means of the two small holes drilled in them. After fiddling with various materials I found that a narrow strip of the same carbon fiber material that I used for my wing spars shows a wet surface long enough to permit a reading. I will need to calibrate the dipstick and mark it with some kind of paint that can be applied with a fine brush. I have a calculated calibration, but I need to confirm it by filling a tank one or two gallons at a time. The wings actually hold 70 gallons each, but since the plugs are below the highest point it will not be possible to dipstick more than 45 gallons. I have never yet put that much fuel (90 gallons) in the plane and in any case the purpose of the dipsticks is not to check fuel quantity before every flight but rather to verify and if necessary reset the totalizer from time to time. In the past I have done this by attaching plastic hoses to the quick drains and measuring the fuel height; it is such an inconvenient process that I have not done it so often as I should. The dipstick will be much more convenient.
[March 20, 2015]
I have done a few minor things in the past week or two. I added a three-inch chimney to the baffle outlet on the #3 cylinder to see whether it affects the cooling at all. An NACA technical report says it will, and the test cylinder was almost exactly the same size as mine, but my chimney is only above the cylinder barrel, not the head, and so any beneficial effect may be imperceptible.
I machined a lot of material off the housing of the landing light, thereby reducing its weight by 1/2 pound.
I cut holes in the tops of both wing roots for the dipstick ports which my neighbor John Biggs is machining for me, but I have not yet bonded the metal ports into place. I did, however, measure the fuel levels through the holes, and it coincided quite closely with what the totalizer said. I had reset the totalizer after the fuel spill incident of January 14, using plastic hoses connected to the sump drains to ascertain the fuel levels.
Biggs also brazed four S-shaped 1/8" stainless steel tubes to a thin rectangular plate which I intend to tape to the top of the cowling behind the cowl outlets to measure the velocity of the emerging cooling air. I'm not sure how well duct tape -- the usual temporariy fastening method for aerial experimenters -- will hold up in a stream of 150-degree air, but in any case I can secure the wake rake to the cowling with safety wire so that even if the tape comes loose the rake will not fly back and gouge the windshield. I installed four 1/8" tubes passing through the firewall (in addition to a couple that are already there for measuring pressures within the cowling) and connected them to a manifold of four air valves that I got at Petco; it's intended for aerating several aquaria. This rig should enable me to ascertain the mass flow of air through the cowling -- which I already know to a good approximation, since I know the pressure drop ("delta p") and the relationship between pressure drop and cooling air flow rate is part of the published description of the engine. But it is always nice to see numbers from different sources confirming one another.
[March 6, 2015]
Now that I've messed up the cowling air inlet by providing it with strange ducts and ramps, I need to repaint it. The problem is, how to paint down inside those narrow, curving ducts. A paint roller about one inch wide and one inch in diameter would do it, but Googling "narrow paint rollers" brings no relief. Perhaps I could make such a roller out of a sponge and a wire hangar. I am a do-it-yourselfer, after all.
[March 5, 2015]
I did the tank vent modification on the left wingtip. I siamesed two 1/4" aluminum tubes together by bending an arc at the end of each and then cutting them off flush with the side of the straight part of the tube. The two bent ends mated neatly, forming a sort of gothic arch, which I sealed with JB Weld. I drilled in from the tip to a point close to the present vent, which I cut off at the outside surface of the end rib of the tank, working through an oval hole I had cut in the saddle between the wing and the upturned tip. I was then able to insert a short length of tubing through the portion of the vent tube that remained in the wing -- the old vent was 3/8" tubing, so the 1/4" tubing fits loosely inside it -- and pot it in place. After inserting the new vent through the drilled hole, I connected it using short lengths of Tygon tubing. Finally, I sealed and contoured the hole at the tip using an epoxy-microballoon paste and temporarily covered the hole at the inboard end with aluminum tape. Eventually I'll add a ply of cloth over it and refinish the scar, but not before doing the same mod on the right wing and flying for a while to be sure nothing is wrong with the venting.
[February 19, 2015]
Nothing done yet on the tips; I've been rebuilding a rotten kitchen counter. I did go flying today, however. Not a very nice day, very hazy, but calm and smooth. Since I was not going anywhere, I backed the power down to 24/2150, 50 LOP, with a fuel flow of 5.7 gph, or around 40% of power. At a density altitude of 6,000 feet, this gave a true speed of 137 knots, or 28 statute miles per gallon at 157 mph. I'm proud of those numbers, in a four-seat airplane with 3,000-mile range, although, to be honest, they are at about 900 pounds below gross weight. The cowl flaps were completely closed, so the exit area was 20 sq. in. Delta p was 4.1 in. H2O, hottest cylinder (#3) 380 F.
I discussed this unexpectedly good performance at low power settings previously, here. (In that case, I was at 14,500 ft. d.a. and the true airspeed for the same fuel flow of 5.7 gph was 157 knots, not 157 mph.) What I did not mention then is that it is not impossible that the parasite drag coefficient increases with speed. For instance, the faster I fly the more the landing gear doors tend to bulge or flex outward, presumably increasing the parasite drag coefficient. On the other hand, my performance prediction program does include a factor to cover that eventuality -- an empirical correction based on the assumption that the parasite drag of many components, notably the wings, is likely to increase with increasing angle of attack. The more likely cause of the anomaly -- which is only an anomaly in the sense that the performance of the airplane doesn't agree with the computer program -- is an erroneous assumption about specific fuel consumption on the part of the program. It thinks the sfc ought to be 0.514 at this low power setting; if it were 0.47 instead, the numbers would match. Can a TSIO-360 Continental, running 50 lean of peak at 35-40% power, achieve an sfc of 0.47? I don't know.
[January 31, 2015]
I spent way too much time thinking -- see previous entry -- about the question of where to put the vent outlet at the wingtip to ensure 1) positive pressure and 2) freedom from icing before Dan Fritz, an RC modeler whom I have never met but who is a good epistolary friend, gently pointed out that the vent line does not have to open at the tip. It's enough that it merely ascend to the tip; it can then drop back down to its present outlet, in a cavity with a non-icing NACA flush inlet in the lower surface just outside the tank. I'm embarrassed to say that this never occurred to me. If it had I might have thought at first that there might be some siphoning problem, but after a Gedankenexperiment or two I would have realized that while there is a scenario in which siphoning could occur, the possibility is sufficiently remote that the advantages of the "rising loop" vent clearly outweigh it.
[January 22, 2015]
After reflecting a little more upon the fuel venting issue I realized that the best solution might be to run the tank vents up the upturned tips. That would put them high enough that no likely amount of tilt would make fuel flow out of them. Fortunately, this would not be very difficult to do; at least I don't think it would. The question then is how the vents would terminate. Often vents stick straight down out of a fuelage or wing and are cut off at a 45-degree angle facing forward, so that a slight overpressure is supplied to the tank. The overpressure is not really needed, but it provides insurance against a possible underpressure due to the local curvature of the surface from whiuch the vent protrudes. You don't want underpressure because you don't want to do anything to impede the flow of fuel to the engine. I could have the vent open at the leading edge of the tip, but the problem with that location is that it would be susceptible to icing. An aft-facing vent at the tip would be staring right into the center of the tip vortex, which is a low-pressure area, so that may not be ideal either.
Don't bother me. I'm thinking.
[January 16, 2015]
Wednesday, the 14th, was a rather eventful day for Melmoth 2. I flew to Las Vegas to pick up a couple of friends and bring them back to LA. We were in the middle of the takeoff roll at North Las Vegas when there was a change in the engine sound and the manifold pressure began to fluctuate. I aborted the takeoff. On removing the right side panel of the cowling we found that a slip joint in the exhaust had parted. I had thought that the geometry of the system made that impossible, and so I had not installed the solid link between the pipes that is supposed to prevent it; I was evidently right for 11 years and a few months, and then wrong. A very friendly A&P, Lenny at EGA Aviation, tied the pipes back together with multiple loops of safety wire and we were on our way. With a nice 15-knot tailwind, we saw groundspeeds around 200 knots all the way to Whiteman, where we left the plane in its hangar.
Late that night, I got a call from the airport saying that avgas had been flowing out the front door of the hangar, and they had had to cut the lock to get inside. There they found the plane listing to port at a crazy angle and fuel running out the tank vent at the wingtip. They collected a bunch of fuel in a jerrycan before finally lifting up the wing and putting a support under it. I came back the next day to find a huge amount of what looked like kittylitter on the hangar floor; it's some sort of absorbent stuff that they use for fuel and oil spills.
This had happened once before, on the way to Oshkosh in 2006 or so. I stayed overnight in Prairie du Chien (which means Dog Prairie, as opposed to Prairie Dog) and in the morning came out to find the plane tilted and a huge fuel stain spreading over the asphalt ramp. That time I dismissed it as a freak event related somehow or other to heavy tanks and a soft strut. That was probably basically right, but this time I gave it a little more thought. The only scenario I have been able to come up with is the following. A couple of days before the flight, I had added air to the right main strut, but I had not been careful to match it to the left otherwise than by eyeball (ideally, there should be 2.25" of exposed piston on each side). On the trip from Las Vegas to LA, the back-seat passenger sat on the right side, and so I fed more fuel from the right tank than from the left. This left the plane somewhat left-wing-heavy and with a softer left than right strut. It looked normal when we closed the hangar, but perhaps the drop in temperature during the late afternoon -- the Prairie du Chien incident occurred at night -- caused the left side to settle a little more. Now, the wings have comparatively little dihedral -- 3.2 degrees -- and when there is a fair amount of fuel in a tank to begin with it does not take a lot of tilt to start the fuel spreading out toward the tip. Evidently, as fuel moved outward the left strut must have settled further while the right one possibly extended a fraction, and so more and more fuel flowed outward in a vicious cycle that ended with it reaching the vent and running out.
I have been thinking about ways to prevent a recurrence of this embarrassing and costly contretemps. One would be to take a piece of 1/4" wall, 1.5" I.D. aluminum tubing and divide it lengthwise to make two pieces that would fit up against the backs of the exposed pistons when the plane is parked. If you didn't notice the big red flags and took off with them in place, they would fall away. You would use them only when there was sufficient fuel aboard to produce the imbalance.
[January 8, 2015]
I measured the pressures in the upper and lower plena. Here is the summary of the results, including the corresponding data from 11/09, before the intake manifold modification.
Beginning at top left, the first two frames show raw pressures, relative to the aircraft static system, in the lower (inlet) plenum and the upper (exit) plenum respectively. The slight downward drift of the lower plenum pressures with increasing cowl flap opening is due to the diminishing resistance in the upper plenum. The marked concavity of the upper-side pressure curves, compared with the expected straight-line variation in outlet area between 20 and 80 square inches, suggests that some extraction effect may be taking place with intermediate cowl flap settings. This may be wishful thinking; no doubt an observer less eager than I to feel that reversing the intake manifold was not a complete waste of time might find some other plausible explanation.
The right-hand chart on the top row shows lower plenum pressure and available dynamic pressure, or q, against indicated airspeed. For some reason, nearly 100% of pressure is recovered at 80 knots, but only 86% at 140. Perhaps the cowling inlet flow is affected (adversely) by Reynolds number.
The bottom row contains three versions of the same variable, namely delta p, or cooling air pressure drop across the engine. The two on the right are the ones I showed on January 4, below, that is, the current measurements and a set taken in 2009, before I reversed the intake manifold and cleaned up the exit airflow. The left plot is the difference between the first two plots in the top row, that is, the upper-plenum pressures subtracted from the lower-plenum ones. In principle, it ought to be identical to the direct measurement of delta p (middle plot, bottom row). In fact, the results coincide nicely at 80, 100 and 120 kias, but the results for 140 kias are quite different. I don't know how to account for this, but I will continue to take delta p measurements in the future at cruising speed (which is usually around 140 kias) to see how they compare with these.
[January 4, 2015]
On the 2nd I collected better-quality data on delta p -- the pressure drop across the engine, and the primary determinant of cooling -- than I got last July after I reversed the intake manifold. It's interesting to compare these data with those from 2009, when I had neither uncluttered the low pressure plenum above the engine nor cluttered up the air inlet with weird ducts. Here are the two data sets side by side (the 80, 100, etc are indicated airspeeds in knots):
There is some imprecision in both data sets, because the cowl flap openings cannot be set exactly. I marked half-inch increments on the side of one flap, which I can see from the cockpit, but their setting is still only accurate to, say, plus or minus a tenth of an inch. Still, two observations about these data can be made. One is that the maximum delta p at 140 knots is now less than it was four years earlier. This could be due to energy loss in the inlet because of the guide vanes I added there. (The reason for those vanes can be found here.) This is a change for the worse, but at least it is at high speed, where cooling effectiveness is not an issue. I should note that the 1.5-inch opening is the largest used for climb; the 2-inch opening is used only on the ground because it provides no additional cooling in flight, but some additonal drag.
The other difference is that delta p is now consistently higher with partially closed cowl flaps. It would be nice to think that it is due to my having removed obstructions from the upper side of the engine. It may be that removing the transverse intake-manifold tubes, which impeded air approaching the exits, improved the aerodynamics of the cowl flaps in a way that is most noticeable in just a limited intermediate range of positions -- a "sweet spot". This is not implausible; the cowl flaps are analogous to a slotted flap, and the aerodynamics of such flaps is sensitive to slot geometry. I do think, however, that the difference, whatever the reason for it, is real, because it is too large to be accounted for by the uncertainty about cowl flap positions.
Next week I will collect data on absolute pressures in the high- and low-pressure plenums. I have the corresponding numbers from 2009. Perhaps they will shed some additional light. The delta p change could be accounted for by increased pressure in the lower plenum or decreased pressure in the upper one; increased pressure in the lower one is, frankly, unlikely.
[December 19, 2014]
A couple of days ago I finished off the layups in the fancy new -- but seemingly not especially effective -- cowling air inlet. My epoxy pump was acting up, so I mixed the epoxy using a balance scale I made years ago out of a few pieces of scrap wood and aluminum and a couple of nails. It works extremely well and is probably more accurate than the pump, which is long overdue for a cleaning. My epoxy is all out of date, but since none of these parts is structural that doesn't matter; it still hardens in the expected time and manner. Now I just have to paint the whole thing -- never my strong suit.
At the suggestion of Peter Lert I ordered an off-roader's running light to use as a landing light -- just pro forma, since I don't fly at night any more. Although small -- 5.5 inches long and maybe 1.25 inches wide -- it was incredibly heavy at 20 ounces. Most of this weight was for a heat sink with half a dozen massive fins. Since the whole thing draws only 18 watts, it's hard to see why it needs such an impressive heat sink. Perhaps it was adapted from an earlier product that used halogens, which give off lots of waste heat. In an effort to get rid of some of the weight I started cutting it apart, and in so doing inadvertently damaged a printed circuit. I ordered another one -- they're fairly cheap, $40 from JC Whitney -- and with what I learned while ruining the first one I think I will be able to machine away at least half the excess weight; the walls of the housing surrounding the lights are about 3/8 of an inch thick. I intend to attach it to the right main landing gear. It's rated for 12 or 24 volts, but I ran it for a while on a 28-volt power supply and it seemed happy enough.
I never get much done during the holidays, and these will be no different.
[December 10, 2014]
A basic measure of cooling efectiveness is delta-p, the pressure drop in cooling air flowing through the cylinder fins and baffles. Ideally, the baffles should block all air flow except through the cylinder fins, and should force air to flow equally over the front and back of each cylinder. In reality, there is some leakage through baffles, and not all cooling air is effectively used. Setting aside those losses, two factors determine delta-p: the pressure recovery in the high-pressure plenum, which in my case is below the engine, and the resistance encountered by air on the way overboard after having passed across the engine. The project of reversing the position of the intake manifold was intended to remove obstructions on the way out; the modifications I have been making to the cooling inlet are intended to reduce losses associated with air entering at high speed and coming to a halt in the plenum. Today I took a few measurements of delta-p that can be compared with ones taken prior to these modifications. There appears to be a slight improvement, but, considering the expected margin of error, it is insignificant.
[December 6, 2014]
As long as I was remodeling the cooling air inlet, I added a ramp in lieu of the vertical barrier, about 9 inches behind the inlet lip, where the front of the nosegear box/engine mount is. I flew yesterday for the first time with the new inlet configuration. The ambient temperature was lower than it has been in the past weeks -- 43 deg F at 10,000 feet -- and I have not collected CHT data systematically in the past, so I have only subjective impressions to go by, but the cooling seemed very good. The oil temperature was down a bit, but not as much as I'd like; still, it was down by more than the ambient temperature drop, so I feel pretty satisfied with the changes to the inlet. I can now set aside the hacksaw with which I was prepared to remove everything I'd added. Apart from making sure I had not dealt a fatal blow to the engine cooling, the purpose of the flight was to collect EGT data in order to evaluate the effect of changing the #2 injector. It looks at though #2 is still way out of line with the others. In fact, it looks worse. I wonder if the correction was accidentally made in the wrong direction. Next week I have a flight to Paso Robles that will give me an hour in which to collect another set of EGT data and also to get definitive delta-p measurements using the new inches-of-water gauge. Incidentally, it's very satisfying to press the rocker switch that controls the cowl flaps and see the delta-p gauge instantly react.
[November 15, 2014]
Back from the east late Wednesday, went Thursday to get my medical renewed, then by the airport to visit the plane. My pitot-static cert expired while I was away, so I won't be able to fly until I get that done next Wednesday. I was hoping to find the replacement injector for the #2 cylinder waiting when I arrived, but it had not yet come; they are running several weeks behind at GAMI, I hope because of a surfeit of orders.
While I was away I visited Randy Greene, an old friend who is CEO of Safe Flight Corporation; they make all sorts of equipment ranging from leading edge stall warnings to autothrottles and other such fancy stuff. We flew the company's 172, which is a testbed for their new angle of attack system. This is a completely revised version of the system in my plane; it uses different electronics throughout, although the leading-edge tab that serves as a flow condition sensor is externally similar to mine. The display, which sat atop the panel in the middle of my line of sight, consists of a stack of green, yellow and red lights. Randy and I have argued for years, nay decades, about the proper orientation of the display in my unit, which is an edgewise meter with a moving pointer. I feel that the instrument is essentially an attitude indicator; when the nose is high, the needle is at the top. He -- and unlike me he owns a couple of jets and is used to flying that sort of heavy metal -- sees it as a flight director; if the nose is going upward, the needle should go downward, meaning "put the nose down" or, alternatively, "your speed is too low." The new instrument takes my view of the matter -- as do other angle of attack displays now on the market -- but Randy has not conceded: The Safe Flight label on the side of the instrument was upside-down. I doubt, however, that that will be the case on production instruments.
Our flight in the 172, which was supposed to acquaint me with the use of the new display, mainly reminded me of how different the 172 is from Melmoth 2, which is practically the only airplane I fly these days. In my airplane, approaching at 70-75 knots, you have a fairly dynamic sense of your energy vector; in the 172, which seemed more like a helicopter, you don't. I felt that we were barely moving on short final, although we were probably only 10 knots slower than Melmoth. Control forces, especially in pitch, are also much higher than in Melmoth, and control responses much less crisp. In short, I was so preoccupied with the unfamiliarity of the airplane that I took no note at all of the AoA indicator during the final stages of the approach -- just where it is supposed to matter most.
[October 18, 2014]
The cowl flap mod was a complete failure. The cowl flaps still come to a halt 1/4 inch before closing at their trailing edges; evidently this is a function of air pressure on the aft portions of the cowl flaps overpowering the motor, not, as I had thought, distortion of the actuation geometry owing to internal pressure on the cowl itself. Now that the clutter on top of the engine has been cleared away it may be possible to revise the geometry of the cowl flap actuators to provide longer lever arms, but that won't help unless the travel of the jackscrew can be increased, and I don't think it can.
On Thursday of last week I collected a new set of EGT data. These numbers, while better than the last set, are still not entirely smooth, but they are a starting point for revising the selection of GAMI injectors to match the new flow conditions with the reversed intake manifold. Because there is more scatter among the EGT peaks than there used to be, I can no longer run as lean as I used to, and so my typical power settings for a given speed have changed. With the stock intake manifold and the standard set of GAMI injectors for my engine, I used to cruise, normally at between 12,000 and 15,000 feet density altitude, at 27 in. Hg and 2,300 rpm, with a fuel flow of around 8.6 gph and a true airspeed of 175 kt (20.35 nmpg). Now, with the mixture distribution somewhat messed up, I set up 26 in Hg and 2,350 rpm at 12,500 feet density altitude and began to detect roughness at 9.3 gph and 176 ktas (18.92 nmpg). Peak EGT at the turbocharger inlet came at 11.1 gph and 190 ktas (17.17 nmpg). I would rather be at 20 nmpg than 17, even though the price of avgas at Whiteman just dropped from $6 a gallon to $5.75.
One way to look at the EGT peaks is in terms of their offsets, in fuel flow, from the average, which is also the peak turbo inlet temperature. The numbers, going from cylinder 1 to 6, are -0.13, -0.53, +0.37, +0.07, +0.37, -0.13. In other words, for example, the #1 cylinder reaches peak at a fuel flow 0.13 gph leaner than peak TIT; it is therefore slightly richer than the average. The most egregious outlier is #2, and so the first step will be to replace it with a leaner one to bring it into better agreement with the others. Then I will do a new sweep and see what else needs to be changed.
[October 11, 2014]
During the past couple of weeks I've taken care of some deferred maintenance and made a couple of minor modifications.
I rebuilt the left outboard flap actuator, which had been leaking for some time with sufficient volume to leave a trail of hydraulic fluid down the underside of the wing. It took me a couple of rebuilds to get the one on the right side to stop leaking -- the design of the cylinder is admittedly defective -- and I hope that this one will now finally stop as well. I have not seen any fluid yet after several in-flight cycles (cycling on the ground, without aerodynamic loads, does not put enough pressure on the cylinder to reveal a leak).
I installed the EGT probe that I got on eBay. It works, but I have not yet done the mixture sweep that is needed to figure out how to rearrange my GAMI injectors to get all cylinders to peak closer together, as they did before I turned the intake manifold around.
I modified the sheet-metal chimney that conducts air overboard after it has passed though the oil cooler. I had used wedge-shaped ducts on both the inlet and outlet sides, but on perusing Paul Lamar's book on cooling rotary engines I noticed that more of an open plenum on the outlet side is apparently preferable.
I replaced the now torn aluminum tape with which I had sealed the gap where the left intake runner passes through the rear baffle with a gasket of sheet silicone; the tape on the right side is still holding together, so I won't bother with it for the time being.
I also began a little project that I have been intending to do ever since I put the final cowl flaps into place in 2006. In principle the trailing edges of the cowl flaps are supposed to close completely, but in fact, I think because bulging of the cowl under pressure slightly changes the geometry of the actuation system, they remain open about a quarter of an inch. This is inconsequential, and may even be beneficial, but I'm moving the travel-limit microswitch from the actuator itself to the cowl flap so that the motor will continue to run until the flap is actually closed, regardless of the pressure within the cowl.
[September 25, 2014]
I solved the problem of the inaccurate inches of water gauge by making a new dial, which I calibrated with my manometer and glued to the front of the instrument. I bought a used EGT probe on eBay; it came today, and I hope to get it installed tomorrow. That will make it possible to do a proper EGT survey and get the peaks for the respective cylinders aligned. George Braly at GAMI was shocked that I use an Alcor analog EGT instrument, and urged me to get a proper engine analyzer. I objected that they are rather expensive, and he replied that most pilots find that they pay for themselves in reduced maintenance costs. He forgot that I have almost no maintenance costs, since I do my own maintenance. I'm trying to stretch out my engine's life so that it and I die at about the same time, since there is no possibility of my being able to afford an overhaul.
While I'm on the subject of money, people sometimes wonder what it cost to built Melmoth 2. The answer is not entirely meaningful, since I already had the engine, instruments, hydraulic pump, and so on, and much of the carbon and glass fiber that I used was given to me; but my materials and services invoices for the 20-year construction period, which I kept for tax reasons, added up to $17,000.
Today I picked up Dan Raymer at Hawthorne and we went to Catalina for lunch. Both airports charge $25 landing fees. At Hawthorne I was at least able to land a second time to drop him off without having to pay again. I always thought Catalina was a special case; I wonder how many other airports have these fees, or will begin to have them. Needless to say, I won't be landing at Hawthorne again soon. Raymer brought along two floating seat cushions for the trip across the channel. Oh ye of little faith! But they are very light in weight and would certainly be preferable to treading water for a long time. My strategy for the 20-mile strait has always been to climb to 5,000 feet by mid-channel; that way I could glide to either side even if the engine were to fail at the worst possible moment. Really, however, one should worry more about engine failures over the city, where the chance of emerging in one piece is much worse.
[September 19, 2014]
I swapped the #1 and #3 EGT wires -- but not the probes this time -- back to where they started from. Now it's the #1 indication that's dead; so the problem is the thermocouple. And I tried out the new inches of water gauge, which turned out to be a huge disappointment; it's completely inaccurate, indicating anywhere from 35 to 50% higher than it should. I also observed that enlarging the outlet of the right-side inlet vane did not have much of an effect on the right-side CHTs, if any. Finally, I checked the induction air temperature while descending at low power and essentially no boost; it was 55 C, much lower than any in-flight oil temperature, and made me wonder whether my my breast-beating over forgetting which way the oil/induction temperature toggle was supposed to point was really warranted. I sink ever deeper into bafflement.
[September 18, 2014]
Although President Obama has taken some flak for saying that a basic principle of his foreign policy is "Don't do stupid stuff," I think that's a really pretty good rule. The problem is to tell what's stupid and what isn't. Sometimes when you're doing something stupid you're thinking it's smart. I suppose I set the bumbling bar pretty high with my confusion over the oil and induction air temperatures -- see the previous entry -- but just because you made one really big mistake doesn't mean you're done for the year. Here's proof.
For a while my #3 EGT indication has been kaput. When the selector switch hits #3 the needle drops over to the left as if poleaxed. The question is, what has failed? The candidates are the probe itself, the connections between the probe and the wires going to the instrument, the connections between those wires and the rotary switch on the indicator, the rotary switch itself, and, rather improbably, the wires themselves. I know the indicator is good because it works for all the other cylinders.
After procrastinating for a suitable period, I decided the time had come for action. So I swapped the probes between the #1 and #3 cylinders, along with their respective wires. Now, that was stupid. I hope someone reading this has to think for a few seconds before realizing why. All I did was move the problem from one cylinder to another. It's as if I heated the probe with a match, and then "tested" it by heating it again with a different match. Needless to say, the behavior was unchanged: when the selector hit #3, the needle keeled over. That was embarrassing, but at least it's over now. I did inspect the connections between the probe and the wires that connect it to the instrument; they were secure and the crimped connectors appeared sound. A little bit of insulation looked a bit scorched, but I didn't think enough to damage the wire. I wish I had had the presence of mind, while I was in the air today, to reach under the panel and wiggle the wire bundle connected to the selector switch. If there's a bad crimp or a loose screw there the needle might jump around a bit.
All of this is important to me because I feel that I can't lean as much before the onset of roughness as I could before I turned the intake manifold around, and the cause is almost certainly that the orifices of the GAMI injectors that worked on the stock manifold are no longer suitable for the reversed one, even though I reversed the injector positions along with the manifold. I need to get smooth, high-resolution EGT data for all six cylinders to see.
In the meantime, I bought an inches-of-water gauge on eBay. It had just a single port, so I added a second port for a reference pressure and sealed the case with epoxy. It will be a more convenient and accurate way to survey cowling pressures than my old water manometer was.
[September 13, 2014]
The areas under the right and left cooling inlet vanes are the same -- about 8.5 square inches each -- but the outlet on the right is about 10% smaller than that on the left. I hope that is the reason for the right bank of cylinders now running 20 deg C hotter than the left. Next week I'll raise the trailing edge of the right vane and see if that helps.
In the course of my months-long investigation of a rise in indicated oil temperature that occurred around December of last year, I compiled a list of all mentions of oil temperature in this document and also of any indications of what could have happened, or what I may have done, to cause the apparent change. The timing of the event was blurred by a period during October and November when the oil temperature and/or induction air temperature indications became intermittent. Both are displayed on the same instrument, selected by a toggle switch which, perhaps significantly, is unlabeled. When the toggle switch is to the left, oil temperature is displayed; to the right, induction air. (Induction air temperature is of interest because compression by the turbocharger raises its temperature significantly.) I always intended to label the two positions of this switch, but for varous reasons never got around to it. I believed, however, that the difference between the readings was obvious and so labels were not really necessary. Cleaning some connectors and repairing some frayed wires eventually cleared up the intermittent indication; I calibrated the temperature probes in the process and found them accurate.
Looking back over the history of oil temperatures going all the way to the fall of 2002, when Melmoth 2 began flying, I found a general pattern of temperatures around 90-110 C depending on flight condition (climb, cruise) and ambient temperature, until I installed the duct that isolated the oil cooler flow from the rest of the cowling. (The oil temperature redline is 116 C, but the desired continuous temperature is around 80 C.) I identified the high temperature of the air entering the oil cooler from below -- around 60 C, or 140 F -- as one of the likely causes of the high oil temperature. The exhaust pipes were evidently heating the air on the "cold" side of the cowling. After I installed the duct I reported that the oil temperatures were now where they were supposed to be, around 80 C. That was in February, 2010. In June I recorded an oil temperature of 88 C; the weather had warmed up a bit. Between then and 2013 I stopped mentioning oil temperature as an issue, but in a table compiled in May 2012 the oil temps appear all to be in the expected 80 C zone while the induction air temps are unexpectedly high -- 90 to 100 C. Over the years I had from time to time noted that the IATs were surprisingly high, and attributed that, somewhat illogically, to the way the probe was mounted at the dead end of the intake manifold, which is on the hot side of the cowling.
A few days ago it occurred to me to check another source of oil temperature data, namely photographs taken in flight in which the instrument panel is visible. In three photos taken between January and July 2011, the toggle switch is to the right; that is, it is displaying induction air temperature, which is 75 or so in the two pictures in which the gauge is readable. All this time, however, in my mind the default position of the switch was "oil," not "air." If I checked IAT at all, it was by switching the toggle to the opposite setting and then back.
Although the evidence is circumstantial, I now suspect that the rise in oil temperature in December of last year, for which no explanation or solution could be found, was not a rise at all; it was a change in the position of the toggle switch, resulting from the testing and calibrating that took place in November. That activity would have dispelled my apparent confusion -- suggested by the photographs in which the toggle switch is to the right -- over which toggle position was oil and which was air. The implication would be that IATs have always been in the 70-85 C range; that oil temps have always been in the 90-110 C range; and that seasonal variations in outside air temperature, and the contiguity of the two temperature ranges, tended to mask my confusion about which reading was which.
This is mortifying. I feel like an old lady who, finding a pair of expensive earrings missing, reports her housekeeper and gardener to the police, only later to find the earrings under her bed. If I am right, then the problem of high oil temperatures remains unsolved, but the supposedly sudden change in December of last year turns out to be a muddle, not a mystery. I humbly apologize to all those readers who took the time to think about the question and write with their suggestions.
[September 11, 2014]
I spent the first half of the week putting a vane into the right side of the engine cooling air inlet to match the one that I had put into the left. The one on the left side had lowered the temperature of air going into the oil cooler by 25 deg F, and had had the unexpected benefit of evening out the CHTs on that side. I hoped the one on the right side would have the same effect on the CHTs, and indeed it did, but it also pushed them up quite a bit, so that I saw 430 while climbing, which is unacceptable. (It was a fairly hot day, 94 on the ground, 55 at 11,500 feet.) The (slightly) hottest cylinder is now #3 rather than #1. It's interesting to see that relatively small changes in the inlet geometry can have such big effects on the CHTs; I just wish it were more obvious to me what needs to be done to get all the temps on the right side to come back down (other than just remove the vane on that side). The temperature rise across the oil cooler exceeded 90 deg F today; that is so large that it got me wondering whether the air outlet is too constricting and is slowing down the air going through the cooler.
[September 4, 2014]
Just to make sure that several previous checks of the functionality of the Vernatherm (which is supposed to regulate the oil temperature at 77 C (170 F)) were valid, I took it to Pacific Oil Cooler Service where they tested it and declared it okay. Not to be unduly easily persuaded, I asked them to lend me another one to try. They did. I flew with it today and found that it made no difference. At 8,500 feet, OAT 21 C, I was seeing about 180 ktas at 9.2 gph; the oil temperature settled at 110 C or 230 F. The seat against which the Vernatherm closes looks and feels smooth and undamaged. I will try to take a photograph of it tomorrow.
In the meantime I made the vane for the right side of the air inlet and also wrapped the exhaust pipes closest to the battery and the oil cooler intake duct with some sort of insulating stuff. One heartening observation was that when I was holding short for several minutes waiting for takeoff clearance, OAT about 85 F, the temperature of the hottest cylinder stabilised at about 160 C (320 F). The CHTs used to slowly climb and climb during long holds, so it may be that getting rid of all the obstructions in the way of the cowling air outlets actually did have a beneficial effect.
A reader wrote to tell me that the heat capacty of air is around one degree Kelvin per Joule per gram. Armed wth that information, I was able to do a quick sanity check on the heat rise across the oil cooler, based on the fuel flow and a general rule that around 8% of the energy in the fuel goes away through oil cooling (and 12% through cylinder head cooling). It came out to 70 degrees F, if I did the math right, and since the measured value is 80, at least it's in the ballpark. I was worried that it would be out by an order of magnitude, or maybe two.
I have probably confused a couple of people about this vane business. Here is a schematic sketch of how it works. The two drawings represent a cross-section of the left half of the cowling, seen from above, with the air inlet to the left. The top drawing shows how air entering the inlet separates from the rapidly spreading cowling sides and must then pass across the exhaust pipes (the three dark circles) to get to the oil cooler air inlet (the oval). The result is that the exhaust pipes heat the air before it gets to the duct inlet, and so the temperature of the air entering the oil cooler is 120 degrees F when the OAT is 75. The lower drawing shows how the vane directs a lot of 75-degree air along the inside of the cowling, where it is sucked into the oil cooler duct at a mere 95 degrees. I could make a closed duct in which the air would gain no heat at all, but I am operating on the assumption, or suspicion, that directing cool air along the cowling sides is beneficial in other, as yet undefined, ways.
[August 20, 2014]
Readers smarter than I may have wondered how I came up with the "33% increase in heat transfer rate" in the previous entry. Actually, it should have been 40%. I don't know anything about heat, but my caculation is as follows. Without the guide vane in the cowling inlet, the inlet and outlet temperatures across the oil cooler were 120 and 180 degrees Fahrenheit respectively. With the vane, they were 95 and 175 (roughly). So the temperature rise was 60 degrees without the vane and 80 with. The inlet air temperatures are respectively 580 and 555 degrees Rankine (that is, above absolute zero), and the temperature rises represent respectively 10.3 and 14.4 percent of those values. 14.4 divided by 10.3 is 1.4, hence a 40% improvement. Does that make any physical sense? Outside air temperatures were roughly the same; I suppose that the efficiency of the cooler improves as the OAT drops and the temperature difference between the cooling air and the hot oil increases.
Since the boundary layer guide vane on the left side seemed to have a generally beneficial effect, I am thinking I may install one on the right side as well -- perhaps helping bring down the temperature of the #1 cylinder, which is usually the hottest -- and add some ramps to smooth the entry of the rest of the cooling air.
[August 18, 2014]
The boundary layer control vane in the cowling air inlet was, in a sense, a huge success. Initially at 7,500 feet, at 140 kias and 8.1 gph, with an outside air temperature of 70 F, the temperature of air entering the oil cooler duct was 94 degrees, with an 80 F temperature rise in the air crossing the cooler; the numbers had been 120 and 60 before, with an OAT of 75. I then descended to 4,500 feet, where the OAT was 81, and slowed to 117 kias with a fuel flow of 4.8 gph. Now the oil cooler duct inlet temperature was 102 and the rise 61. In spite of the 33% increase in heat transfer rate, however, the oil temperature was still 108 C at 7,500 feet and 97 at 4,500. Its remarkable stability suggests a new possibility: that it has been being regulated by the Vernatherm all along, the oil temperature has always been the intended 78 C, and the high indication is due to a fault in the wiring between the instrument and the sensor, which includes two connectors. This hypothesis would require an element of temperature dependence, however, since the oil temperature reads correctly when the engine is cold. I'm not sure it's really plausible.
One incidental and unexpected side effect of the flow diverter is that the CHTs of the three cylinders on the left side of the engine are now just about identical.
[August 14, 2014]
I will not get to test it until Monday, but I have installed a temporary vane in the engine air inlet. It's quite crude, but if the idea has any merit -- which is by no means certain -- even a crude vane will reveal it. It consists simply of a copy of the inside surface of the inlet, back to about 10 inches into the cowling, that is raised about an inch above the inner surface. In principle it would direct a sheet of air along the inner surface -- air likes to follow surfaces, provided that it does not have to flow "uphill" against rising pressure to do so -- and that air would be sucked into the oil cooler duct without having passed over an exhaust pipe or the turbocharger. Most of the pressure recovery -- that is, conversion of velocity into pressure -- of an inlet like this happens in front of the inlet, however, and it's possible that there simply won't be enough velocity in the directed sheet of air to make any difference. We'll see next week. Here's what it looks like:
[August 7, 2014]
I have had a 1968 Chevy Malibu for 37 years. It has 450,000 miles (or somewhat more, actually, because the odometer stopped moving as it arrived at the last "50,000"). I am giving it to my son Nick, who loves it more than I do. It is somewhat threadbare, as everything I own tends to become, and he is having it fixed up at the shop of a friend of mine. This person lives in Jacumba, a tiny California desert town at the Mexican border. Fortuitously, Jacumba has a 2,400-foot gravel airstrip that is used for glider flying on weekends. There is a mountain at one end of the runway and the Mexican border is so close -- just a couple of hundred yards -- that you can fly on only one side of the strip; but it has a good surface. Yesterday Nick made the 3-hour drive to Jacumba in the Chevy, which we figure will remain there for a couple of years. I flew down to retrieve him. It was the first time I'd flown since getting back from Cape Cod.
At this point the reversal of the intake manifold has become sufficiently remote that my impressions are perhaps more objective than they were in the excitement of initial testing. My sense now is that nothing was gained in either cooling effectiveness or speed (yesterday it was 162 ktas at 7.7 gph -- about normal) whereas the change might have adversely affected the mixture distribution. It seems to me now that peak EGT is less distinct than it used to be and that the onset of roughness with leaning takes place earlier than it did before. I used to be able to lean to 150 LOP without any roughness; now roughness begins to appear around 50 LOP. I need to repeat the manometer and EGT tests that I did a month ago, and try to get better-quality data. Perhaps that would reveal whether I need to rearrange the GAMI injectors or get different ones.
It does seem that moving the throttle body to the "cold" side of the baffles may have improved the quality of the long-term idle at high temperatures, but extreme conditions occur so infrequently that I won't know for sure for a while. At any rate, that improvement hardly warrants the effort and expense that went into the change.
The oil temperature is still unacceptably and inexplicably high; it rose to 115 C during the climbout from Jacumba -- quite hot outside, and a steep climb to clear mountains -- and dropped to 95 in cruise at a low power setting. I will experiment with vanes to direct fresher air to the oil cooler duct inlet before resorting to the laborious and unwelcome extremity of adding yet another separate air intake to the cowling.
The gear retraction has become sluggish, and I am inclined to suspect the piston O-ring in the main actuator; but I need to get the plane up on jacks and be sure that the various bearings and links are all moving freely. Ars longa, vita brevis.
[July 31, 2014]
I got back from Cape Cod Tuesday at midnight. Yesterday I drained the oil, and finally discovered, after having this airplane for nearly 12 years and changing the oil I don't know how many times, how to do it without spilling a drop. The location of the sump drain just above the top of the nosewheel leg makes it difficult, and I've tried all sorts of awkward arrangements with funnels and tubes, both rigid and flexible. For some reason it never occurred to me to bend up a piece of sheet metal into a sluice to carry the oil backward past the strut and let it pour directly into a bucket. I should have asked my 21-month-old granddaughter Sasha for advice; she shows considerable mechanical aptitude already. I also serviced the flaps by adding a small amount of hydraulic fluid to the right-side circuits. In theory it should never be necessary to do this, but I haven't done it for several years, and that's a fair approximation of never.
[July 11, 2014]
I am leaving tonight on another trip for a couple of weeks. When I get back I'll see about putting some vanes into the cooling air inlet to keep some of the flow attached to the sides of the cowling. I also need to change the oil and re-align the flaps; today I noticed that at full flap the right flap was not extended as far as the left. There are four "bubble traps" in the system for this purpose. I have not opened any of them in a couple of years at least, so the system has been working fairly well.
[July 2, 2014]
I finally collected some pressure measurements inside the cowling. They were somewhat puzzling. For one thing, the quality of the data was not very good, and I'm not sure why; the data that I took with Hans Kandlbauer in 2009 were much smoother. It's pointless, perhaps, to compare data collected yesterday with those from more than four years ago taken by a person in the right seat with different parallax, etc. The old data suggested, however, that the pressure difference between the lower (high pressure) and upper plenums varies more or less linearly between zero and 1.5 inches of cowl flap opening (measured at the trailing edge of the cowl flaps) and also more or less linearly with speed between 80 and 140 kias, and I suppose I can use that observation to smooth out some of the scatter in the more recent measurements. At any rate, the upper plenum pressure seemed generally to have dropped by between 0.5 and 1.5 inches of water. This was what I was aiming for by removing the obstruction of the air outlets by the transverse portions of the intake manifold. So far so good. The lower plenum pressures have also dropped; this was to be expected, since, other things being equal, they are a function of the outlet resistance and therefore of the upper deck pressure. More surprisingly, the delta p -- the pressure drop across the engine, from the high pressure (bottom) plenum to the low pressure (top) plenum -- has also diminished. This is unexpected and I think must be due either to new leakage or to bad measurements.
I have developed a new theory about the high oil temperature. It is due to global warming. No, seriously; this has been a very warm winter, and earlier measurements were taken at considerably lower OATs. I have continued to monitor the inlet and outlet temperatures in the oil cooler duct, and observe the same 60 deg. F rise; but what is striking is how hot the air entering the duct is. It is actually hotter than air at the back of the engine, near the throttle. I thought that by placing the bellmouth of the duct below the exhaust pipes I was preventing it from ingesting pre-heated air, but looking into the cowling air intake yesterday I realized that if, as is quite possible, the flow is separating from the inner surface of the cowling behind the inlet, which expands much more rapidly than an ideal diffuser, the only way for air to get to the oil cooler duct inlet is to travel over the exhaust pipes first. I am toying with the idea of putting a vane in there to direct air along the lower inside of the cowling. I have thought occasionally about putting my little TV camera and some tufts inside the cowling to see what the flow in there is doing; now may be the time.
[June 25, 2014]
A recheck of the temperatures across the oil cooler confirmed a rise of 60 deg. F. What is surprising is that the inlet temperature is 120, the outlet 180, with an ambient temperature of 75. I have a chart of cooling air temperature rise for an IO-550 engine, and it seems that the air temperature rise is generally around one-third of the difference between the cylinder head temperature and the ambient air temperature. If that's any guide, the 60-deg rise seems about right. (The oil temperature, currently 210-220 deg F, is measured at the oil cooler outlet, so the oil in the cooler starts off hotter than that.) But it's the 120-degree inlet temperature that concerns me now. Why is it so hot? On May 12, 2012, when I measured temperatures at the future throttle body location (behind the engine, high up, on the cold side), I saw around 95 in cruise; this was at 14,000 feet, however, and the OAT was 43 F, so maybe the "cold" side of the cowling really is a steady 50 F above ambient.
[June 19, 2014]
A flight to measure the temperature rise across the oil cooler produced results that seemed surprising until I calibrated the Radio Shack probe in the new (brand name "RediChek") device and found that the old sender, while physically compatible with the new device, required a big correction. The correction curve turns out to be T = .77(t+23) in Fahrenheit. This obviates my observations of June 17 about the absence of a pressure gradient across the engine during cooldown; the corrected temperatures show the lower plenum to be consistently 40 deg. F cooler than the upper, even with the tail to the wind. When I got the plane out of the wind the difference was more like 70 degrees. That's more like it. The temperature rise across the oil cooler was about 60 deg F, which seems like less than it should be.
I collected another batch of EGT data, trying to be more careful this time, but there's more scatter in the new data than in the old. One difficulty is that the fuel flow indication increments by tenths of a gallon per hour, and so when it says 9.2 you don't know where you are between 9.15 and 9.25. The difference can have a significant effect on EGT.
[June 17, 2014]
Both of my Radio Shack remote barbecue temperature probes having ceased to work, I got a new one, this time with two indications ("food" and "smoker"). Fortuitously, it is compatible with the thermocouples from the old ones, so I can put four thermocouples in various locations and plug them into the transmitter in different combinations. Yesterday I made a short test flight with the oil filter (which is in series with the cooler) bypassed, just to make certain that the high oil temperature was not due to the filter being somehow blocked (though this would be extremely unlikely, since it has its own internal bypass valve). No joy there. I also tracked the temperatures above the engine and along the right side of the oil sump, where the fuel lines run from the fuel pump to the throttle/fuel controller. I wanted to be sure that radiant heating from the exhaust pipes was not affecting the fuel lines. That probe reported a balmy 80-90 F in climb and slow cruise (the OAT was 80 on the ground). What was interesting to learn, however, was that after shutdown the temperature throughout the cowling, below and above the engine, rose to a more or less uniform 200 F. I was parked facing downwind and so did not get whatever advantage might have been provided by a breeze on the air intake, but it was interesting to see that pumping due to hot air flowing out of the outlets -- cowl flaps wide open, of course -- did not create much of a temperature gradient across the engine. When I put the airplane into the hangar, maybe 10 minutes after shutting down, the expected gradient appeared. The last reading I got before turning off the temperature gadget was 180 below the engine and 220 above. Remarkably, the cowling shows no sign of deformation after 11 years of this abuse, even though Safe-T-Poxy is supposed soften at 160. Clearly it responds well to progressive heat treatment.
One place I would like to measure temperatures is across the oil cooler. In principle one would expect to see no temperature rise until the oil temperature hits about 170 F. At that point the Vernatherm valve should start to close, directing oil through the cooler and filter, and there should be an increasing temperature difference across the cooler.
My hangar neighbor Claude Morgan suggested I cut open the oil filter can to check for metal in the filter, on the theory that high oil temperature could indicate a hot bearing. I did, and didn't find any metal. It's time for an oil change; I'll get a spectroscopic oil analysis just to be certain.
[June 12, 2014]
After returning late last night from Boston, I did a flight today to try to pin down the EGTs, which in principle ought to reveal the effects reversing the intake manifold had on mixture distribution. I'll have to repeat this test more systematically, because this time I failed to record fuel flow, which ought to be the abscissa parameter, and also because the #3 (right middle) cylinder's EGT probe was not working. I also want to install a couple of air temperature probes to get the temperatures in the two plenums, and maybe set up my manometer to re-check delta-p (the pressure drop across the engine) as well.
I flew at 10.500 feet; the density altitude was 13,300. Power was around 27/2300, which represents an open throttle and open wastegate at that altitude (the wastegate duct diameter is small, and so there is some boost even with the wastegate open). My analog EGT gauge (Alcor, circa 1970) does not allow very precise measurement -- maybe 5-deg F increments -- and I was in a bit of a hurry, but here is what I got:
The top (blue) line is TIT -- turbine (or turbocharger) inlet temperature. It is hotter than the others because that probe is in a constant stream of exhaust gas, whereas the others just get a shot when the exhaust valve opens and then cool the rest of the time. (The initial steep rise is due to the fact that I started out using half-turns of the mixture control, then changed to quarter-turns.) The random fluctuations are presumably due to measurement errors; it might be useful to smooth the data mathematically to identify more clearly the peaks, but collecting the data more deliberately and carefully might help too. At least they all cluster within a half-turn of the mixture knob. Nevertheless, I got the impression that whereas I used to be able to lean to 75 or more LOP, I now start feeling roughness at 35 LOP or so. One thing I want to look at when I get the #3 probe working again is whether the cylinders on one side are collectively peaking before those on the other. I had some concern that this might occur because of the 90-degree bend in the inlet duct a few inches before the throttle body.
One striking thing that I observed was a steady 149 kias (183 ktas) at 8.8 gph. This is about 4 knots better than I would have expected, and implies that a not negligible drag reduction took place. Now, cooling drag is always the great unknown, and there are all sorts of wild reports about what a huge fraction of total drag it can be. It is very hard to believe, however, that cleaning some obstacles out of the flow path inside the cowling (where velocities are comparatively low) could reduce F (the "equivalent flat plate area") from 2.35 to 2.15 square feet. It would be nice to believe it, but I'm sure this gift will be withdrawn -- I'm sorry sir, that $10,000 was accidentally credited to your account -- the next time I fly.
[May 21, 2014]
An hour-long flight yesterday. I sensed a few subtle changes, but nothing dramatic. For some reason the EGTs on the individual cylinders seemed closer to one another than they used to, but at the same time I felt that peak EGT on the TIT, which I use for leaning, was flatter or less distinct than it used to be. These are contradictory impressions, but I was flying in turbulent air under a 4,000-foot overcast at low power (20/2100, 5.4 gph) and so those indications are atypical in any case. We're going east again for a couple of weeks on Sunday, but when we come back I'll do a systematic sweep at cruise power and altitude to map the EGTs against fuel flow and compare them with the ones I recorded ten years ago when I first installed the GAMI injectors. I will also collect data on pressure drop across the engine to see whether cleaning up the upper plenum had any effect.
The engine felt happy. CHTs were generally very low because of the low power. The oil temperature is still too high, but that's not surprising since I didn't modify those components other than to move the oil filter to a different location and replace the hoses to it with longer ones. Start was immediate and normal, so putting the fuel controller at the opposite end of the engine from the fuel pump does not appear to have created any problem in that department. After landing I inspected the engine and noted a slight fuel stain at one connection in the new stainless lines; the B-nut was not fully tightened. Otherwise, everything looked good.
It's possible that this whole manifold-reversal project will turn out to have been a huge waste of time, money and effort. It was fun, though, and I like the way the engine looks.
[May 20, 2014]
I made the turbo to throttle duct on Saturday by splicing four segments of aluminum pipe with laminations of Hysol epoxy, which can withstand the 200+ deg. F temperatures of the turbo discharge without softening. Today I used aluminum tape to temporarily close the gaps where the intake manifold passes through the baffles, and then did a 15-minute ground run with the cowling on. At one point I ran at high power until the hottest cylinder hit 200 deg. C (392 F). then throttled back to an idle. The CHT slowly dropped by 10 degrees or so. This is significant, because I believe that with the old manifold arrangement it would have continued to rise. I also did not sense any of the rough running that used to occur during long periods of idling; so it may be that clearing the cooling air outlet path of the obstructions created by the old manifold, and/or moving the fuel controller to the cool side of the baffles, has actually had an effect. It may also be that I am kidding myself; that tends to happen just after I have made some beneficial-seeming change. Unfortunately my remote temperature probe -- a Radio Shack gadget intended for grilling meat on a back yard barbeque while watching television in the den -- did not work for some reason, and so I did not get a reading of the temperatures in the environment of the new fuel lines. Tomorrow I will fly, weather permitting.
[May 12, 2014]
I ran a quart of so of fuel through the engine to check for leaks. There were none in the new plumbing, but there was a drip at a pipe thread fitting coming out of the fuel flow meter. That is a fitting that I have not touched during the current work, so I have no idea how long, or how much, it's been leaking. I suppose I can, however, congratulate myself on 1) not having burned up in flight and 2) having achieved such performance as I have achieved on a slightly lower fuel flow than I thought.
At any rate, I fixed the leak, secured a few loose ends, and put a temporary duct between the turbocharger and the throttle. I put all my tools away -- ritually signifying the end of a phase and the start of a new one -- and set aside the vast collection of nuts, bolts, washers, brackets, clamps, and so on that somehow had been made homeless over the last couple of months. I rolled the airplane out onto the taxiway, planted a couple of fire extinguishers in front of it, gave it a final looking-over, and climbed in.
After a good deal of geriatric coughing and sputtering it settled down and ran normally. I idled for a few minutes at 1,300 rpm, did a mag check at 1,700, and then shut it down. I looked it over carefully and found no oil or fuel stains. I need to replace various clamps and ties that I removed -- a lot of the wires and hoses behind the engine have been rearranged -- and do some more ground running, including a full-power run-up, before it will be ready to fly.
[May 9, 2014]
The stainless steel fuel lines are all in place. It turned out to be possible, as I had hoped, to run them close to the rear baffles so that they do not interfere with access to any part of the accessory case. They're quite difficult to bend, and once bent impossible to unbend, so I made each piece first out of aluminum tubing and then copied the dimensions and angles in stainless. This seems to have worked pretty well. To give myself a clear view of what I was doing, I took off the starter; after finishing the fuel lines I realized that they ran right through a bracket connecting the rear baffle and the starter adapter. I'll have to make a new bracket that somehow or other goes around them. I finished right at the end of the day, and had time only to pump some fuel through the system to check for leaks. There seems to be a big leak right at the fuel pump; everything else is dry. I'll figure it out Monday and then run the engine.
[May 4, 2014]
The plumbing for supplying upper-deck pressure to the injectors, fuel pump and magnetos is almost complete, and I managed to make all of it, so far, out of leftover tubing and fittings. I suppose at least part of the satisfaction I derive from finding re-usable materials in my junk-littered hangar is due to its confirming a belief, which underlies my reluctance to throw anything away, that some day even the most improbable scrap of stuff may come in handy. For the last piece, which is two feet long, however, I'm going to have to buy some 3/8" tubing, and it actually would not have killed me to use new tubing for the whole thing. I carom back and forth between extravagance and economy. A serial arachno-eksaeolist, I do blow out the spiders before re-using old tubing.
I found that I have a second tube bender for 1/4" tubing with a larger bend radius than that of the one I normally use; it works better for the stainless tubing, and I don't think I will need to fill the tubing with sand before bending it. That will leave, apart from some details like a missing lock washer here and cotter key there (of which I keep a careful list, since I would otherwise be certain to forget them), just the two fuel lines between the fuel pump and the throttle, and the big duct between the turbo and the intake manifold. The big duct continues to be a puzzlement; I can't find out who bends 2.25-inch .035 wall aluminum tubing. Even Woolf in Michigan, which specializes in this kind of stuff, apparently draws the line at .065, though if I spent hundreds of dollars on a special setup I suppose they might go thinner. Woolf specializes in extremely tight bends -- bend radius equal to tube diameter -- but for reasons of avoiding flow separation I would like to use the largest radii I can fit in the space. Apparently the best I will be able to do from them is a 180-degree 4-inch radius bend with .065 wall. Putting that together with various scraps from my heap, I will be able to assemble the required duct. It may be temporary anyway, because if I have not completely exhausted my appetite for modifications by the time this project is done the next one would be an intercooler that would replace most of this duct.
I like the look of the new plumbing; it's neater and more rational than the old. I hope it works.
[April 14, 2014]
I made a teensy bit of progress today on plumbing up the fuel pump before closing the hangar for a couple of weeks while Nancy and I go east to visit our progeny.
One reason that adding systems to a homebuilt notoriously takes as long as building the airframe is that there are so many decisions to be made about routing wires, hoses, air ducts and fuel lines. The present quandaries revolve around the two 1/4" stainless steel fuel lines joining the fuel pump and the throttle, which are at opposite ends of the engine. They will run alongside the oil sump (the underside of the engine being the cold air side) and snake their way up behind the rear baffles in such a way as not to compromise the accessibility of the magnetos, alternator, and so on, which is currently very good because I left a tremendous amount of space between the engine and the firewall when I first laid out the airplane. There are already a couple of steel hangers dangling from the sump bolts; these are the natural places to attach aluminum or phenolic blocks to secure the fuel lines. But it seems that while I'm at it I ought to include the 3/8" fuel supply and the 1/4" vapor return lines in the remodeling. Those lines are currently Aeroquip hoses, because they need to be flexible, but there is no reason they need to go all the way to the front of the engine; they could just go from the firewall to the back end of the engine, and continue forward as hard stainless lines. Or the hard lines could run from the firewall to the front of the enigne, with short flexible links to the fuel pump. That would make a neater and less bulky installation, but Claude Morgan, a hangar neigbor who in addition to being a retired UAL captain is an A&P, mentioned to me that it is preferred to run fuel lines above electrical wires, I suppose so that if a hot wire parts it does not fall down and short against a fuel line. That complicates matters further; there is no lack of wiring around the bottom of the engine. I suppose you could put firesleeve around the stainless lines, but that would somewhat defeat the purpose of using them in the first place. Maybe heatshrink would be sufficient. Plenty to think about while hiding the Easter eggs.
[April 12, 2014]
Now that the throttle cable problem has been dealt with, a new problem has come to take its place. The 2.25-inch SCEET hose that I had expected to use to connect the turbo to the intake manifold is unable to bend gracefully to the radii required; it wrinkles up inside like an accordion. I need to find some already-bent thin-wall tubing of 6 or 8-inch radius, or else find a tube bender who can make the stuff for me. The company that did the intake manifold bends seemed barely able to cope with material of .065 wall thickness; this ought to be more like .032 at the most.
[April 11, 2014]
The excess length of the throttle cable produced this goofy-looking arrangement:
The C-clamp and cleco will be replaced by bolts securing a bracket that supports the fore (left, in the picture) end of the metal sleeve within which the push-pull cable slides. This sleeve is normally intended to pivot over a range of 20 degrees or so to allow attachment to radial arms like the lever on the fuel control; in this case, the link takes care of the misalignment issue and the sleeve needs to be held still to prevent random variations in throttle position, to say nothing of the possibility of locking overcenter at full throttle. (In this picture the throttle is at idle.)
The light tan-colored duct bolted to the back end of the throttle body is where the air duct from the turbocharger attaches. The threaded boss on its near side is for an air line that goes to the injectors, the magnetos and the fuel pump to provide them with turbo discharge pressure. The little dark nubbin visible through the hole is the induction air temperature probe, which enters through a similiar boss on the opposite side. It is aligned with the throttle butterfly, and so the aerodynamic disturbance it creates will not, I think, matter. The throttle body sits on an aluminum rail and is stabilized laterally and vertically by a thin steel plate anchored to the two upper vacuum-pump studs. The forward end of the rail is bolted to the engine baffles at a point close to where the baffles are secured by an accessory-case stud. The point of all this is to prevent vibration of the throttle body, and the whole setup is, as John Thorp said of my first airplane, "built like a brick shithouse" -- that is, stouter by far than the intended use requires.
[April 9, 2014]
The throttle cable turned out to be a problem. It is 3 inches too long, because Morse cables, or at least McMaster-Carr's Morse cables, come only in 1-foot increments, and it turns out I need a 21-inch one. Furthermore, the dimension from the anchoring groove to the threaded end was different from that on the previous cable, and so I had to make new hardware for connecting to the quadrant and the throttle. For the time being I am going to use a sort of trailing link to connect the engine end of the Morse cable to the throttle control arm, but sooner or later I will no doubt find out where to get Morse cables made to a custom length.
The throttle support is now in place and feels pretty good.
[April 2, 2014]
The reassembly of the engine compartment is progressing, so far without any major problems. The rear baffles are back in place, split now so that they can be removed in spite of the intake manifold passing through them. I will need to come up with a way to seal the clearance between the baffles and the manifold; split fiberglass flanges, laid up in place, are my current favorite candidate. I re-installed the Sky-Tec "lightweight" starter, which is indeed lighter than the original Delco, but not by much, and am keeping my fingers crossed, since it has not so far covered itself with glory. I am working now on the support for the throttle body, which does not weigh much but needs to be kept from jiggling around. After that I will install the new throttle cable and arrange the routing of the turbo-to-throttle air duct and the new oil lines.
I anticipate that the final step will also be most difficult: routing the stainless steel fuel lines between the fuel pump, the throttle and the fuel distributor. In 2004 I moved the distributor, which used to sit on top of the engine, to the front, below the propeller, where it is in the intake airstream and is not heated by the engine. It, the throttle and the fuel pump formed a tight group near the front of the engine, joined by a few short lines and hoses. Now, with the throttle at the rear, it's necessary to duct fuel twice the length of the engine, from the fuel pump back to the throttle and then from the throttle forward again to the distributor. This is straightforward for three-quarters of the way, but gets tricky when the two fuel lines pass behind the accessory case, since you don't want them to interfere with access to the magnetos, alternator and so on. I intend to mock them up in aluminum, which is much easier to form than stainless, run the engine to make sure everything works properly, and then copy the aluminum lines in stainless.
We're going to Connecticut on the 15th to visit our son and his family. I was hoping to get this project finished before we go, but with taxes needing to be done -- I do my own -- as well as various other preparations, I'm starting to have my doubts.
[March 26, 2014]
I finally got the intake manifold tubes back from the welder today and installed them. The top of the engine is now distinctly less cluttered than it was. Here is the previous setup:
And here is the new one:
The only things that will be added are the tube running from the breather at the front of the engine to the oil separator on the rear baffle and a line running from the throttle body to the two injector shroud rails. It should be easier now for cooling air to find its way to the outlets at the front of the cowling.
The next step is to revise the rear baffles so that they split around the intake tubes, and then to install the fuel lines and the air lines that supply upper-deck pressure to the injectors and the fuel pump. Finally, the oil filter, which has moved to the right side of the firewall, will need new, longer hoses, and I'll replace the turbo oil scavenge line just because it's old.
[March 19, 2014]
The chalice of jury service passed before me, but being present at jury selection for a multiple murder trial was its own reward. Despite all the praise one hears of the jury system, I got the feeling that in difficult cases a just verdict would be a matter of chance. The occasional ruthlessness and mendacity of prosecutors are notorious, but to judge from what I saw on Monday their obtuseness should more than compensate. On the other hand, the common thread linking the prosecution's many peremptory challenges seemed to be any evidence that a prospective juror was capable of nuanced thought. The judge, Robert Perry, seemed amiable, balanced and intelligent. I was grateful for his light-heartedness, but the citizen beside me at one point leaned over to whisper that she thought it inappropriate to the gruesome crimes being tried.
I got the S-ducts back from the welder on Tuesday and today spend four hours making a fixture for welding them to the two rearmost elements in the existing manifold. It's still not finished. I always marvel at how many unforeseen complications conspire to stretch out the time things take, and yet I never factor them into my estimates. I guess that's what makes them unforeseen.
I told the welder that the welds in the duct segment did not need a lot of penetration, but he must have forgotten, because there's quite a lot of roughness on the insides of the joints. I ordered from McMaster-Carr something called a "ball hone" with which I hope to be able to take away at least some of the crud in the curved portions. The straight segments are accessible with an ordinary drum sander. The roughness may not matter much; the average speed of the airflow in the manifold is only about 70 mph at cruise (100+ at takeoff), and the throttle messes up the flow in advance anyway.
Once I have the new ducts bolted to the engine, the next difficult step will be to make up a fitting to attach the throttle body to the accessory case in order to support its weight. The rest is mainly a matter of reassembling the baffles and making new fuel and air pressure lines between the throttle and the fuel pump. That seems now as if it ought to be comparatively straightforward, but no doubt it will bring along its own retinue of unforeseen complications.
[March 15, 2014]
The tubes are at the welder's, and I've taken everything off the top of the engine. Unfortunately I have jury duty next week but with luck I will be sent home as unsuitable for making any serious decisions.
[February 28, 2014]
The tube bender delivered me four 170-degree bends of 5-inch radius. Two were good, with no rippling on the inner surface; two had some rippling. But since I need only two, I will use the inferior ones for practice. Here one has been sawn into the three segments that will be welded together to form the somewhat sinuous duct from the Y-shaped throttle body to the log manifold over each bank of cylinders. Part of the spare throttle body I got on eBay is visible, upside-down, on the right side of the picture.
The first difficulty that arises is that the cross-section of the tubes ceases to be round in the bends. The outer surface is stretched and the inner one compressed, with the result that the inner one not only grows thicker but also pushes the middle of the tube outward. This is typical:
The mismatches are not too bad when segments are joined in an S curve in a single plane, that is, with a rotation of 180 degrees; but when you rotate one 90 degrees with respect to the other, as I will be doing, you are matching the widest dimension with the narrowest. I am not sure how to correct this problem, but I suspect that like many other problems it might be solved with a few judicious blows of a hammer. I will see on Monday. The aim is to get as smooth a duct wall surface as possible, and so it would be nice if the inner contours matched.
Surprisingly, the dimension between the centers of the intake ports on opposite banks is uncertain. My ancient and disintegrating Continental installation blueprint says the manifold runners are 21 inches apart and the intake ports 24.24 inches apart. That would make the offset from a runner to a port 1.62 inches. I have carefully measured the two manifold segments that I have (and which I will saw up to incorporate into the new manifold) and the offset is 1.70 in., which would put the intake ports 24.40 inches apart. Eighty thousandths doesn't sound like much, but when you're trying to bolt metal parts together it's prohibitive, and resorting to the hammer solution is not advisable. Fortunately, the ducts converge on the throttle at an angle of about 49 degrees, so if I tool up for the large dimension and it turns out to be incorrect when the parts are moved from the jig to the engine, I can trim off a small amount and move the throttle body forward slightly.
[February 25, 2014]
A small setback: The aluminum tubing ducts that I had designed to connect the intake manifold runners to the throttle body turned out not to be within the capabilities of the highly experienced tube bender who is doing them. There was not enough "tangent" between curved segments in different planes. I had a feeling that might be the case, but I hoped he would have some magical way of grabbing the tubes in spite of their being bent every which way. Apparently not. Instead he will make some U-shaped bends of 5-inch radius and I will cut them apart and have them welded back together in the required twisted-S shape. The wall thickness is .065, and I hope that the weld penetration can be sufficiently shallow to prevent much roughness forming on the inside of the tubes. I got the new throttle cable, for which I will need to make a new hole in the firewall. I have all the necessary parts for the intake manifold and am steeling myself to start sawing them up.
Incredibly, McMaster-Carr, from whom I have been buying a lot of stuff lately, charges about $60 for a 6-foot length of 2-inch OD .065 wall 6061-T6 tubing; I got an 8-foot length from Industrial Metal Supply in Sun Valley for $26, which included tax and an $8 cutting fee, the standard length of one "stick" being 20 feet. Industrial used to be a couple of miles east of where it is now, and it used to stock a lot of surplus sheet, plate and extrusions in aircraft alloys, 2014, 2024, 7075 and so on. That was when Lockheed was still operating nearby. The first Melmoth was build entirely of aluminum bought at $2 or so a pound from Industrial. Those days are gone, or almost; there is still a small, very nice metal dealer that stocks those alloys a bit east of where Industrial used to be; but the quantities and variety are not what they were in what I -- not the owners -- consider to have been Industrial's heyday.
[February 10, 2014]
I cautiously sent the WLR (world's longest reamer) a few inches into the piano hinge this morning, rotating and pushing it by hand. I observed that what collected between the flutes was mostly black muck, presumably composed of congealed grease, aluminum oxide, and airborne particulate matter of various species. I also observed that the lithium grease with which I had smeared the hinge pins was quite viscous. I accordingly cleaned off the pins and lubricated them with, of all things, 3-in-1 oil. This had the effect of reducing the "bump" in the elevator travel to a fraction of what it was before I began this process a month ago. I think that in order to ream the piano hinge -- I understand the objections to this process that several people have raised -- it would be best first to remove the elevator and to clean out the two sides of the hinge separately. Now that the friction is so diminished, however, I may not be very strongly motivated to do that.
I have been trying to establish the best position for the throttle body above and behind the engine. I had decided to use double-wall SCEET tubing between it and the two runners of intake manifold, but realized today that SCEET is not sufficiently flexible to make the necessary bends without wrinkling up accordion-fashion on the inside of the bend. So it will have to be aluminum tubing, which at least will have the advantage of stabilizing the assembly laterally.
[February 7, 2014]
Today the world's longest reamer was assembled by my neighbor, who machined a stepped V-block out of a piece of steel bar stock and then brazed the .098 reamer to the 6 foot long .095 shaft. I will give it a very tentative and cautious try next week.
I received this picture of the Rutan Catbird attached to an email today:
I was struck by the many resemblances to Melmoth 2: T tail, high aspect ratio low wing with similar planforms and upturned tips, bubble-style canopy, cooling air vents on top of the cowling and near the front. Like Melmoth 2, it is a 200-hp airplane using Roncz laminar sections for the wing. My first thought was that I must have unconsciously copied all these features. I then checked the dates and found that the Catbird was designed, as a potential Bonanza replacement for Beech, about five years after Melmoth 2 was. Although Rutan and I had many contacts, I don't recall much discussion of my design, then in the early stages of construction, and in any case it would be fanciful to imagine that Rutan would be influenced by me. It is more likely that we had discussed some of these features in general terms, or they were just in the atmosphere at the time. For example, Rutan had used top surface air outlets on other designs but had placed them farther aft. I thought the idea of moving them forward into a region of lower pressure was mine, but I guess it must have been a pretty obvious variation on the theme. He had certainly made clear to me the value of wingspan, something Melmoth 1 sorely lacked. Some significant differences between the two airplanes are the canard surface on Catbird, the fact that it is a 5- rather than 4-seater, and the fact that it was intended to be pressurized, although I don't think the pressurization was ever implemented. I'm not sure whether Catbird has flaps; at a certain point Rutan started arguing against flaps, having observed that he never landed on anything but paved runways at least 3,000 feet long. Personally, I have found the Fowler flaps on Melmoth 2 to be one of the more satisfying aspects of the design, but I'm not sure that would be a sufficient justification for putting them on a commercial product. On the other hand, I wonder whether Catbird could possibly meet the FAA's 61-knot stall speed requirement for single-engine airplanes; Melmoth 2 does so easily.
[January 31, 2014]
I did both cold and warm compression checks today and also inspected the bottom plugs. The plugs in the four front cylinders were dry; those in the rear two were slightly damp. All were clean and medium to dark gray in color. I don't know why the two rear cylinders should be different from the others, but at any rate there was nothing alarming about the plugs. The cold compressions were 74 - 79 - 78 - 75 - 80 - 74 and the warm 77 - 76 - 76 - 76 - 78 - 75. (The engine has 1,324 hours, and more than 35 years, since new.) Driving home from the airport I was wondering if you could dream up a figure of merit for compression tests -- something like the average divided by, say the square root of the largest difference. Never mind, I decided. At any rate, the compressions seemed acceptable and did not suggest that there would be a lot of blowby, so the reason for the rise in oil temperature remains a mystery.
[January 28, 2014]
I had the Vernatherm -- the thermostat that controls the oil temperature by forcing oil to flow through the oil cooler once it has heated up -- tested by Pacific Continental Engines. It seems to be okay. One of their guys came over to inspect the seat against which the Vernatherm closes; it is okay too. He suggested that excessive blowby on a cylinder could cause elevated oil temperature, and that engines that have been stored a long time and suffered some corrosion in their cylinders could be prone to this. He didn't know it, but my engine had been stored for 20 years while I was building the airplane. He suggested doing a warm compression check and borescoping the cylinders to look for "glazed" areas where the hone pattern has been completely polished away. I have done cold compression checks from time to time and found all of the cylinders to be in the middle to high 70s; I'm not sure how a warm check would compare with a cold one, but I suppose it would be worse because the oil would be thinner. We'll see. He also suggested that when I reverse the manifold I ought to add a balancing tube between the closed ends of the right and left intake runners. That has been suggested before, and I think Continental says it doesn't do anything.
[January 23, 2014]
I replaced the oil cooler with the refurbished one -- quite an operation, taking parts of three days, because of all the baffling surrounding it. Unfortunately, the change had no effect; the oil is still as hot as before.
I found a throttle body for my engine on eBay for $40; it will make it easier to make various parts for the reversed intake manifold without having to ground the plane for a long time.
I had been noticing for some time that my landings were getting worse. Melmoth 2 is a very easy airplane to land smoothly, and there is no reason every landing should not be a perfect greaser -- you should barely know when the tires touch. But I had been putting it down with a definite tap-tap, and I became aware that I was flaring with a series of small jerks -- these were not my passengers; they were wrist movements -- rather than a smooth motion. The reason for this turns out to have been not advancing age but hinge friction. Merely lubricating the hinge pin made a big difference; today I was able to flare with a smooth motion and grease the landing, in spite of a turbulent final approach and a quartering tailwind.
The plan of sending a reamer down the elevator hinge bore has been getting generally bad reviews from correspondents. Each person has a different view of why it will not work, however, so at least there is not one obvious objection. With all this naysaying, I can't resist giving it a try. I always remind myself of the advice of my skydiving jumpmaster at Harvard, John Leibacher, now an astronomer in Tucson, who, when I explained that I wanted to build my own plane and had been reading everything I could find on aeronautical engineering, said, "You can't build an airplane out of a cookbook!"
[January 20, 2014]
Dave Ganzer of AeroVironment, who probably knows a good deal more about this than I do, wrote to warn me that reaming the hinge bore would not work, because -- if I interpret his explanation correctly -- the problem is probably a large-scale bend in the hinge. I am assuming that it is local waviness. I used a straight, rigid fixture for bonding the hinges in place when I built the stabilizer and elevator -- this was in the 1980s -- but I failed to realize how large the clearance between the hinge bore and the hinge wire is, and so my very straight, very rigid fixture did not compel the hinges to be as straight as it was. I now realize, 30 years too late, that I should have used .098 drill rod, rather than .088 hinge wire, between the hinges and the jig. At any rate, I have ordered all the materials for the reaming operation, so I may as well give it a try.
[January 17, 2014]
My old friend and fellow airplane mess-arounder Peter Lert suggested, in an email rather alarmingly entitled "Redneck reamer", that I rough up the end of a hinge wire with a file or Dremel and send it down the hinge bore with an electric drill. I decided, however, to give the high tech solution a first try. My neighbor John Biggs, who is a skilled welder and machinist, thought he could weld a reamer to a piece of drill rod with the requisite alignment, so I am going to get an .098 reamer and a six-foot length of .095 drill rod and see whether that combination can clean up the hinge bore if sent through it very carefully, with frequent chip clearance.
[January 10, 2014]
Swapping the oil temp probes had no effect, as I expected, so I took my spare oil cooler to Pacific Oil Coolers in La Verne, about half an hour's drive from here, to be cleaned out and pressure tested. They found a cracked hold-down lug and wanted to sell me a new cooler, which would be $650 or so, on the reasoning that welding the lug and re-machining the gasket surface would cost $500. I asked them to clean out the cooler and return it to me with the cracked lug, which I'm sure I can get welded, and re-machine myself, for $20, if not for free. They readily agreed. For an experimental airplane, I don't need the official yellow "return to service" tag.
In the meantime I decided to do something about the increasing friction in the elevator hinges. The elevator is connected to the stabilizer by a continuous piano hinge that's about ten feet long, with a five-foot hinge wire inserted from either end. When I built these parts in the 1980s, it was difficult to perfectly align the piano hinges, which are bonded and riveted to the surfaces, over a distance of 10 feet. I came close enough that the pin could be inserted fairly easily, but there was a resistance "bump" in the middle of the elevator travel where the misalignment is worst. The pins had not been removed or lubricated for 11 years, and I suppose they had gotten dirty. It turned out to be very difficult to get the left-hand pin out; it finally moved after being doused with oceans of WD-40 and encouraged with a hammer. The right-hand pin slid out easily. I cleaned and greased the pins and re-installed them. It would have been better to remove the elevator entirely and clean out the hinges, but that's more of a process than I was willing to face that day. The friction is much reduced, but the resistance bump is still there. This got me thinking about whether there is some way to send a reamer down that long tunnel and shave away some material where the misalignments are. The hole in the extruded hinge is .098 in diameter, and the hinge pin is .088, so there is not a lot of beef there to work with.
[December 24, 2013]
Since some point in the not too distant past the oil temperature has suddenly been up around 95-100 C rather than the expected 78. My first thought was the Vernatherm, a thermal valve that shuts off a bypass duct in the lubrication system, forcing oil through the oil cooler. I'm not sure how a Vernatherm can go wrong, but apparently they sometimes do. I took it out and put it in a pan of boiling water; it got 5/32" longer, which sounds about right. Later I consulted a nearby A&P, who said 1) I should use oil for that sort of thing; 2) the point is not just to see if the Vernatherm grows, but to find out the temperature at which it starts expanding -- or reaches its maximum length, I forget which; and 3) I should try to remember the last thing I did to the engine before this problem presented itself. Unfortunately I do not keep a log of engine parameters on each flight -- I should -- and so I could not pinpoint when the oil temperature had gone up, but that did remind me that back in the middle of November I had fiddled with the oil and induction air temperature probes and had probably swapped probes in the process. So before I start tearing into the oil system I guess I should swap some probes first. I am not optimistic, however, because I had checked all three of the probes I have, and all indicated exactly 100 C in boiling water.
There was no exhaust staining on the baffle where the leak had been that I repaired a couple of weeks ago, so evidently the gasket is holding, at least for the time being.
[December 18, 2013]
On Sunday I went up to Paso Robles for a very interesting and enjoyable day during which Mike Melvill checked out in Javier Arango's Sopwith Tabloid, the only one flying in the world (and therefore, to borrow the terminology of the rights contracts I sign for my magazine articles, in the Universe). I got to run an 80-hp Le Rhone rotary in a Pup securely achored to the ground. The engine controls on the rotary are queer by modern standards. There are separate levers for air and fuel, so that you control mixture by their relative positions, and there is a button on the stick that interrupts the ignition entirely. In flight the engine uses basically three power settings: full power (around 1,100 rpm static), partial power (800-900 rpm static) and off. You can't leave it off for too long, because it will stop spinning; the plane is too slow for the prop to windmill. Next trip I'll try the Camel's engine, which has a different arrangement: full power all the time, annd several levels of ignition interrupt, shutting down various numbers of cylinders. Melvill, who has flown just about everything and I'm sure could comfortably fly anything he hasn't already, reported some initial awkwardness with the Tabloid's "blip switch". Until you get used to it -- I noticed this just fiddling with the Pup's, which is similar -- it's easy to get confused between "stop" and "go", especially because we're in the habit of associating a positive action like pressing a button with "go" rather than "stop".
I climbed to 14,500 on the flight up; 178 ktas on 8.5 gph. Disappointingly, replacing the exhaust gasket on the #1 cylinder did not make it run any cooler; it's still up around 390 when the others are at 370 or less. I have not yet had time to check whether there is any fresh staining on the adjacent baffle. Also puzzling, and probably more urgent, is the suddenly elevated oil temperature. It goes right up to redline (230 F) in the climb, and cools down to 200 or so in cruise. It should be at 170, and was until a few weeks ago. I don't know what's changed, but I need to figure it out. Another thing I need to deal with is friction in the elevator hinge. It's not a problem in flight, but on the ground I'm aware that the friction is higher than it should be. There's about 10 feet of piano hinge there -- the idea was to make an airtight seal -- that hasn't been cleaned or lubricated in more than 10 years. I'm not sure how to go about cleaning out all those little holes -- 240 of them -- but obviously it will be necessary to take the elevator off to get at them at all.
[December 12, 2013]
On removing a section of the engine baffling to make a small modification connected with the eventual (dare I say "impending"?) reversal of the intake manifold, I found a lot of exhaust staining behind the #1 cylinder. This may explain why that cylinder has been running warner than the others. In order to replace the exhaust gasket I had to drop the entire exhaust manifold on that side (the right), and in two instances rather than the nut coming off the stud the stud backed out of the cylinder. One of the nuts on #1 was incredibly difficult to coax off as well. This was Thursday, and I was supposed to go somewhere the following Tuesday. Early Friday morning I ordered a "tight spot thread cleaning die" from McMaster-Carr, naively imagining, in this age of nearly instant delivery from Amazon, that it would arrive on Saturday. It didn't, of course. On Monday morning I drove down to McMaster-Carr, which is about 20 miles from my house, and got this die, which is basically a 5/16-24 nut with some notches in the threads and costs $1.31. (The original order arrived after dark on Monday.) When I tried to use it, however, I couldn't get it to start on the dirty stud. Eventually I managed to clean the stud up with a wire brush and with a "cleaning die" of my own that I made by filing notches in the threads of an AN nut.
In the meantime I had gotten six of the thin stamped stainless gaskets, which it is customary to use in pairs even though the Continental overhaul manual doesn't say so. A mechanic told me they should be installed "back to back", an instruction that I later realized was ambiguous since there was no way to know which side of the gasket, which has a raised bead around the rim of the hole, is the "back". When I installed the exhaust system back in the 1990s, I had nested them instead, and so for a while I imagined that that mistake was the cause of the eventual leak. Then Mike Melvill called my attention to the description of these gaskets in the Aircraft Spruce catalog. It says you're supposed to nest them; so maybe I had it right in the first place. I got a third opinion from an old and wise-looking A&P, who said nest them and install with the raised bead against the cylinder. He also said to bang the ears on the exhaust flange down with a hammer so that the flange is flat; somehow, although the material is 1/4" thick steel, these ears get bent upward so that contact around the rim of the hole is not as intimate as it should be. I didn't do this, and probably the gaskets will leak again. At least next time I'll know what to look for. A fourth informant told me that minor exhaust leaks can be corrected with red silicone. That got me thinking about the flanged connections I have at several points in the exhaust system, for instance at each end of the heater muff. Gaskets for those have always been a problem, and I think I read in some Lycoming bulletin that they should actually be assembled without any gasket at all. I don't think my flanges align that perfectly, but I wonder whether a bead of red silicone would be a better bet there than a solid gasket.
As it turned out the Tuesday appointment was canceled, and so the big rush was in vain.
[November 27, 2013]
Last week I finally tackled one of my two remaining hydraulic leaks. This one was under the right rear seat in the #2 master cylinder in the flap actuation system, operating details of which may be found here and for some nine months previous. I would regularly place a "sanitary napkin" consisting of a folded-up paper towel under the cylinder, and after a few flights it would be soaked with hydraulic fluid. Of course, I was also having to replenish the hydraulic reservoir unreasonably often. Having removed the cylinder and dismantled it, I found several longitudinal scratches on the 3/8" shaft. The scratches looked too fine to account for much leakage -- it took an 8x lupe to see them, and then only in certain light -- but I polished them out by chucking the shaft in the milling machine and grinding it successively with 320, 600 and 1500-grip emery paper until no visible traces remained. I found the shaft O-ring to be slightly twisted as well. I greased the O-ring groove and the new O-ring, reassembled the whole thing very carefully, filled it with hydraulic fluid so that it would not be necessary to re-bleed the system, and re-installed it together with its sanitary napkin. Yesterday after flying I checked the napkin and found it to be perfectly dry. I had also noticed after landing that the left flap retracted perfectly; previously the inboard end, where the #2 actuator is, tended to lag slightly behind the outboard, presumably because some of the fluid that should have been going from the master cylinder to the actuator had been leaking out past the O-ring instead. A great victory in my struggle against hydraulic fluid leaks! Now I have only the one in the #1 (left outboard) actuator to deal with.
The induction air temperature indication, which was working on the 16th, disappeared practically as soon as I got into the air. Fortunately, it is of no importance at the moment.
Yesterday I also tufted the inboard trailing edge of the wing to see to what extent the weak boundary-layer flow there, particularly pronounced at approach speed as seen here, is affected by increasing speed. The two pictures below show an area somewhat outboard of the 85-knot one, so they are not strictly comparable. The first was taken at 100 kias, the second at 130. They do indicate some improvement -- as would be expected -- with diminishing angle of attack, and a general tendency, also expected, for flow quality near the trailing edge to be influenced by profile thickness. The thickness at the innermost tuft in the pictures below is about 17.5% of chord; at the outermost tuft, near the outer flap track, it is about 15.75% of chord. Laminar sections with the maximum thickness far aft and with rapid pressure recovery are especially sensitive to thickness effects once they get above 15%.
I put a tuft directly ahead of the flap track fairing, and on its centerline, to see where it would go. It dresses on the left.
[November 16, 2013]
Finally, after dismantling everything for the umpteenth time, I have the oil and induction air temperature indications working again. I was right on November 5 to think that the oil temp was back to working and the induction air temp wasn't. In the end it was just a question of painstakingly cleaning out a Cannon plug and a Molex connector; all of the wires were intact, and the AN5525-1 resistance temp probes, including a spare, were all good and indicated 100 C when immersed in a bowl of boiling water.
[November 12, 2013]
Yesterday I made a flight to further wring out the Auto-Lean and also to check that the oil temperature indicator was working again. As to the latter, it wasn't; it turns out that what was working, as before, was the induction air temperature - the two use the same indicator, and are selected by a small toggle switch. I need to label the two positions; I keep forgetting which is which. At the moment the oil temp needle jumps to the left end of the dial when oil is selected; I'm not sure whether this means a dead short or an open circuit, but it will be easy to find out.
As far as the Auto-Lean is concerned, I found that peak EGT rose by about 50 deg. F between 2,000 feet, where I initially leaned to 50 LOP (lean of peak), and 12,500 feet, where I leveled out. The power setting was 27/2300 during the entire climb. The result of the rise in peak EGT was that the initial offset of 50 LOP gradually became 100 LOP. I tentatively concluded that I should select 25 LOP after takeoff, let the offset grow to 75, and then re-lean on leveling out.
This is what the Auto-Lean looks like. The black strap over the vernier button keeps it unlocked, so that it can be driven back and forth by a linear actuator that is connected to it with a quick-release fitting. The control head is below and to the right of the flap lever.
Curious once again about lower power settings, I tried reducing power to 23/1900, about 35%. Here the Auto-Lean did not do so well; it overshot on the lean side, causing the engine to cough and stumble. I disconnected it and leaned manually, eventually settling at a fuel flow of 5.7 gph. This yielded an indicated airspeed of 122 knots, a true speed of 153 knots, and fuel mileage of 27 nmpg; the density altitude was 14,500 ft.
This is remarkable performance for a 4-seat airplane, and I say that without any intent of patting myself on the back. It just seems to have happened. It is particularly unexpected because my performance calculation program predicts that a considerably higher fuel flow - about 6.4 gph - ought to be required to maintain that speed.
A great many assumptions enter into a performance calculation. For example, although the figure of 5.7 gph comes from an Alcor digital fuel flow meter that is most likely accurate, the amount of thrust actually available to overcome drag depends on two unknowns: the specific fuel consumption (sfc) and the propeller efficiency (usually symbolized by the Greek letter eta). At this relatively low indicated airspeed and power setting, furthermore, the fraction of the total drag that is due to lift - the induced drag - is about one sixth, compared with a tenth or so at a more typical 65% power setting; so the total drag is more significantly affected by the factor called e, the "span efficiency factor," which expresses how much worse the complete airplane is than an ideal wing, of the same span and aspect ratio, in isolation. Neither sfc, eta nor e can be known with certainty.
From speeds at higher power settings, where the influence of the induced drag is smaller, I have concluded that the equivalent flat plate area of Melmoth 2 is 2.35 square feet. (This corresponds to a CDp, or parasite drag coefficient, of 0.022.) This value, which by the way is not exceptionally low, is unlikely to change significantly at lower speeds, although my performance calculation program does assume that it will increase slowly with increasing angle of attack. In order to arrive at the observed performance at 35% of power it is necessary to assume a specific fuel consumption of 0.43, a propeller efficiency of 85%, and an e of 0.9. All of these values are right at the limit of plausibility. It seems like a sort of perfect storm of good numbers.
Actually, the rough correction for growth of parasite drag with increasing angle of attack, which is mostly intended to account for the rising pressure drag of the wing, may be wrong. The program makes the CDp 0.0232 at 122 kias; if it is in fact lower than that, then some of the other parameters would not have to be quite so improbably good. But the difference would be small.
So I seem to have lucked out. I recently heard an expression that seemed to me to encapsulate my style of engineering: "putting his spin on a revolving door." In other words, moving, but not going anywhere new. What I have done in designing Melmoth 2 is apply principles that I learned from other people. If the result has turned out unexpectedly well, the credit is theirs, not mine.
Oh, by the way -- I got as far as Santa Barbara, and when I turned back high clouds had painted the afternoon sea with a opalescent sheen.
[November 5, 2013]
I finally got the oil temp to settle down by, among other things, swapping probes between it and the induction air temperature. Now, however, the induction air temp is not indicating anything at all. I tried swapping in yet another probe and it still didn't work, so I don't think the thermocouple is the problem. Since the IAT was always unrealistically high with the probe in its present position, I am going to wait until I do the manifold reversal to troubleshoot it.
I finished the permanent installation of the Auto-Lean. In the process, I somehow disconnected a Molex connector in the fuel boost pump circuit; or perhaps it came disconnected as a completely separate misfortune. Anyway, the disconnected connector was behind the panel, thoroughly hidden from view, and I was unaware of it. This morning I was supposed to go up to Paso Robles, but the fuel boost pump wouldn't run, and so the engine wouldn't start. I started taking things apart, and after a while discovered that neither the power nor the ground at the fuel pump had continuity. That should have tipped me off that the problem had to be a connector somewhere -- too unlikely, otherwise, that both legs of a circuit would become disconnected at once -- but instead I was baffled and kept taking more and more things apart until finally I got a clear sight line to the connector. It's always interesting to see how obvious things become once you understand them.
[October 30, 2013]
An email from a Defiant owner who has the same overheating problems as I do when idling his front engine for long periods -- he mentioned Oshkosh, which just happens to be where I, too, have encountered this situation -- got me thinking again about why updraft cowlings might cool an idling engine less well than downdraft ones do. One thought that occurred to me is that when a cowling has two small inlets symmetrically situated beside the spinner, as most downdraft cowlings do, the blades completely occlude the inlets with each passage, leaving air little choice but to be forced into the cowling, whereas the wider single inlet below the spinner that both the Defiant and Melmoth have is only partially occluded, so that air can be squished out on either side of a blade as it goes by.
My correspondent tells me not all Defiants have this problem. If this is true, it does not seem to support my hypothesis; but I'm not sure how scientific a survey we're talking about. I would be curious to know how well various cooling arrangements and inlet designs work during long periods of idling on the ground in hot weather. I assume that any factory product can idle indefinitely on a 100-degree day without exceeding some equilibrium CHT in the middle of the green. (It can't be at the top of the green, because then when you start the takeoff run the engine will overtemp before you get a good flow of air through the cowling.) There aren't a lot of updraft-cooled factory airplanes; maybe some Aero Commanders? Time for a Google search.
[October 15, 2013]
I'm feeling quite pleased with the Auto-Lean. I find that after cleaning up and setting climb power I can just tell it to go to 50 LOP, and I don't need to think about mixture again until I level out. I used to spend 30 seconds or more delicately turning the mixture vernier a bit at a time and waiting for the TIT to hit peak and start to drop; this was time during which I was not keeping as good a lookout for traffic as I might. In addition, it feels more precise than manual leaning does.
Today a photographer, Carla Richmond, who is doing a portrait series of "men and their toys," met me at the airport a little before sunrise - photographers love the "golden hour" when the sun is just on the horizon - and spent a good long time taking about a million pictures of me and the plane and even things like trays full of bolts and clamps, the clutter in my rollaway's drawers, my maintenance log and a dust-covered hand-cream dispenser. When she was done I took her up for a half-hour flight out to the ocean and back. She had never been in a small airplane before, it was a windless and remarkably clear morning, and she thought it all very beautiful and, as she said, "calm." Taking someone up who has never been up that way - under a big transparent canopy, flying low over the hills and the city - refreshes my own sense of the wonder and beauty, and even the calm, of flying.
Nancy and I are going to Boston and New York again tomorrow morning; back in 10 days.
[October 10, 2013]
Flew to Paso Robles to take some measurements from which I hope to calculate the moment of inertia of a Le Rhone radial engine. Knowing the moment of inertia, it will be possible to quantify the gyroscopic moments experienced by an airplane like the Sopwith Camel.
I took off a few minutes before 9 a.m. It was a clear, still day, with a 20-knot flow on my nose but very smooth air over the mountains in spite of that. I climbed to 12,500 feet, set up 27/2200, and let the Auto-Lean gadget find and maintain 50 LOP. It did so, and speed and fuel flow settled down at 174 ktas and 8.1 gph. This was surprising, because it was a little better than expected; I usually say I cruise at 170 ktas and 8.4 gph at that altitude. During the climb I was aware of a sort of rhythmic shudder passing through the airframe every two or three seconds. I assumed it had something to do with the engine, but when I leveled out it disappeared, and so I began to suspect something aerodynamic. I don't know what; I will have to observe it for a while. A quick inspection after I returned to Whiteman revealed a worn piano hinge on the right outboard main gear door; I don't know whether that could cause the vibration I felt, but in any case I need to replace it.
Today the erratic alternator behaved normally; I guess you're not truly erratic until you're erratic only part of the time.
[October 5, 2013]
Sky-Tec fixed the starter for free, even though it was a bit out of warranty, so that's one gold star for them. I don't think I'll bother putting it back on for the time being, however; the weight difference is inconsequential.
I finally got the physical installation of the "Auto-Lean" gadget done, but then it didn't work; it's possible I have the polarity of the wires from the TIT thermocouple reversed. The oil temp needle is still bouncing around and the alternator is still behaving strangely, sometimes showing a 10 amp charge (and 28 volts on the voltmeter), sometimes zero and 25 volts or so. I don't know what to make of this; if it were just the alternator being intermittent, I would expect to see a small discharge on the ammeter (which shows current between the battery and the bus, and normally shows zero in flight once the battery is fully charged) when the voltmeter is showing what appears to be battery rather than alternator voltage; after all, there are various loads, avionics etc, running all the time. Why would it indicate precisely zero current but less than 28 volts? This is shortly after takeoff, when I would expect to see a steady recharge since the battery is slightly depleted from starting and holding at idle. If I run the hydraulic pump, on the other hand, I see a solid 17-amp drain, which suggests that the alternator is not picking up the slack. For the time being I can live with it because the battery seems to stay charged, but sooner or later I have to figure it out. As for the oil temp indicator, that's just a bad connection somewhere; I'll find it sooner or later.
I tufted the left aileron, very sparsely, just to see whether it showed a lot of spanwise flow -- in the inboard direction on the upper surface -- as the ailerons on Melmoth 1 did. (Those were piano-hinged on the lower surface.) During initial climb at 85 kias (takeoff flap) and 95 kias (flap retracted), the aft tuft at the inboard end of the aileron went completely crazy and quickly unwove itself into a bunch of separate strands. The pool of turbulent separated air along upper surface at the the trailing edge is quite evident in this video as well. At 123 kias the tufts looked a bit better behaved:
An odd thing is the way the tufts are angled slightly away from the surface at 123 kias; I'm not sure whether that is just due to the expected thickening of the boundary layer or whether it's exaggerated by leakage through the gap. It would be interesting to tuft the undersides, but I have no way to see them.
At 140 kias the tufts cling more closely to the surface:
[September 13, 2013]
Yesterday my "lightweight" Sky-Tec starter failed, fortunately at my hangar and not somewhere far away. I installed this thing in late June or early July of 2011, after a previous Sky-Tec design had ruined the starter clutch on my engine to the tune of $800. I forget what I paid for the original Sky-Tec, which I removed in February 2010, but they took $250 more for the new -5 with a clutch that allows the permanent-magnet starter to freewheel when it is not energized, thereby sparing the clutch inside the engine. I probably haven't gotten more than a couple of hundred starts out of the new one, which drew a cool 480 amps on the test bench at Aero Accessories in Van Nuys. Dead short. Nobody I have spoken to has had a kind word to say about any of the lightweight starters; apparently all brands are likewise unreliable. Furthermore, the Sky-Tec, at least, is not field-repairable; I guess you're AOG until they send you a new one (and you send them yet more money). Still, this could be seen as a safety feature; if you can't start, you can't fly.
I will put the old "heavy" starter back on the engine -- the -5 Sky-Tec with the solenoid is not actually that much lighter -- but it will present a new obstruction for the ducting of the reversed intake manifold. I am shopping around for a #6 cyl intake tube for the 360 Continental (I found a #5 and ordered it) so that I don't have to destroy the originals to mock up the new arrangement. I thought I had worked out a very simple path from the existing duct to the throttle body, which is going to be sitting above the vacuum pump, but I realized yesterday that the oil filler neck on my engine is different from the one on the engine installation drawing blueprints I got from Continental 40 years or so ago, and it obstructs the path I had planned. The fat starter will be another problem. Since I plan to connect the log manifold to the throttle body with SCEET hose, little deviations won't really matter, provided that I maintain symmetry. It would be prettier to do the transitions with aluminum tubing, though, and, as in most love affairs, looks are a consideration. Twists and turns that don't bother SCEET can be quite a bit more awkward for aluminum.
This intake-manifold-reversing idea has been floating around for three years now. Nobody could accuse me of plunging rashly ahead.
[August 21, 2013]
Yesterday I got out to the airport -- visiting children and grandchildren have diverted my attention from the Great White Offspring -- and took a bit of a sightseeing flight westward toward Oxnard, then around the end of the Santa Monica Mountains and back along the coast and across the mountains at Malibu Canyon into the west Valley. It's an interesting trajectory, not only because of the variety of city, mountains and sea that it includes, but also because of the always surprising variety of houses built by and for the fabulously wealthy on the ridges and in the foothills. This time I noticed for the first time, at the west end of the range, what appeared to be a couple of huge airplane wings resting on a mountaintop. Descending for a closer look, I found them to be just that; two vast swept wings that had become the roof of a house. When I got home and described this to my son he told me that it is a well-known thing: someone had incorporated a pair of 747 wings into a house in the mountains. Indeed, it turns out that there is a whole Wikipedia article about the place. At any rate, the mountains above Malibu are full of these remarkable houses. In the 1950s, in fact, when these Ozymandias-style palaces were far fewer in number, we used to visit, on foot, the unfinished and highly eccentric house of one Louis (or Lewis) Beach (or Beech) Marvin III, heir to the green stamps (or maybe blue chip stamps) fortune, who briefly dated Gladys, a.k.a. Sissy, the beautiful and clever sister of my erudite friend and schoolmate Tom Houston. In the atrium, open to the elements, a doomed grand piano hung suspended by cables from the roof.
Outbound and returning, I crossed the Van Nuys ILS to check my receiver. After the ILS quit working a couple of weeks ago, I had swapped the nav receivers, so that what was #2 was now driving the #1 OBS/ILS. It worked; at least the needles worked, the flags remaining proudly unmoved. Now each of my almost 40 year old Collins nav receivers has a disability: #2's ILS function is out, and #1 lacks the first digit in the display. Since the first digit is always a 1, this is not a big problem. The oil temperature needle is still wobbly -- I haven't yet gotten around to a really thorough inspection and cleaning of all the connectors and connections -- and the ammeter is displaying an odd behavior: It will display zero for a while, and then five amps for a while, then zero again, then seven amps, and so on. I guess I should know by now that exotic and mysterious electrical gremlins almost always turn out to involve a faulty ground connection somewhere or other.
I turn 70 today; this month the airplane turns 31, if you count from the start of construction. Omnes una manet nox!
[August 6, 2013]
I am neither dead nor ill; just briefly dormant. I was away -- not Oshkosh, but Cape Cod again -- for two weeks, and before that had some writing and other stuff to take care of, so I hadn't been doing much with the plane. I did fly around a bit to see whether cleaning the connectors had corrected the random fluctuations of the oil temperature indication. It was more stable than before, but still not perfectly steady. I need to get some spray contact-cleaning solvent and really wash the oil out of the connectors, particularly the Cannon plug that attaches to the probe itself. In the meantime I became aware that the ILS function of my #1 NAV receiver has quit working. I've begun making the wire harness for the auto-leaning gadget -- see previous entry -- and have mentally reversed the intake manifold many times; now I have but to do it in reality.
[June 14, 2013]
My oil temperature indication -- not the temperature itself, obviously -- began fluctuating rapidly on the flight down from Paso. I cleaned up a bunch of connections, but when I flew to test the vacuum pump -- it appears normal -- the oil temp was still jumping around. I then decided the problem was an apparent short in a miniature switch that selects whether the OT gauge shows oil temperature or induction air temperature. I replaced the switch, but got such unpredictable results -- some good, some bad -- while testing the system on the ground that I gave up fiddling with it until I have a chance to test it again in the air.
As far as the ailerons are concerned, I like them a lot up to 125 kias or so, but at cruising speed (around 140 kias) they're too heavy for me to be able to deflect them fully without extreme effort. I think that after a suitable breather I'll try moving the hinge line back some more.
A guy sent me a gadget to try out, and I'm beginning to install it. It's an electronically controlled mixture servo that seeks a selected EGT, like 50 F lean of peak (my personal favorite) and then holds it. Its usefulness is limited to maintaining a steady temperature; it does not readjust if you climb or descend or change power setting or the OAT has a big change. Still, I'm curious to see how it compares with manual control.
[June 7, 2013]
I got a $100 vacuum pump rebuild kit from Aircraft Spruce and overhauled my vacuum pump yesterday. On the Internet I found various dire warnings against doing this, but I can't see how there can be much harm in it, especially since I fly IFR so seldom. The instructions in the kit were laughable and I had to feel my way, aided by several consultations with a hangar neighbor, Claude Morgan, who knew no more about it than I did but was willing to second my hunches. The rotor was a fraction too thick and bound when the drive end cap was tightened down; I had to sand one or two thousandths off it before it would spin freely. I'll fly it today if there isn't a presidential TFR over the whole LA area. I'll look pretty silly if it fails immediately.
The more I fly the new ailerons the more I like them.
[June 1, 2013]
Today I flew up to Paso Robles for Chuck Wentworth's annual Antique Aero barbeque. On the way up I cruised at 25/2100 at 12,500 feet, 167 ktas with a fuel flow of 7.7 gph. (On a trip up there in February, I went a little slower, 149 ktas at 21/2000, 5.4 gph.) The speed coincides exactly with my computer simulation, which was calibrated to match the measured performance, so despite their larger gaps the new ailerons seem not to have affected the drag to a noticeable extent. The vacuum pump failed at some point; I noticed it when departing from PRB. I think it was the first vacuum pump failure I've had in 50 years of flying. It was quite insidious, and it took me a while to understand what had happened; I'm glad it didn't occur in IMC. Of course, I was in VMC, looking at the DG only intermittently and at the AH not at all. Still, I should have a warning light or tone (or both) for loss of suction.
Behind me on final approach at PRB -- the arrival was like Oshkosh, airplanes everywhere -- was a Lockheed Lodestar, which when it departed in the afternoon made a low pass at speed -- a fantastic looking and sounding airplane with a couple of 1,200-hp P&Ws. I feel a certain affinity for those Lockheeds because they use Fowler flaps like mine, that translate to the trailing edge of the wing before deflecting.
[May 30, 2013]
The new ailerons are now flying. They do reduce the stick forces, but at cruise speed (usually around 145 kias) the forces are still a little higher than I would like. Very roughly, I would guess that the stick force per unit of aileron deflection is now about half what it was before. Because of the design of the hinge hardware, I still have the option of shifting the hinge line farther aft by small increments. At the moment I feel all aileroned out, but I may start fiddling with the hinge location again in the future. It is currently 1.2 inches (at the root) aft of its previous position.
The testing procedure consisted of two phases. The first was to establish that there was no reversal or overbalance. I tested this by putting the airplane into a 45-degree bank in one direction and then applying a full stick deflection in the other. You want the stick force to be at least constant, or to increase more or less smoothly, with increasing aileron deflection. If the resistance diminished as the aileron deflection increased, it would be a sign that the ailerons were overbalanced, that is, the hinge line was too far aft. The worst case would be that the ailerons would pull away from center, a condition known as "snatch." You do this test at a fairly low speed so that there is no danger of the ailerons going to full deflection and your being unable to re-center them. A related issue is aileron reversal, in which the deflected aileron, acting behind the torsional axis of the wing, twists the wing in such a way that up aileron makes the lift increase rather than decrease. My wings are quite stiff, being thick -- 13% at the tip and 18% at the root -- and skinned with carbon fiber, and at the speeds I fly aileron reversal is not likely.
The other thing that needs to be checked is susceptibility to flutter. Again, low (ie under 200 kias) speeds and thick, stiff wings make flutter comparatively unlikely, but since it depends on an accidental coincidence of resonant frequencies you can't be sure without either ground vibration testing or in-flight testing by "pulsing" the controls. The former is very expensive, the latter a bit nervous-making, but free. John Thorp called it "tickling the dragon's tail." Beginning at a low speed and working upward by small increments, you slap the stick sideways hard enough to give the ailerons a visible jolt. You want them to return instantly to trail without oscillating; this is called "dead beat" behavior. I have so far pulsed the ailerons at up to 150 kias and their response is dead beat; as the testing progresses I will go up to 190 kias, which is the speed to which the rest of the controls, and the original ailerons, had been cleared by Mike Melvill in 2002. The faster you go the closer you are to the speed of onset of flutter -- which could be 300 knots or 191, no way to know -- and it's customary to dive past the target speed and pulse the surfaces while decelerating through it, just in case something starts to shake.
Prior to test-flying the ailerons I ran some computer analyses on them, using the PSW panel code. I made simplified models of the new ailerons and the original ones and computed the pressure distribution on their surfaces. I then integrated the pressures on the aileron surfaces only and obtained a moment about the hinge location. According to the computer, the hinge moments of the new ailerons were about 30% of those of the old ones. More important, they were of the same sign at maximum deflection; in other words, the computer did not think that snatch would occur.
Here is what the pressure distribution on the wing with an upward-deflected aileron looks like. The redder colors represent low pressures, green neutral, and blue high. Note the bulge on the lower surface, which is the leading edge of the aileron emerging below the airfoil contour because the hinge line is so far aft -- it's on the chord line, about at the station of the yellow band aft of the fuchsia bulge. It's noteworthy that although the angle of attack of the wing was zero for this analysis, the upward deflection of the aileron causes the pressure distribution over the entire airfoil, normally low pressure on top and high on the bottom, to be reversed. In other words, the increment or decrement of lift caused by a deflected trailing-edge flap is not confined to the flap itself; it is spread over the entire surface.
One final thing that was gratifying -- the two ailerons were sufficiently similar to one another that there was no apparent need for a trim tab.
[May 6, 2013]
Final weights on the ailerons, with 100% static balance, are 1,363 g (3 lb) and 1,284 g (2 lb 13.3 oz). Contouring, paint and counterbalance added nearly 50% to their weight. Each is about 1 kg (2.2 lb) lighter than the original ailerons.
[April 28, 2013]
Nancy and I returned on Wednesday night from a three-week trip. I spent Thursday answering letters and recovering from a cold I caught while away, and on Friday went to the airport. I intended to fly, but I found that my head was still so congested that my ears would feel full just going up and down the hills of Echo Park, so instead I did a little more work on the ailerons. I tested their stiffness by supporting them on their hinge pins, placing a 21-pound cinderblock at mid span, and measuring the deflection, which was about .12 in. for a 60-inch span. The purpose of this test was merely to be able to compare their stiffness with that of the original ailerons in order to see whether they are likely to create any new susceptibilities to flutter. I also measured the mass required to balance them, and was mildly surprised to find one of them requiring nearly twice as much as the other. The difference reflects different amounts and distributions of filler on their surfaces, magnified by the filler being farther from the hinge line than the counterweight is. I ordered 12 feet of 5/16 x .035" SS tubing from McMaster-Carr to use as counterweight material; it should arrive on Tuesday.
[March 29, 2013]
I notice, looking back over the past few weeks of entries, that 1) I have been progressing very slowly and 2) I have been repeating myself quite a lot. The repetitions are due in part to the sporadic nature of these reports, which gives me time to forget what I said in previous ones, and in part to the fact that whatever can be said about one aileron is likely to be equally true of the other. Besides, I'm getting old. A new rudder would perhaps involve less redundancy. As far as the slowness is concerned, it is due mostly to competing demands on my time. If I had my druthers I would spend more time working on the plane than I do; it is sad that my father thoughtlessly neglected to amass vast wealth.
I see that some time ago I said that I would test-fly the ailerons before painting them. Obviously, I didn't. In retrospect I'm not sure why I thought that would be a good idea; the only thing about them that can be changed is the position of the hinge line, and that can be done just as well after painting as before.
I had an instructive experience a few days ago. My oil filter is mounted upside-down, so that it drains into the engine after shut-down and therefore never spills any oil when it is changed. I had changed the oil and filter a few days earlier, and had not removed the top cowling to do so, since it is not difficult to get at the filter through the left side cowl panel. Last Thursday was the first time I intended to fly after the oil change. I started the engine and taxied a few hundred feet, but I kept hearing an odd sound, a sort of sssht...sssht. Then I noticed that my oil pressure was about 10 psi, and I immediately shut down the engine. I looked back to see a trail of oil where I had been and a hangar neighbor following me on foot; getting out, I found oil pouring out of the cowling. Together we pushed the airplane back to my hangar; he was kind enough to get a bag of kitty litter from the gas pit and spread it on the pool of oil I'd left on the taxiway. I wiped the worst of the oil off the cowling and fuselage and sprayed everything with detergent before going home. It was apparent that the oil leak was coming from the oil filter, but I didn't know why. The next day I took off the filter and found that when I removed the old filter its gasket had fallen off and remained resting on the mounting pad, somewhat off-center. Because I was looking into the cowling from the side, I had not seen it. When I put on the new filter it tightened down on top of the old gasket. It looked and felt normal, but actually was not sealed at all.
I had to add eight quarts to bring the oil back to its normal level -- which is eight quarts. No harm seems to have been done -- the next time I flew all temperatures, pressures and sounds were normal -- but henceforth I will be more attentive to even routine jobs like unscrewing an oil filter. And if you had asked me whether I always check oil pressure after start-up, I would have said yes; but obviously I didn't.
[March 28, 2013]
I'm finally painting the ailerons. I should just have time to attach the hinge hardware at the start of next week and perhaps balance them -- probably not the latter -- before leaving on a three-week trip to the east coast. The current plan, when I get back, is to take them out to Mojave, install them there, and make the first test flight from the 10,000-foot runway. I doubt that they will be overbalanced; in fact, my main concern is that after all this work there will be little or no difference in their hinge moments.
Although the aileron looks oddly beige in the photo below, it isn't; it's "ivory", the same color as the rest of the airplane. In fact, if anything it's lighter. I'm painting it, as the rest of the plane was painted, with a brush, but it's not coming out as smooth as the rest of the airplane. I've lost my touch.
[March 16, 2013]
As I did on the left side, I removed the right aileron in order to 1) make new hinges and 2) put the old hinges and aileron back into place. This took a several hours of cutting and fitting. Before replacing the old aileron, I temporarily put the new one into place, adjusted the hinges so that the lower surface was flush with the wing, and laid down a strip of filler over about half the span of the upper side where the wing surface was slightly higher than that of the aileron. That strip of filler, which is just a couple of inches wide and feathers into the aileron surface at its rear edge, will serve as a guide for contouring the upper surface. (The leading edge of the filler strip is rough because I trowelled my excess filler on there; it's the smooth upper surface that will be the guide.)
[March 7, 2013]
In the past couple of weeks I have found time to laminate the second aileron and complete the contouring of the first. It's incredible how long this has taken me; small wonder the entire airplane took 20 years. The last step in contouring was to spray the aileron with several coats of a dark gray primer and wet-sand it with 600. The result is a very pleasing surface, reminiscent of the Santa Clara black pottery one sees in Santa Fe; unfortunately this will have to be replaced with boring fake-looking glossy white paint in which a few bugs and bits of airborne grit are bound to become entombed. It was interesting, by the way, and surprising, to find that the weights of the two ailerons, in their uncontoured state, were within a few grams of each other: about 815 grams, or 28 ounces, each. Their area is 2.7 sq. ft. Unfortunately, countouring, balance weight and attachment hardware will increase that weight by 50%.
Part of contouring each aileron is to mount it in the wing and ensure surface continuity. To do this on the right aileron I have first to revise the hinges on that wing; so I still have a way to go. On the left side I contoured the underside first, adjusted the hinges to position it correctly, and then laid down a band of filler on the top surface and squeegee'd it to the proper height with a thin aluminum strip bridging the wing and the aileron. After it cured I used that band as a guide for contouring the rest of the upper surface. The layer of filler is mostly very thin; you can see the underlying black skin through it.
I have been busy in the past few weeks designing a set of new wheel pants and gear leg fairings for an old Stinson. The result looks very close to optimal on the computer, but you never know how these things are going to behave in real life. The existing pants showed horrible flow separation between the leg and the inboard side of the pant facing it. Whoever designed them seems to have had no idea of interference drag.
[February 16, 2013]
Contouring -- filling and smoothing the surface before painting -- notoriously requires hundreds of hours of tedious and messy work on composite airplanes whose skins are not made in female molds. The curse of it is that the closer you come to perfection the more glaring tiny imperfections appear, and so you feel compelled to erase increasingly inconsequential blemishes. Almost all of the contouring on my airplane was done by a professional, Roy Bailets, and I have never developed much skill in that department. So I can have major stumbles, as I did when I so grievously undercatalyzed a coat of polyester primer on one side of the left aileron that I had no choice but to scrape it off. Twenty hours after application it still had the consistency of clay. I have since learned that the recommended ratio of primer to catalyst is 64:1. I had misguidedly used something like a tenth of the proper amount. Why did I not read the directions on the can? I did. They said something like, "For mixing instructions, see product data sheet" -- a data sheet that I did not have.
[February 3, 2013]
On Monday, the day I was intending to test the left aileron on the airplane, I received an email from a reader of this site, Harry Manvel, warning me to approach asymmetrical ailerons with caution. He knew a builder, he said, who had flown with two different ailerons, and had had to hold full lateral stick deflection until he could get back on the ground. In that case, the chords of the ailerons had been quite different, Manvel said, and so it "might be apples and oranges." The chord of my new ailerons is the same as that of the old ones, but his warning got me thinking, and I realized that because the hinge moments of the two ailerons would presumably be different, and since ailerons naturally tend to float upward, the old aileron would float upward, overpowering the new one and pushing it downward, and I would have to hold left stick continually. This could be quite unpleasant, since the roll forces are high and the stick is very short. Left stick, furthermore, is the more difficult to hold. Even if the situation were not dangerous, it would camouflage whatever impressions I hoped to get of the feel of the new aileron, and would render the whole experiment pointless. So I didn't do it.
[February 2, 2013]
The weight of the left aileron is now up to 2.5 pounds. That includes the attachment hardware and a 100-gram, or about 3.5-ounce, balance weight in the nose. The rest is filler. The balance weight consists of a 20-inch length of 5/16" stainless steel tubing, slipped into the 3/8" tube that is built into the nose of the aileron, and held in place spanwise by wooden dowels inserted from either end. Cotter keys retain the dowels. Because the hinge line of the the original ailerons is relatively farther forward, they required considerably more balance weight and weigh about 5 pounds each.
I was surprised, when I got the dowels at Home Depot, to see that they were made in China. How can it be that a round piece of quite ordinary wood, manufactured by an entirely automatic process, can be more cheaply created in China and shipped to the US than made here?
If other obligations do not prevent me, I will install the left aileron and fly it early next week to see whether there is any indication of hinge moment reversal -- or, for that matter, of hinge moment reduction. Of course, with one of the original ailerons and one new one, it will not be easy to tell what is what; but I hope to get some useful impressions.
[January 22, 2013]
After several days of filing and fitting, I finished the new aileron hinges for the left wing. The aileron somehow turned out to be the right length; it did not require any fancy shims or joggles to slide snugly into place between the hinges. The trickier hinge was the outboard. The original hinge consists of a flanged bellcrank bearing set in a 3/4-inch hole in a fiberglass plate. The new hinge is a 3/4" O.D. spherical bearing, and its center is 0.825 inch farther aft. The whole assembly fits within the contour of the wing, which is about 1.5 inch deep at this point. The problem was how to integrate the new hinge with the existing plate without making it impossible to re-install the existing bearing, since I am not yet ready to permanently install the new aileron. It was touch-and-go for a while, but everything worked out nicely in the end.
I have begun contouring the left aileron; here it is mounted to a work table and slathered with a mixture of glass microballoons and epoxy.
The procedure is to put on too much and then sand it away. The bare aileron weighed 850 grams, or about 1 lb 14 oz; I am curious to see how much the finish adds. Notwithstanding my earlier resolution to leave the underside uncontoured, I am doing it because the trough where the lower skin joins the upper at the trailing edge is on the underside, and it has to be filled anyway. Filling the weave over the rest of the surface adds very little weight, and reduces the risk that I will sand though the skin at the edge of the trough. I know of one instance in which the builder of a composite homebuilt actually got killed by overly zealous sanding.
[January 11, 2013]
The inboard end of the aileron looks like this.
The lower hole, with the nutplate threads just visible, is the hinge point; the actuating pushrod will be pinned through the upper holes. Hinge and pushrod attachment are an inch apart; the chord here is about eight inches. The rectangular well in the end rib is to provide clearance for the nutplate in case it needs to be moved to adjust the aerodynamic balance. The hinge point is currently at 25% of the nominal chord -- by "nominal" I mean not counting the extension for the counterweight.
[January 7, 2013]
Despite the holidays and the diversion of our visiting children and grandchildren. the left aileron is nearly done; I just need to prime the aluminum hardware at either end and fill the notch at the trailing edge. It currently weighs just under two pounds, but that will go up a bit with paint and the nose counterweight.
I was in doubt as to whether to fill and smooth the surface before painting it. A nicely finished surface would look nicer, of course, but otherwise serve no purpose. In principle, I should not care if people looking at it say to themselves, "Wow, what a mess!" But Mike Melvill said that he grew heartily tired of explaining the unsmoothed control surfaces of Rutan's original VarEze to curious onlookers, and recommended filling and contouring as a preventive measure. My compromise solution will probably be to contour only the upper surfaces; that way I will have to explain myself only to little people. In any case, I will not paint it before test flying it.
Here is the detail at the tip, with the corresponding parts from the other tip beside it. The chord of the aileron here is five inches.
The requirement was to provide a 1/4" steel pin for the hinge, and distribute the forces from it into the phenolic end rib and from there into the carbon skin, while preserving the option of moving the pin fore or aft to adjust the stick forces. The solution I chose is a 1/8" aluminum plate secured to the aileron end with three 10-32 countersunk screws, and a flanged stainless-steel pin that nests in a recess in the plate. The flange is very slightly thicker than the well is deep, so that it is clamped in place against the aileron. The load to be carried is on the order of 80 pounds.
The tube in the nose of the aileron is part of the counterweight. It is 3/8 x .028 SS, and runs the full length. I plan to add additional weight, up to about 105% static balance, by sliding a 5/16-inch wooden dowel into the SS tube with lead pellets epoxied into holes drilled in the dowel.
I still have to modify the hinge brackets on the wings, both to allow adjusting the hinge line if necessary and to preserve the option of going back to the original ailerons if for some reason I choose to.
[December 12, 2012]
This morning I laid up the lower-surface skin on the left aileron and vacuum-bagged it. The bag is simply a piece of 4-mil plastic sheet (the kind that is sold in 10x25 foot rolls in hardware stores) folded over and sealed along the edges with some very sticky mastic called bagging tape; I suspect this stuff must have some more mundane primary purpose in the building trades, like bedding window panes, since it is fairly cheap. The single-ply skin of 10-mil bidirectional carbon cloth is covered with a thin ply of dacron, which peels off later (hence the name "peel ply") and leaves a clean surface ready for subsequent bonding or finishing. Then comes an absorbent layer to wick up excess epoxy; I used a cut-up T shirt. A couple of straight extrusions are taped to the underside of the foam core, and a piece of 1/2-inch square steel tubing is laid atop the trailing edge, to keep everything straight. I use about half an atmosphere of vacuum; that's not very critical in this case, since I am not forcing a large amount of epoxy out of the carbon skin. The weather is cool -- around 60, with rain coming -- and it will take a couple of days for the layup to cure thoroughly, but it will be sufficiently cured tomorrow to remove it from the bag. Time permitting, I may be able to do the other side on Friday. In the picture below, the light-brown stuff is the epoxy seeping through the T-shirt, most of it in the vicinity of the spar cap.
[December 6, 2012]
I bonded the stainless tube into place for the left aileron. I was uncertain whether to then do the same for the right or to complete the left first; I will take the latter course, so as to avoid any irrecoverable mess-ups. I tried in vain to get the two 30-inch segments of trim (which I intended to use as supports while bagging the skin) to line up properly. The idea was to bag the trim blocks -- the portions of the foam blocks cut away when hot-wiring out the aileron cores -- down to the flat table, then to lay the aileron core on them and bag the skin onto one side of it; but as soon as I pulled a vacuum on the trim blocks they would turn out to be slightly misaligned, in spite of my repeatedly shimming them with layers of .003 plastic sheet. Plan B is to secure a couple of straight extrusions to the backside of the core with masking tape, and then to use a free bag for the lamination. The important thing is just for the ailerons to be more or less straight and particularly for the trailing edge to be straight, since it is the place where a kink or wave would be most obvious to the eye. Aerodynamically, perfect straightness will not make much of a difference.
I flew to San Luis Obispo yesterday wth Mike and Sally Melvill to see Ray Henning, who was down from Seattle with his friend Yvonne to visit wineries and the scenes of his reckless youth. The day was perfectly clear and in the late-afternoon light, as we returned to Tehachapi, the mountains and valleys of the coastal range were very beautiful.
It was dusk as I flew back to Whiteman, and I had the flashers and nav lights on. At a certain point I noticed that the ammeter was indicating a 10-amp charge -- it ought to show zero, once the battery is fully charged, which it normally is within a few minutes of takeoff -- and the voltmeter was indicating 26 volts rather than the expected 28. After a minute or so of this the ammeter suddenly jumped back to normal; and after a few more minutes this behavior repeated itself. I hate electrical gremlins; I never understand them.
After the 100-mile clarity of the rest of the trip, the LA basin was filled with a thick haze; Whiteman was VFR, but, although it was still twilight and there was plenty of ambient light, I could see only the two VASI lights until I got within a mile and a half of the runway. I don't know how newcomers manage to find an airport on days like this.
[November 30, 2012]
Some progress, despite the holidays, which tend to bring everything to a halt. I laminated the end ribs into place with two plies of carbon. The bidirectional carbon cloth I have turns out to be .010 thick, not .006 as I believed, so I will use just one ply for the skins. The end ribs get the additional ply because they support all the concentrated loads. Mike Melvill machined some small parts for the inboard hinge and pushrod attachment and the outboard hinge pin. Each aileron will be held in place by a single bolt; a cantilever pin projecting from the end rib will slide into a spherical bearing at the outboard end. The next step is to bond a 3/8" stainless steel tube into place in the leading edge; the mass-balancing material will go into it.
[November 16, 2012]
I was wrong to think that I will be able to skin two ailerons at once. I overlooked the fact that the two outboard cores were cut from the same blank, overlapping one another. I suppose, however, that something is to be said for learning from the mistakes I will inevitably make on the first aileron, and avoiding them on the second. Not to say that I will avoid making new mistakes on the second.
The first blunder I uncovered was that I used a blank 31 inches long for the outboard cores, believing it was 30 inches long; hence there is a small, probably undetectable error in taper, and I had to cut the end ribs off those cores, trim the cores to the proper length, and reattach the ribs. I am now adjusting the heights and positions of the trim pieces that will support the cores during skinning. One lesson that I learned too late is that it was a false economy to cut the two end cores out of a single blank; I should have used a different blank for each core, and set the templates in such a way that they ended up properly aligned on the table without a lot of trimming and shimming. Here, at any rate, is the core for the left aileron, temporarily laid out on the workbench. The groove for the spar cap is visible, as is the pocket in the inboard end rib that allows the nutplate for the hinge bolt to be adjusted fore and aft.
[November 10, 2012]
It's difficult to predict the hinge moments of aerodynamically balanced control surfaces, and so I designed the new ailerons to allow the hinge line to be shifted over a pretty wide range. Three #10 nutplates on each of the 1/16" phenolic ribs embedded in the inboard and outboard ends of the ailerons -- these are the same phenolic patterns as were used for hot-wiring the cores -- allow the chordwise position of the hinge hardware to be adjusted. Of course, the hinge points on the wings have to be adjusted too. Maybe, however, I'll get lucky and the hinge moments will be acceptable the first time around, using what seems, from a half-century-old NACA report, to be a good default position.
So far I have only bonded the phenolic ribs to the cores. The next step is to vacuum-bag two plies of carbon cloth over these end ribs, extending an inch or so over the core. After that, I will align the two 30-inch core segments of each aileron with each other, supported by the foam blocks out of which they were cut, and bond in place the 3/8" stainless steel tube that runs as a counterweight along the projecting leadng edge (see here). After that, one side (the bottom) is skinned, the whole thing is flipped and the other side skinned, and finally a closing tape is added along the leading edge. The unidirectional carbon spar caps, which are there to prevent the ailerons from bowing excessively under air loads (since the hinges are at the outer ends rather than at intermediate locations along the span), will be sandwiched between the two plies of the skin.
This is quite a lot of operations, but I think that although the skins can go on only one side at a time, it will at least be possible to do both ailerons at once.
[November 8, 2012]
Melvill and I flew to Paso Robles to check out some test equipment in one of Javier Arango's Sopwith Camels. This time Mike remembered to bring his iPad and Stratus ADS-B receiver. Although my initial impression was mainly of the number of thumbprints an iPad accumulates and of their remarkable conspicuousness under a bubble canopy, I couldn't help being impressed by the torrent of information the thing supplies. Situational awareness will become a thing of the past, I fear. I hate to admit how much time we spent staring at the iPad rather than looking outside the airplane.
[October 31, 2012]
Today is the tenth anniversary of Melmoth 2's first flight.
Yesterday Mike Melvill and I flew up to Stockton to have lunch with Dick Eklund, an old friend of mine and protege of John Thorp's who lives in what used to be Thorp's house, built in 1862 by Thorp's grandfather. That gent came to California with the gold rush, but rather than prospect he opened a grocery store in what is now Lockeford. Dick manages the support of T-18s, and has been repairing his own T-18 after an accident. It's nearly ready to fly again. Mike's EZ was having an oil change, and so I picked him up at Tehachapi. The round trip was about 620 sm, the time about 3.5 hours, and the fuel burn around 32 gallons. We cruised at 11,500 and 12,500, at the usual 140 kias and 8.5 gph. There were no clouds and very little wind; on the way up our GPS groundspeed, 174 knots, was identical to our true airspeed, and on the way back down we may have had two or three knots of headwind.
Mike had intended to bring his iPad, but forgot it, to his great regret because he was enthusiastic about showing me what a great convenience it is for flying. It happens that a friend of ours, believing that she had lost her iPad, bought a new one, only to have the old one returned. She lent it to us, and I am going to try it, once I find out what accessories and subscriptions I need. Mike commented on getting into my airplane on the "classic" instrument panel; he suggested -- I believe facetiously, but I'm not certain -- that it might be a good idea to just velcro an iPad up over it.
[October 24, 2012]
In ten years I have had six biennial static/transponder checks, and of those two have involved me in expense and wasted time because of false results that turned out to be due to problems with the test equipment. This time, at least, the technician stuck around to troubleshoot the problem, and offered to pay the cost of my having unnecessarily shipped the encoder back to the manufacturer after his previous visit (I declined). He also helped me find a static leak, where I had modified the plumbing last year because of a problem with water getting into it. Anyway, now everything is fine again.
Tomorrow Russ Hardwick and I are hotwiring the cores for the new ailerons. The hotwire is a 43-inch-long piece of .032 stainless steel safety wire stretched taut and electrically heated to the point that it melts or vaporizes its way through plastic foam. Two people guide the wire along templates secured to the ends of the foam blank, using correspondingly spaced and numbered index marks to keep in step with one another. If all goes well, the result is a smooth foam core of exactly the right shape and size. To prevent the wire sagging because of the drag of the foam, we are going to do two 30-inch cores instead of one 60-inch one. The portion of the foam block that lies outside the core will later serve as a jig to support it during laminating.
[October 14, 2012]
Someone asked whether the panel lights should be red to preserve night vision.
I learned to fly 50 years ago. At that time panel lights were usually red and the instrument panel itself was black. At some point, I forget when, panels began to be painted gray and instrument lights turned white. I don't know why this change occurred, though I'm sure it is well documented in the annals of the FAA Aeromedical people at Oklahoma City. Perhaps it had to do with middle-aged pilots using white flashlights to read increasingly crowded charts. Perhaps it was an early signal of the gradual decrease in sensory connection between pilots and the world outside the cockpit, epitomized today by game-like electronic displays for navigation and terrain avoidance. My habit, when I was regularly flying at night, was to turn the panel lights as low as possible and to allow my eyes to achieve the greatest possible degree of dark accommodation. It was pleasing to be able to discern through Melmoth's transparent canopy the Milky Way, the swarms of faint stars, and the outlines of mountains against the faint skyglow of a western night. While crossing the Pacific, in fact, I turned off all the interior and exterior lights for a while in order better to appreciate the spelean blackness that surrounded us.
From an old man's reluctance to relinquish habits formed when I was first a pilot, I have painted the panel of Melmoth 2 (or at least the parts of it that I have bothered to paint at all) black, and I suppose that if I were to resume night flying, which is unlikely, I might find the five white LEDs that currently constitute my entire interior lighting unacceptably bright. It would not be very difficult to replace them with red ones, and/or to add a dimmer.
[October 11, 2012]
While waiting for my encoder to return from the factory, I wired and temporarily installed some panel lights. I had bought five medium-intensity LEDs and mounted them in parallel on a piece of thin fiberglass laminate. (My friend Russ Hardwick, who knows something about electricity, says I should have put them in series; to my objection that that way the failure of one would cause all to fail he replied that LEDs never fail. I guess I could have provided an equally forceful argument: I never fly at night.) The choice of five was sheer guesswork, but turns out to be a pretty good first cut, if my impression of their brightness from throwing a rug over the canopy and sitting inside is any indication. The assembly is currently just snapped into place in the overhead and held by friction. The panel lights share a switch and breaker with the nav lights; at the moment there is no provision for dimming.
[October 9, 2012]
I converted the paper templates into computer files of coordinate lists in airfoil section format, and thus was able to ensure that the middle one was precisely intermediate between the ends and that all three matched the corresponding wing sections. Based on Part 23 control surface loads, the limit load on each aileron is 154 pounds, which produces a moment of 1150 in-lbs about 25 inches from the inboard end. The section depth at that point is about two inches. By good luck I happened to have a slab of the unidirectional carbon fiber laminate that I made for my wing spar caps back in the 1980s (never throw anything away!). It is .080 thick, and strips about 3/8" wide along the top and bottom high points will provide the requisite bending strength and stiffness. A single ply of bidirectional carbon cloth would be sufficient for torsional loads, but I think I will use two plies for the sake of a more durable surface. The last few days I have been busy with my biennial pilot-static-transponder certification and with wiring panel lights, however, and I have not made any practical progress on the ailerons.
[September 28, 2012]
To the three approaches to reducing aileron hinge moments listed below, a correspondent added yet another: pneumatic boosting. He suggested using the pressure difference between upper and lower wing surfaces, but I think ram pressure would work better. The pressure would be valved to bellows that would push the ailerons one way or the other, depending on stick position. Denny Polen used that method in his Polen Special, a 300-mph Midget Mustang. But I think it's a bit too complicated for me.
After fiddling around on the computer for hours, I finally reverted to the old paper cutout method of designing control-surface profiles, with this result:
The length of the longest section is 8 inches. The profiles represent the inboard and outboard ends of the aileron and a section halfway between them; the foam core would be hot-wired in two 30-inch-long segments, because it's difficult to hot-wire small radii over a 60-inch span. The nose contours are designed to provide 1/8" clearance from the existing cove lips at full deflection. The projection on the leading edge is provision for a counterweight, basically a piece of 3/8" diameter tubing of aluminum or steel that runs the entire length of the aileron.
[September 27, 2012]
Several readers joined the discussion of aileron balancing. One suggested spade balances, which competition aerobatic airplanes often have. These are flat plates, normally aligned with the airstream, mounted on arms projecting downward and forward from the ailerons. They are powerful and convenient, but too draggy to use on what is supposed to be a clean airplane. Another asked whether gearing couldn't be used to reduce the stick forces. The answer to that question, which is not intuitively obvious, is no: a series of bellcranks between the stick and the aileron can slightly modify the distribution of effort vs deflection, but the total amount of work that has to be done remains the same. In other words, only the stick length and swing, and the aileron hinge moment, matter; all the gearing between them cancels out (except for a little additional friction).
A question was raised about the need for thickening the aileron on the lower surface as well as the upper, since flow has a natural tendency to remain attached to the lower surface. The point is well taken, especially in view of the fact that with the wing developing lift there is going to be some leakage through the aileron gap from bottom to top. I would think it would mostly involve boundary-layer air, and would enhance the likelihood that a more energetic flow would reattach to the lower surface of the aileron. I don't think, however, that any harm would come from thickening both surfaces of the ailerons, and the balancing effect of flow over the portion of the aileron ahead of the hinge might be enhanced.
I realized last night that the design as shown below has a potentially dangerous characteristic. I defined the hinge location in such a way that the nose of the aileron, which is a circular arc, would touch the cove lip at its extreme upward deflection of 25 degrees. The problem with this lack of clearance is that under load the wing and aileron may bend differently, and the lip could bite into the aileron and trap it. Something of that sort happened to a factory Cirrus during flight testing. Because it occurred at low altitude, the plane, which wouldn't stop rolling, crashed before the pilot could bail out. I have to either shorten the aileron chord and move the hinge backward a little more, or else take a divot out of the leading edge to provide clearance. The divot is probably the better choice. It would normally be hidden within the cove, and so it would not add any ugliness (always a major consideration).
[September 24, 2012]
One of my few persistent dissatisfactions with Melmoth 2 has been with the aileron hinge moments -- that is, with the stick forces in roll. At 140 kias, the ailerons don't move more than two or three degrees before the stick force becomes uncomfortably high. As a result, I have never rolled this airplane. I used to roll Melmoth 1 all the time -- probably to the dismay of my passengers. Melmoth 2 would be more fun to fly if it had lighter roll forces, and I have thought a great deal about how to bring that about.
Various approaches are possible; they fall into three categories. One is to slice off a portion of the trailing edge of each aileron, hinge it, and link it with a pushrod to the wing in such a way that deflecting the aileron upward causes the tab to rotate downward; this is properly called a "lagging balance tab," though many people would call it a "servo tab." A second approach would be to recontour the ailerons, making them flat-sided rather than cusped and providing them with a beveled trailing edge; this approach was used on Mooneys, which were notorious for their stiff ailerons. A third approach would be to replace the present ailerons with aerodynamically balanced ones.
I'm against beveled ailerons because they're so ugly. Balance tabs add weight at the trailing edge, where you least want it, and reduce the effectiveness of the ailerons. Aerodynamically balanced ailerons imply larger gaps and some additional drag, and their behavior is very difficult to predict. So I have remained in a quandary, and done nothing, lo these many years.
Lately, however, I overhauled the control-surface-design portion of my lofting program, and now I have Hoerner and various wartime reports on aileron hinge moments spread out on my desk and am teetering on the brink of making myself a new set of ailerons. Pretty much for aesthetic reasons, I am inclining toward the aerodynamically balanced variety. The most generally useful source of data on these is NACA Advance Confidential Report No. L4E13 from May, 1944, ANALYSIS OF AVAILABLE DATA ON CONTROL SURFACES HAVING PLAIN-OVERHANG AND FRISE BALANCES, by the alliterative duo of Paul Purser and Thomas Toll. The importance of balanced controls increased during the war as fighter speeds rose and bombers grew larger but boosted controls had not yet become the norm. Their design is tricky; they are sensitive to hinge position and nose shape, as well as angle of attack. It seems, however, that the most reliable first cut is to design the section with a circular-arc leading edge, as if it were unbalanced (this is the current design), but then to shift the hinge line aft to about the quarter-chord point of the aileron. Since there is some risk of overbalance with this procedure, I am considering a design in which the inboard hinge location, at least, could be shifted fore or aft a little if need be.
In addition to moving the aileron hinge line aft, I would thicken the ailerons slightly with respect to the wing profile. This is a trick used to encourage reattachment of the boundary layer to the ailerons aft of the gap. It would actually be preferable to thin the wing ahead of the ailerons, but it's too late for that.
Here is the portion of the wing between spanwise stations 140 and 200, with the new aileron profiles and hinge locations indicated. The cove lips, marked by tiny blue-green plus signs, remain unchanged, as do the deflections (-25,+12) and the actuating hardware. The present hinge location is at the same chordwise station as the cove lips. The vertical line is the rear spar location.
[September 14, 2012]
The faulty mag had evidently had a coil failure. The coil, which carried a stamped date of 1981, had been left in place when the mag had its 500-hour inspection just a couple of months ago. It was not covered by the warranty. I found this odd, but the guy at the shop explained that coil failures are unpredictable, not particularly correlated with age, and that to routinely replace coils would nearly double the cost of the inspection without necessaily serving any purpose. I suppose I can see the logic of that. On the last day before Nancy and I left for a 3-week trip to New York, Cambridge and Cape Cod (we seem to be becoming habitually bicoastal), I reinstalled the repaired mag, timed it and did a run-up, but did not have time to fly. We are now back, and I'm going to go out to fly it today, although the forecast temperature at the airport is 102.
When we landed at LAX yesterday the airport was under one of those strange fog banks that leave one half of a runway in the clear and shroud the other in mist. We taxied past a Korean Air A-380, and I was struck by the gull-wing-like distribution of dihedral. I suppose in order to keep the landing gear trucks short and the engines above ground, the blimp-like fuselage sits low and the wing inner panels angle rather steeply upward. The outer panels are more horizontal, or at least appear so; when they're full of fuel they sag, and it's hard to judge how they would look in flight.
[August 20, 2012]
On runup today I found that my left mag was completely inop. This must be why old-timers check their mags after landing. Tomorrow I'll take it to the shop that recently overhauled it. Had lunch with Jerry Slocum and Mike Melvill; Mike's Long-EZ, he said, has more than 4,000 hours on it. It looks beautiful, and brand new, but it's more than 30 years old.
[August 15, 2012]
Prices for the 20 amp-hr Yuasa batteries I use are all over the map, but I found a couple for $60 (each) at Amazon. Yesterday they arrived and today I installed them and put them on a slow charge.
Replacing the batteries is quite a big production, because first they have to be filled with acid -- they come dry -- and the acid (sulfuric, dilute) did not come with them. I started out by buying two boxes of the stuff at an AutoZone store near the airport. When this turned out to be insufficient, I went back, only to learn that a gentleman had just bought their last two boxes -- that gentleman being I. I found another box at another store -- AutoZones are all over the place here, like Starbucks -- and finally got the fluid into the batteries without spraying too much on my hands and in my eyes.
Getting the batteries into the plane is the next problem. Their terminals are rectangular lead cages with a nut inside. The machine screw that engages this nut is a little too short, and I always end up having to shim one or two of the nuts up with cardboard to get them to engage with the screws. I noticed at AutoZone that they carry a motorcycle battery dimensionally similar to mine, and with a similar model code, but sold under the name of "Duralast". They were $60 too, and came with their own supply of acid. Maybe I'll try them next time, if I don't hear something awful about them first. I've observed that one of the laws of marketing seems to require presenting as a virtue your product's principal defect; thus, I am inclined to suspect that Duralast batteries would last less long than other types.
Several people have suggested that I use a different type of battery, for instance a gel cell; but the battery box, which is pretty much integral with the cowling, is built around these particular batteries; any replacement would have to have exactly the same dimensions.
[August 8, 2012]
Yesterday I flew down to Torrance to meet with some people connected with a South African kit and LSA manufacturer called The Airplane Factory. They make 2- and 4-seat versions of a low-wing all-metal design called "Sling", and have flown both versions around the world. From Torrance a bunch of us flew in three airplanes -- a Sling two-seater, a Brazilian Samba "motorglider", and Melmoth 2 -- over to Catalina Island for lunch. Mike Blyth, one of the company's founders, rode with me. After lunch the other two planes took off, but Mike and I found ourselves stuck on the ground; Melmoth would not start. In fact, it would not turn over. In fact, the voltmeter read nine volts, and dropped to near zero if I pressed the start switch. This was puzzling, since the batteries are quite fresh and the starter had cranked powerfully on the day's two previous starts.
Electrical problems are particularly annoying, because they are often hard to understand, hard to locate, and impossible to see. The first thought that goes through one's mind in a case like this is a bad ground, possibly corrosion at a battery terminal. We cleaned up all the battery connections, without effect. Finally, directed by the sympathetic fellow manning the Unicom, we located a start cart, which consisted of an old stick-shift pickup with a couple of batteries in back and 12 and 24-volt outlets on the front bumper (where I would never have found them, had Mike not thought to look there). Melmoth has an external-power socket -- it has been used many times -- and now it started right up. Keeping the engine running, I dropped Mike at Torrance with an emphatic (and unnecessary in this case, since he is very experienced with airplanes and propellers) briefing to go off the trailing edge of the wing and stay away from the propeller.
Voltmeter and ammeter readings were normal during the flight. After shutting down at Whiteman I tried to restart and got the same result as at Catalina -- that is, no result at all. The voltmeter again indicated low and dropped to almost nothing when I pressed the start button. I checked the voltage at the battery terminals; 25.4, which is normal immediately after shutdown. During the flight, however, I had noticed that two electronic devices with reset buttons, the GPS and the fuel totalizer, had to be reset several times. This suggested momentary power interruptions. Suspicion now falls upon the master switch and the master contactor; I will check them out today.
[later...]
Every time there is an electrical problem, my first impulse is to assume some very exotic reason for it. Then, after I get tired of imagining arcane phenomena never encountered before, I fall back upon the general-purpose "bad ground" theory. That one works a large part of the time. But sometimes the cause is even simpler than that.
Bad battery! One of the two 12-volt batteries that I run in series had apparently suffered some sort of major internal breakdown. It delivered 12+ volts to a voltmeter, but as soon as you put a load on it that dropped to almost nothing. I guess it would be handy if I added a three-way selector switch to the on-board voltmeter circuit, so that you could look at either battery separately or both together. Apparently failures like this occur without warning, however, so I'm not sure that this one could have been foreseen; but at least it might have been diagnosed more quickly.
[August 3, 2012]
The "Driver" cylinder no longer leaks.
[July 27, 2012]
After returning from two weeks on the east coast I resumed my overhaul of the auxiliary cylinder on the flap controller (labeled "Driver" here). The telltale paper towels that I put under hydraulics to detect drips are always pink under this cylinder, whose function is to make sure that when the flap retracts all four actuating cylinders end up back at their initial extension. It's a single-acting cylinder -- it just pushes, doesn't pull -- and although I could not find any obvious source of leakage when I took it apart (on July 9, just before I left) I decided to replace the aluminum piston with a steel one on the principle that one ought not to have an aluminum piston running in an aluminum cylinder if it is not immersed in fluid on both sides. Yesterday I rough-machined the new piston; today I will attach it to the shaft, finish machine it, and, if all goes well, assemble the cylinder and install it in the airplane.
If it still leaks, suspicion will fall upon the hose; but leaky high-pressure hoses are rare indeed. A few weeks ago I looked at a small HD color video camera to replace my now rather outdated low-def black and white one. It is slightly larger than my present one (which is about the size of a sugar cube) but color would make it easier to see something like a drop of hydraulic fluid forming on the underside of a cylinder or hose. If the cylinder still leaks after this fix, I guess the next step will be to make a movie about it.
[July 5, 2012]
I found some references to cooling-air temperature rise in old technical papers. The three values cited were 120, 130, and 150 degrees F, so the 121-128 range I recorded was at least in the ballpark. They also talk about cylinder head temperatures higher than I allow -- eg 435 F -- and about more demanding cooling scenarios, like a full-power climb; so I suppose the fact that my temperature rise is on the low end of the scale might be related to the fact that I climb at 65% power and cruise at 55%.
I have wondered whether it really makes much sense to climb at reduced power. Rate of climb is directly proportional to excess power, and the engine is more efficient at higher power settings than at lower ones; so it would seem that at any given indicated airspeed I might as well climb at the highest power setting consistent with good cooling. The only argument in favor of spending more time in the climb is that it means spending more time at the most efficient angle of attack.
[July 3, 2012]
I moved my high-tech backyard chef's RF meat temp probe to the hot side of the baffles in order to find out the temperature of the outgoing cooling air and also the temperature of the throttle environment during long periods of idling.
Altitude | OAT C, F | Cowl temp | Rise | Remarks |
Ground | 28, 82 | 68, 154 | 40, 72 | After runup |
5,000 | 23, 73 | 83, 181 | 60, 108 | climbing at 105 kias, 50 lean of peak, cowl flaps open 1" |
7,000 | 20, 68 | 87, 189 | 67, 121 | |
9,000 | 18, 64 | 89, 192 | 71, 128 | |
11,500 | 14, 57 | 81, 178 | 67, 121 | cowl flaps open 0.5", 140 kias |
11,500 | 13, 55 | 79, 174 | 66, 119 | cowl flaps closed, 138 kias, 27/2300; hot cylinder 175C/350F |
11,500 | 13, 55 | 81, 178 | 68, 123 | 30/2300, 144 kias |
9,000 | 17, 63 | 71, 160 | 54, 97 | descending, 160 kias, 23/2300 |
6,500 | 22, 72 | 69, 156 | 47, 84 | |
Ground | 28, 82 | 92, 198 | 64, 116 | 2 minutes after shut-down, cowl flaps open |
During the climb I was adjusting the cowl flaps to keep the hottest cylinder below 200 C (392 F). It's interesting that the upper deck temperature rise seems to stay close to 67 C (120 F) under various cruising conditions. Now I need to dig through my papers on cooling and try to find out whether this would be considered a good temperature rise or not. Obviously you would like to stuff as much heat as possible into as little air as possible, but the returns diminish as the air heats up. It should also be possible to calculate the cooling air volume, since the heat rejection of the engine is known (I think). Actually, you can get that from the delta-p -- the pressure drop across the cylinders -- too.
[June 22, 2012]
Run-up this time was good -- there had been a loose nut on one plug -- and the test flight went fine. I had a distinct impression of more power during the initial climb; I was 1,000 feet agl halfway through the crosswind leg, despite climbing at a nominal 75% power setting. A perceptible increase in power seemed unlikely to me, but I mentioned it to the mechanic who had installed the mags and he did not seem skeptical; he said that ignition harnesses begin to deteriorate after five years or so in use. I don't know whether my Bendix harness was 20 years old or 40, but in any case it was well into the post-five-year phase. I'm not sure, however, what "deteriorate" means in this context. If the harness looks good, has no kinks or chafing, and the leads into the plugs are in good condition, is there any hidden deterioration? Do the wires get tired of the hard work of carrying high-voltage current? Perhaps the conductor migrates toward the shield in tight bends. I don't know.
[June 21, 2012]
Last Saturday an A&P from one of local shops, Able Air, came over to my hangar and installed and timed a pair of overhauled Slick mags, leaving it to me to add the harness. I looked online for tips on how to do this and found none, except the comment that it would take about four hours. What a laugh. It took me four hours on each of three days. Well, maybe three on one of them. Perhaps if you were exactly replacing an existing harness it would take four hours. But the new harness is longer than the old Bendix one, and allows for more natural paths which, in turn, required making new holes through baffles and closing old ones, deciding on new clamp locations, and so on. Not realizing at first that this was the case, I mistakenly thought I should sort out and attach the plug leads first and secure the magneto caps afterwards. In retrospect, this made very little sense. I ended up arranging and rearranging the leads two or three times before getting them sufficiently untangled to tie down. I then had to add the pressurization plumbing and the air filters, which had been removed when I put the unpressurized Bendix mags on in 2003, and finally the tie-wraps and the attendant bloodshed. The last thing I did was attach the P leads. For some reason that I can't remember now -- it dates back to 1997 or so -- I had wired the P leads as full circuits running from the mags to the panel switches and then back to grounds on the mags. This was quite unnecessary; the ground terminal can be near the switch, and should be. But it was at least convenient to attach the ground leads to the Bendix mag cases, which bristle with #10 screws. The Slicks don't have any place to attach a ground lead, so I had to extend them to somewhere else, which happened to be a ground post on the alternator. Actually, now that I think about it, this whole story makes no sense either. In 1997 the Slicks were on the engine -- I took them off and put on the Bendixes after one of the Slicks had a coil failure on the way to Oshkosh in 2003 -- and so when I first installed the engine I must have found a place on the mags to attach the grounds. It's a mystery.
Yesterday afternoon I finally started the engine, which ran, although a bit more roughly on the left mag alone than on the right. So at least the leads are going to the right plugs.
While doing this I was reflecting on the sensations of manual work as opposed to writing. Time passes frictionlessly at the hangar. Sometimes I experience little waves of frustration or impatience, but mainly I remain in a state of absorption that is neither happy nor unhappy, but mindless, if you take "mind" to mean the continuous fretful agitation of the personality that reminds us that we are alive and that we continue to be ourselves rather than someone else. I have gravitated to the mindless state for many years now, spending thousands of hours working on my two planes. I am reminded of a comment in an old New Yorker article that the stream of consciousness of an alligator is probably like a dial tone. Mine is like that when I work; or perhaps a busy signal. To say that "I love the work" would be sentimentalizing it. Perhaps it's just an escape -- but from what? My life is not exactly full of troubles.
As the title of this blog implies, a little inner voice tells me that I have chosen to do mechanical work rather than to "strictly meditate the thankless muse", and that there is something shameful in this. On the other hand, offers a rival voice, perhaps I have simply followed the path for which I was better suited.
[June 13, 2012]
The Australian tech support guy was unable to figure out from the photos I sent him what was wrong with my ultrasonic motion detector, so I got another kit and assembled it last night. This one works, as far as I can tell; I now need to test it in flight. My other ultrasonics project -- the rangefinder that I thought could be used as an airspeed measuring system, completely independent of the pitot -- will not work, I realized this morning, because changing speed will change not only the transit time of the sonar signal but also its frequency, and so the receiver, which is tuned to 40 kHz, will not recognize the return signal. I should have realized that a year ago; I fail more and more intelligence tests these days. I suppose it is some comfort that none of the people with whom I discussed the scheme pointed out this rather obvious flaw in it; or maybe they were just polite. I suppose that an electronically astute person could work around the difficulty with variable tuning and some sort of speed-feedback scheme, but I am unfortunately not he.
I suppose that if I insist on using the ultrasonic rangefinder, which is accurate to 0.1 inch or better, for something, it could be as a very fancy flap or airbrake position indicator or a squat switch.
Later in the day...
Had lunch with Russ Hardwick, talked over the question of the Doppler effect on the ultrasonic airspeed gadget. I was confused; it would not be an issue, because since both transmitter and receiver are moving at the same speed, they compensate for one another. A stationary observer between them would hear the transmitted ping as shifted upward in pitch (assuming it is facing upwind) but the receiver, because of its own motion, would cancel out the shift.
[June 6, 2012]
Rather comically, on my first flight after taping the pre-landing checklist to the panel and adding a window in the nosewheel well through which to verify that the gear is down, I ignored both. Old dog, new tricks.
I had my Slick pressurized mags overhauled and acquired a new ignition harness, my old Slick harness having evidently disappeared, probably with the dissolution of my overhauler, Western Cylinder, after the death of Mike Attolico. I'll have them installed and timed next week.
In the meantime I've been fiddling around with some electronic projects. This is completely new terrain for me. I had gotten an ultrasonic rangefinder (a "Parallax Ping") about a year ago but I didn't understand how to use it; just recently I got a student microcontroller kit called a BASIC Stamp and found an article online showing how to program it to interface with the Ping. Sure enough, it works. If I can successfully desolder either the transmitter or the receiver from the Ping board, I should be able to rig up the experimental electronic airspeed indicator I wrote about a year ago. I also got a DIY ultrasonic motion detector that I hope to use as a ground proximity sensor; the idea is to trigger a landing gear warning if the plane is 20 feet or less from the ground and the gear is not down. So far it refuses to work and after a few initially promising emails the product support guy in Australia has fallen silent, perhaps after seeing the photos I sent him of the assembled board. I hope he eventually returns to my aid.
[May 17, 2012]
On Tuesday I flew up to Tehachapi with Jerry Slocum, an old friend from Melmoth 1 days, for lunch with Mike and Sally Melvill. On the return flight to Whiteman, we had a near escape from disaster. We were on short final, at maybe 100 feet, when someone in a Skyhawk holding short for takeoff called the tower to say that our gear was not down. I put it down and we landed uneventfully. But if that guy had not been holding there, and had not paid attention to the landing airplane, I would have seriously damaged the airframe, engine and propeller.
Naturally I have thought a lot about how this happened. Usually mental failures of this kind are connected with deviations from habitual patterns or with unexpected, distracting external events; but there had been none. The approach was the usual straight-in from the Newhall Pass. The normal sequence of events is to slow from 130 or 120 kias four or five miles out by opening the airbrake. At 100 I lower the gear and extend 10 degrees of flap. I trim to approach speed, turn off the fuel tank auto switcher, open the cowl flaps, put the prop in fine pitch, make sure the mixture is rich, and open the wastegate fully. All this is usually accomplished by the three-mile call. I go to full flap at about one mile.
On this occasion I somehow missed the gear-lowering step. That is puzzling in itself. I can't account for it, and I can't think of what I could do to prevent such a mental slip in the future.
But what is odder still, and what I can do something about, is that I have a clear memory of checking that the gear was down, and believing that I saw the indication that it was. As Jerry said, it was a case of seeing what I expected to see. The gear up/gear down indication consists of two labels on a large torque tube near the floor on the right side of the cockpit. One label says "GEAR UP" and the other simply says "DOWN". Both have bright aluminum-tape pointers that align with a fiduciary mark when the gear is either up or down. All three gears are mechanically interconnected, and so the position of this torque tube signals the state of the entire landing gear.
What I now understand about this system and how I relate to it is that I have always used it to check that the gear has cycled fully. That is, I have paid more attention to the alignment of the silver arrow and the fiduciary mark than I have to the words UP and DOWN. When I glanced at it on this approach, I verified that the marks lined up -- but I evidently failed to register the fact that the nearby word was UP and not DOWN. (Actually, the word UP is partly eclipsed by the arrow, an infelicity that I had ignored in the belief that it was clear enough.)
I need to provide a more direct, non-verbal signal of gear position. The simplest would be to put on the torque tube conspicuous red and green stripes that would rotate into sight as the gear went up or down. That would be a simple improvement that would eliminate the need to actually read a word and grasp its meaning. It would also be quite easy to add a microswitch, or two microswitches, that would light up red and green lights on the panel -- though lights are surprisingly easy to ignore. The most complex arrangement, and most similar to those in production airplanes, would be to combine those microswitches with a third on the flap actuator starwheel, or to use a motion detector to sense the proximity of the ground, so that the combination of full flap or ground proximity and retracted gear would sound a buzzer.
No system is perfect, witness the gear-up landings that occur in airplanes provided with all sorts of ingenious lights and buzzers. But I now realize how imperfect my present system is, and how much it relies upon a certain quality of alertness and attention on my part. I gave myself enough of a scare that it will probably be several years before I backslide to one casual braindead glance at the torque tube to verify gear position; but at any rate it seems important to add some conspicuous color to it right away.
Another thing that might be wise would be to put the pre-landing checklist on the panel. I never use the paper one on my kneepad, always relying on memory, because pre-landing is such a busy time that consulting the checklist seems cumbersome. I'm not sure I would use it if it were permanently on view, and it would certainly not prevent such primitive errors as looking at the word UP and not noticing that it was not DOWN; but it might add a small extra margin of reliability.
Thinking about intercooling, I collected some temperature data. It was a warm day, OAT 18C above standard. I had a temperature probe installed where the throttle body will be if the manifold is reversed, and there is a built-in induction air temperature probe at the end of the left log manifold. The IAT probe, which is simply an AN oil temperature probe, has always indicated implausibly high -- around 100C; it seems that it is actually reporting the temperature of the aluminum manifold, not the air inside it. Here are the temperatures I recorded (all Celsius):
The OAT gauge, which is digital, is acting up and practically unreadable, so the OAT numbers may be off; they certainly don't display the expected lapse rate of 2C per 1000 feet, but it wouldn't be the first time Los Angeles had an inversion. The IAT numbers are obviously suspect. The cowl temperatures make sense, since the air at the place they are being measured, high up behind the engine, has passed by the exhaust pipes and the turbocharger to get there. The purpose of collecting this information was to help decide whether an intercooler, if I were to install an intercooler -- which is by no means certain; that's a separate decision -- could use internal cowling air or would require a separate outside air inlet.
By the way, specialists are fond of insisting that "intercooler" is a misnomer, because intercoolers are properly heat exchangers placed between stages of multiple-compressor superchargers, and that the proper term is "aftercooler". This seems like a display of erudition for its own sake -- a crime of which I am often guilty myself -- because the "inter" could just as well mean "between the compressor and the throttle" as "between one compressor and another." Besides, for etymological parallelism, "aftercooler" ought to be "postcooler", though "tc" doesn't roll off the tongue quite as nicely as "rc" does.
Anyway, the real question is not what it ought to be called, but whether or not it's worth having. I ran some rough numbers and concluded that the additional heating burden created by compressing air at 18,000 feet is about 10% of the engine's natural heat rejection. If you can keep the CHTs down with the existing cooling flow, then the only reason for the intercooler would be detonation margin. Unfortunately that is something I know next to nothing about. At 30 in. Hg at 18,000 feet, the turbo output is at 175F or so; rather hot.
The engine began to feel slightly rough at 14,000 feet and 2,300/27; if I increased the rpm and reduced the manifold pressure, it smoothed out. This did not feel like cross-firing due to unpressurized magnetos, which manifests itself as random small jolts, but at any rate I am thinking about replacing my unpressurized Bendix mags with pressurized Slicks. They were on the engine when I first flew this airplane, and I replaced them with the Bendixes -- stored ever since I installed the turbocharger on Melmoth 1 in 1980 -- after one of the Slicks had a coil failure en route to OSH in 2003.
[April 30, 2012]
The end cap bore having been enlarged by .006, the wastegate passed the latest flight test without any problem. Now it has but to stand the test of time.
[April 24, 2012]
I turned the wastegate spool down to .738, put it back on the plane, and flew it today for the first time. The test was generally successful. The turbo seems to be able to deliver more pressure at lower rpm than it used to; if this is true (my first impressions, which include the recurrent feeling that my car's engine runs better after I clean the windshield, are often not borne out by later experience) then it is most likely due to the improved breathing of the larger, three-necked banjo box. The wastegate spool worked during most of the flight, but it seized during the descent. On disassembly, which required a hammer, it was evident that the spool shaft had galled in the end cap bore, most likely because the end cap cooled faster than the shaft did. Enlarging the end cap bore a bit should take care of that.
Here's what the thing looks like in place:
[April 19, 2012]
The wastegate is now installed, but on the first ground runup it stuck at about 45 degrees of rotation. It is typical of me that I would rely on intuition to select my clearances, and only do the required (and very simple) calculations after my guess turns out to be wrong. So after yesterday's unsuccessful test I at last checked the coefficient of thermal expansion of stainless steel. The spool (the rotating part with the blade or butterfly at the end) is 3/4" in diameter, and would expand by about 0.012" at the peak turbine inlet temperature (1650 F). The tube inside which it turns (the "boss") gets hot too, of course; if it were at the same temperature it would expand by the same amount and clearances would be preserved, but it is exposed to cold air and so expands less. I found some data online about auto exhaust surface temperatures at full-throttle operation; they suggested that the boss might get up to only 800 or so, in which case the differential expansion would be .006. The current difference between the boss bore (.750) and the spool diameter (.746) is just .004, so I obviously have to take off a few thousandths more. Just to complicate matters, there must be a temperature gradient along both the spool and the boss, so I am working with a lot of unknowns and will have to proceed a little bit at a time.
Here is the complete wastegate. The bellhorn to which the vernier push-pull cable attaches is still missing, because we won't know how long it can be until the assembly is in place. Mike is coming down tomorrow for a fitting. The valve spool is retained by a cap about the size of a quarter, which in turn is held in place by a stainless-steel band secured on the back side of the bypass tube with a single bolt (see the drawing lying under parts in next picture down). The design is intended to make disassembly easy. In the exhaust system, even stainless steel parts eventually accumulate a layer of crud, which can be removed by a light scouring with emery paper. I'm hoping that regular cleaning will help keep the wastegate working smoothly.
[April 12, 2012]
Mike Melvill, who apparently got his taxes done early, decided to go ahead and make the rest of the parts for my adjustable wastegate. In the picture below, the spool is an aluminum test article for the milling-machine program. The real spool is 321 stainless steel.
The original design, reflected in the sketch lying under the parts, had called for a piston ring sealing the spool against the "boss" -- the short tube sticking out of the side of the J-shaped one. (A picture of the whole thing in its original, non-adjustable form is below.) I didn't know the dimensions of the piston ring yet, and we decided to go ahead without it, and instead to provide two flanges between which some sort of glass or ceramic packing would be wound. The blade-like portion of the spool is the butterfly:
The butterfly appears too short in the right hand image, but that's a trick of the light on its generously-radiused base. The full diameter of the spool actually does not intrude into the bypass duct.
I have not gotten my taxes done yet, and so this is not going to be installed before next week.
[April 6, 2012]
The air filter box and triple-duct banjo box are now in place, as is the vernier cable for the wastegate. Mike Melvill volunteered to machine out the plug in the wastegate, which was galled into place, and to ream it to .750. My neighbor says he'll have the butterfly done this weekend. Making allowance for unexpected developments and for the Rule of Three -- which states that a job will take three times as long as you expect, even if you take the Rule of Three into account -- I may be able to fly in a couple of weeks.
[March 29, 2012]
Advancing on three fronts, I have nearly finished the new banjo box for the turbo air inlet, partially machined poppet valves for the main gear oleo orifice plates, and partially destroyed the fixed wastegate assembly. This last item, while not directly constructive, may be viewed as the sort of bridge-burning gesture that leaves one no choice but to go forward.
My oleo maven has become interested in instrumenting my landing gear in order to measure deflection, rebound, acceleration and so on, but since it makes sense to get data for the stock oleo first, I won't be doing the orifice modification right away.
As for the wastegate, my next-door neighbor, who has a machine ship in his garage, had some 3/4-inch 303 round bar stock and volunteered to machine the butterfly for me. I am now waiting for him to do so; I don't feel that I can rush him, but in a few days I may begin mumbling the word "grounded" in subliminal tones. I found a usable vernier cable among the decades' worth of precious stuff, read "junk," in my hangar. It's a crummy-looking thing, probably a 40-year-old mixture control from a 172 or something like that, but it's the right length and a different color and shape than my mixture vernier -- it's good to differentiate things. I was wrong, by the way, when I wrote on March 16 that the tee pipe is smaller than the bypass pipe; they have the same O.D., and so it will be possible bore the tee out to 3/4 I.D. and therefore to fully shut the wastegate -- not that that is necessarily a good thing.
Tomorrow I plan to do the final layups on the new three-duct banjo box, which looks like some sort of artificial heart:
The thing next to it is the air box, which sits below the filter. The triple ducts are 2.25 in. in diameter; for years I have made do with a single duct and a considerably smaller banjo box, but it probably rendered the turbo somewhat asthmatic. That didn't matter so much when I didn't have a proper wastegate, but once I can make full use of the turbo it should be better to let it breathe more freely. We'll see.
[March 20, 2012]
A couple of weeks ago someone suggested that a good way to inflate the main gear oleos equally was to put a tee on the strut pump output and inflate them both at once. This sounded reasonable and so I did it. Fortunately the modification was cheap, because it didn't really work. For one thing, if one strut was a little taller than it should be, it would not come down; the air valve is one-way. But that's not a big deal; you have to bleed air out of an overinflated strut anyway. (Struts get overinflated seasonally, when rising temperatures make the air or nitrogen in them expand.) The real problem is that when you inflate a strut you are not adjusting the pressure, only the piston extension. Once the piston starts to emerge, the pressure remains constant; it is simply the load on the strut divided by the area of the piston. The amount of piston that is exposed becomes a function of the amount of space in the oleo that is not occupied by hydraulic oil. So if the struts are not identically charged wth oil, they will not extend to identical heights. Not that it matters, unless they're wildly out of whack. But the whole point of the exercise was to get the struts equal, and, because I had used different methods of filling the two struts and they didn't contain identical amounts of oil, it didn't really work that way.
Another complication arose yesterday when I needed to add air to my nose strut. It's necessary to close one branch of the tee in order to pump up a single oleo, so I would have to add a petcock on one side. Considering that this well-intentioned trick was intended to be a simplification, it seemed to be getting more, rather than less, complicated.
I may have a chance to equalize the fluid levels in the struts in the not too distant future, however, because my oleo strut consultant has proposed that I replace the fixed orifices in the struts with ones incorporating check valves that would uncover additional orifices during the compression stroke. These would have less damping on compression and more on rebound, which is to say that they would provide squishier landings with less bounce. Not that I have ever bounced a landing in this airplane; it's such a floater that even a bad landing amounts to nothing more than a stiff tap. But you can see that any bounce in landing gear is bad, and so very high rebound damping is desirable. Javier Arango, who owns a Corsair, told me the other day that its landing gear has virtually no rebound at all; it squishes down on a hard landing and then just oozes back up -- clearly preferable to Cessna-like springiness when landing on a carrier. This would be a very simple modification, and I am inclined to do it as a matter of principle.
[March 16, 2012]
I made a plug for the new banjo box for the turbo inlet, but I probably won't get around to laminating it until next week. I also thought some more about the wastegate. This is what the present one looks like:
The bent bypass tube is 7/8" in diameter, with an I.D. of 3/4". The tee entering it from the left is 3/4" O.D. The present "gate" consists of the threaded bolt (secured by safety wire) that screws into the tee from the left; it has a bullet-shaped end that partially blocks the bypass tube. The idea is to replace this fixed obstruction with something adjustable. I thought a butterfly, but my machinist friend Homer, who is something of an expert on engines, didn't seem enthusiastic about that idea. I got the feeling that he thought that small parts operating at very high temperatures can be troublesome. He suggested replacing the fixed bullet with one that slides in and out. But he has not seen the engine in real life, and did not realize the space constraints surrounding it. As far as I can see, the only way for the push-pull cable to get to the wastewate is from above and inboard, and at a right angle to the tee pipe. My latest proposal to him (upon which he has not yet commented) combines the rotation of the butterfly with the massiveness of the bullet:
This is basically a butterfly, but with no issues of securing it to a shaft and with a big heat sink attached to it. It would be a loose fit in the tee pipe -- maybe .005 radial clearance -- and could have a piston ring for sealing, though I'm not sure that would be necessary because it will expand somewhat relative to the cooler tee pipe. Because the I.D. of the tee is less than that of the bypass tube, there would be a small segment-shaped leak on each side of the bullet when it is closed; but there can be a bootstrapping problem if a wastegate seals perfectly, so perhaps that wouldn't matter.
[March 13, 2012]
As part of my effort to delay indefinitely the day when I take a hacksaw to my $1,500 Continental intake manifold, I started working on increasing the size of the air duct leading from the air filter to the turbocharger. My present scheme, which may succumb to practical difficulties as I implement it, is to add two more SCAT ducts going from the inlet air box to the banjo at the turbo inlet. The big difficulty here is that I put the turbo air inlet too close to the firewall, and so the banjo can be only about 1.5 inches deep. A single 3.5-inch duct would be nice, but won't fit. Three separate 2.25-inch ducts are not an ideal solution, but they are bound to be better than one. Resistance is a function of flow speed, and so tripling duct area should reduce resistance by a factor of nine or so.
After ignoring the subject for years, I took another look at the wastegate. The present wastegate is the fixed one from the Piper Arrow and Seneca; designed for absolute simplicity of manufacture and operation, it is really just a fixed leak that limits exhaust flow to the turbo with the unintended consequence that at lower altitudes the turbo is usually blowing against a partially-closed throttle. It's okay for middle altitudes, but not very good higher up. I wanted to replace it with a butterfly. Homer Knapp, my machinist friend whom I trust for advice about such things, suggested a loose-fitting sliding plug instead, with a piston ring at one end. The thing will be manually controlled, and so it needs to offer as little resistance to adjustment as possible.
I checked compressions for the first time in a couple of years. I don't put much stock in compression tests -- if you look at them over many years for the same engine, they wander all over the map -- but it was nice to see that at 1,200 hours all of them are still 76/80 or better.
[February 21, 2012]
Some combination of 1) overhauling the struts, 2) getting the fluid levels right, 3) getting the inflation levels right, and 4) retracting the flaps during rollout seems to have eliminated the "sagging strut" problem. That took way too long -- on to something more interesting!
[February 18, 2012]
Two hours indeed. Actually, it took me four and a half hours to overhaul the left main strut, repack the wheel bearings, and put everything back together again. Some of that time was spent cleaning years' worth of grime from the gear, however, and some making new tools and re-discovering which old ones to use, and some going to buy more hydraulic fluid, so I think the whole job really could be done in three hours or less by a well-organized mechanic. Since it needs to be done only every few years, you forget all the tricks in the interval. Removing the gear from the airplane and replacing it is quite simple, and dismantling the strut itself takes just a couple of minutes. I found that the main O-ring that seals the sliding piston was twisted, but it still seemed to be sealing all right. O-rings are remarkable things. It may, however, have been increasing "stiction" in that strut. I set both struts to 2.7 inches cylinder-to-fork, but this morning I re-read the pertinent page of the owner's manual and saw that it's supposed to be just 2 inches. I guess I've had my struts over-inflated all these years. The manual doesn't say at what weight the struts should be showing 2 inches; I assume it means something like half-full tanks (for a Cherokee) and no people inside, since that might be the typical condition of an airplane in the shop.
One thing I didn't do, and should have, was replace the brake pucks; but they still have some life left. They're currently at 0.175 inches; the rivets meet the disks at 0.125.
To fill the strut, I made a special tool consisting of an AN816-4 pipe-to-flare fitting with a 2.5-inch long 3/16" OD aluminum tube pressed into the pipe-thread end. This is inserted in the normally plugged hole at the top of the strut, and a hose goes from it into a can of hydraulic fluid. The strut is then slid in and out a few times, drawing fluid in and expelling it by turns, and ending with the strut fully compressed. The effect of the extension tube is to preserve a couple of inches of airspace at the top of the strut, as required. (The reason this tool is needed for my struts, and not for unmodified Cherokee struts, is explained at January 5, below.) This operation could be performed in situ if there were a small hole in the wing skin above the strut, but it doesn't seem as though one needs to add fluid to the struts that often. If you have to add fluid, there's a leak, and so you might as well pull the strut and fix the leak.
People often say that struts should be charged with nitrogen, but I prefer a mixture of 78% nitrogen with miscellaneous other gases.
[February 16, 2012]
I was supposed to fly with Jerry Slocum, an old friend, to Tehachapi to have lunch with Mike and Sally Melvill, but a brief storm went through yesterday and left behind it 35-knot gusts at a right angle to the runway; so we took a rain check. Jerry and I went to the Whiteman restaurant and talked for almost four hours about old times, mutual friends, the Airbus vs Boeing controversy, travel, ageing, and various other topics. After he left I decided to overhaul the left main gear strut. This time, having learned one or two things from doing the other one, I was able to remove the strut from the airplane in half an hour. The whole operation shouldn't take more than two hours, if nothing turns out to be wrong. I'll replace the brake pucks while I'm at it; I should have done that on the other side too.
[February 11, 2012]
We came back last Tuesday from two weeks on the east coast. On Thursday I did a circuit of the pattern to test the theory that retracting the flaps during the roll-out would reduce the tendency for one main gear strut or the other to remain excessively extended. The experiment was inconclusive; the weather was quite warm -- around 80 -- and both struts were over-inflated to begin with, the left more than the right. I remembered to use the airbrake this time, so at least I now have some video representative of the real landing configuration. The airbrake, which is a board of about 2.25 square feet that sticks out of the belly just ahead of the wing at a 60-degree angle, produces some helpful nose-up trim and also a little extra lift. I use it on landing as though it were a second flap.
I removed the fairing and camera from the left boarding step and will put them on the right in order to see how well the right main gear doors are closing.
The problem of bending tubing to connect the existing intake manifold to a throttle body mounted at the back of the engine turns out to be more of a challenge than I first thought, but it finally dawned on me that there is a simple solution: SCAT or SCEET hose, the type with an internal liner that smooths airflow.
I have also been thinking about the $30 ultrasonic rangefinder that I got a while ago when I was musing upon alternative ways to measure airspeed. It occurred to me that it could also be used as a squat switch; the gear would not retract when the belly of the plane was, say, four feet or less from the ground. (You'd have to have an override switch, of course, in case it malfunctioned.) The problem for me is that this rangefinder is not a turnkey device; it requires one to supply a circuit to convert its output pulse duration, which is proportional to the time of travel of the sound from the emitter to the reflector and back, to a digital form. No doubt this interface presents no difficulty to the electronics hobbyist, but I am not he. I have to call the manufacturer and see whether he is willing to be helpful; some are, some aren't.
[January 21, 2012]
I posted an edited version of the flight test video here. The quality is not very good -- I need to get a newer spy camera -- but the general impressions are clear enough.
[January 20, 2012]
Yesterday I attached a little video camera to the left boarding step to find out how well my gear doors are closing. The last time I tried to do this, several years ago, the step strut vibrated so violently, and at just the right frequency, that the set screw holding the lens in the camera backed out and the lens disappeared shortly after takeoff. The strut is rectangular in section, and vibrations like that are usually due to vortices being shed from alternate sides in rapid succession. This time, I made an airfoil-shaped fairing around the strut with foam and aluminum tape. It still vibrated, but not to the point of dismantling the camera (for which I got a new lens). I was also interested in observing the behavior of the left main landing gear strut, since I have become convinced -- actually, it is obvious, now that the scales have fallen from my eyes -- that the "slumping strut" problem was not a slumping strut at all, but rather a sticking, and perhaps slightly overinflated, strut on the opposite side. The test consisted of a single flight around the pattern, with the downwind leg extended about three miles so that I could accelerate to cruising speed.
As far as the landing gear doors are concerned, the camera could see only the left and nose gear doors; I will have to put the camera on the other side to see the right doors. After retraction and during initial climb, the doors are not perfectly closed, but they are satisfactory; at 145 kias, which would be a typical indicated airspeed at cruise, they bulge out slightly. The worst gap, around 3/8 of an inch, is at the lower half of the outer door, which seems to flex outward. It is a simple 1/4-inch thick sandwich of carbon and glass; I could stiffen it with some simple ribs. I doubt that the drag penalty is very great, but I would like the doors to shut nicely for aesthetic reasons at the very least.
As for the strut, it was interesting to see that the left main seemed to remain somewhat overextended for a long time after touchdown. On seeing the tape, it struck me that this problem, which began to manifest itself about a year and a half ago, might be related to the flaps, which relieve the weight on the gear after landing. Furthermore, to reduce lift I usually move the stick forward once the nose gear has touched the ground; this, too, has the effect of lifting the tail and slightly relieving the main gear loads. I also am in the habit of braking rather hard, because I like to turn off at the taxiway that leads to my hangar and not have to back-taxi to it; and hard braking puts a load on the strut that increases friction and makes it move less freely. It seems as though the solution to this problem might be some combination of 1) carefully ensuring that the main struts are equally inflated; 2) retracting the flap during roll-out; 3) not braking harder than necessary; and 4) not pushing the stick forward during roll-out.
[January 14, 2012]
Jon Karkow pointed me to a Piper owners' forum where there was a discussion of slumping struts on Cherokees. So it turns out this problem is not confined to me. Participants gave various explanations, one suggesting that the problem is not the right strut collapsing, it's the left strut remaining excessively extended after landing because of "stiction" or starting friction (which is greater than sliding friction). So maybe I need to overhaul the left strut as well.
[January 11, 2012]
Shot a coupled ILS approach to Van Nuys; very calm day, and it worked nicely. Then I returned to Whiteman and landed, and to my amazement and very great disappointment as I turned left off the runway the right strut compressed in the same way as before I overhauled it. Complete bafflement.
[January 6, 2012]
With much spillage, since I did not have a proper funnel and was pouring from a 1-quart can into a 3/8-inch hole, I got the oleo filled to something like the proper height with hydraulic fluid and reinstalled it in the airplane. Now I just have to understand why having too much fluid and not enough air in it was having the observed effect. I cleaned and repacked the wheel bearings while I was at it. It's never clear to me why this is necessary; a car goes tens of thousands of miles between wheel bearing services; an airplane rolls only a few miles a year.
[January 5, 2012]
Nothing was wrong inside the oleo. The cause of the problem has to be an incorrect amount of hydraulic fluid. I moved the air valves when I modified the PA28R struts for Melmoth, and so can't use the Piper method for adding fluid, which involves overfilling and then compressing the strut to force excess fluid out the air valve. The problem is that without the air valve being in its original position, about two inches below the top of the cylinder, there is no convenient way to set the height of hydraulic fluid inside the strut. There is an inconvenient way; a 1/8" pipe thread plug in the top of the strut can be removed, and fluid sucked out through a straw, as it were, to the proper depth; or a special temrporary plug could be inserted with a tube extending two inches into the strut, and the strut filled, extended, and then re-compressed, forcing fluid out that tube and preserving the proper amount of air in the strut. Unfortunately, this top plug is inaccessible when the strut is in the wing. I guess I could drill a hole in the skin above the strut to get at it. Another possibility would be to take the air valve and insert a bent tube of the proper length with which to suck out excess fluid; but I'm not sure there is room inside the oleo to feed in a bent tube at that location. Another possibility would be measurement: determine the volume of hydraulic fluid required to fill the strut, and put in just that amount. That, however, would require completely emptying the strut to start with, and that can be done only by removing the piston from the cylinder -- possible, again, but not exactly convenient. Fortunately, the oleos hold air and fluid indefinitely, and so replenishment is a rare event. For the time being, I will do nothing, since with the strut out of the airplane I can remove the top plug and get the fluid level right.
[January 4, 2012]
I took the right main strut off the plane today to overhaul it and perhaps to discover the cause of its strange tendency to compress on turning left off the runway after landing and then gradually to re-extend while taxiing. The fluid was very dirty, but apart from that the condition of the inside of the oleo was unremarkable. There was some superficial corrosion on the unpainted, exposed top of the cylinder; not bad, considering that this strut was assembled more than 20 years ago. I'll clean it up and chromate or alodine the exposed parts before re-assembly. I bought two rebuild kits in order to motivate myself to overhaul the right strut as well, but I did partly dismantle it and replace a couple of O-rings just a few years ago and so I will probably end up stockpiling the rebuild kit until the right strut begins to act up.
[December 20, 2011]
For some time now I have not left the battery tenders continuously connected to the batteries, and the battery water level has stayed put, surpporting my suspicion that the water had been evaporating not because the batteries were too hot in flight, but because they were too warm during the much longer periods spent parked in the hangar. I have searched in vain on line for mention of battery tenders cooking away battery water (or of my specific type -- the brand name is Schumacher, I believe -- doing so) and have not found anything.
My hope of getting the intake manifold modification done during November was vain; the month came and went without much being accomplished, and now, in the most accomplishment-free month of the year, nothing will get done until January. I have been studying drawings of the engine and trying to figure how how best to route the 2-inch tubes running from the throttle body to the log manifolds. The problem is how to get around the oil filler neck on one side and the starter motor mounting flange on the other, while keeping the two branches mirror images of one another. No doubt there is an infinity of possible solutions, serpentine or tortuous in various degrees, but whatever combination of bends I come up with I have to be able to describe to the tube bender with a reasonable confidence of his producing usable parts.
Mike Melvill came down to have lunch with me and our friend Jerry Slocum, who was in LA for a few hours on his way back to Salt Lake from a pleasure cruise through the Panama Canal. (Jerry used to go with me in Melmoth 1, many a Wednesday during the late '70s and early '80s, to lunch with Burt Rutan and a few other friends at Reno's cafe at Mojave; he always ordered a patty melt.) Mike's Long-EZ is very well equipped, including WAAS and an Aspen PFD, and we talked about the extreme accuracy of GPS approaches, plus or minus half a meter, and how you could probably make a hard but non-damaging landing in zero-zero conditions, if you had to, hands off, using the coupled autopilot. (Airlines do this all the time; as Jerry pointed out, we have probably all ridden along during practice autoland landings without ever knowing it.) I suggested that the addition of a rangefinder from a camera could provide you with height information as you neared the runway, and you could even manage a flare of sorts. Actually, I think that perhaps modern cameras focus digitally, by looking for sharp edges, rather than by ultrasonic pinging; but our discussion reminded me of the ultrasonic rangefinder I bought a few months ago (for $30) when I was thinking about experimenting with it as a non-aerodynamic way of measuring airspeed. Unfortunately the thing came with no guidance whatever about how actually to use it; it was assumed that the sort of electronic hobbyist who would buy it would know what to do with it. Not me. And now, alas, Paul Lipps has died.
[December 9, 2011]
I made the gadget to turn the oxygen on and off. It pulls the 3/32 cable 2.25 inches, locks overcenter, and when unlatched it releases the cable and a spring closes the bottle valve. The reason for this arrangement, rather than a simple solenoid, was concern that the rapid, powerful action of a solenoid might eventually damage the valve seat. The handle is on the left sidewall, by the pilot's seat.
The outlets (there are just two) are between the front and rear seats, on the centerline.
Today I sawed off the leaking fitting (called a "cone") on the 3/16-inch ox line from the bottle to the manifold (visible here) and spent a couple of hours struggling to put on a new one. I tried silver solder, then regular solder, and finally called my friend Homer Knapp, who was stuck in traffic somewhere in Westwood but remained on the phone (it's illegal to use a cell phone while driving here) long enough to tell me that I needed to get some white paste flux at a welding supply store. You'd think I would know stuff like that, but no. Airplanes don't call for a lot of silver soldering or brazing. It was 4:45, getting dark, but there's a welding supply store across the road from the airport (it's where I get my "aviator's breathing oxygen" at a deep discount) and I got some there. It worked like a charm. Actually, super glue would probably have been good enough; the force trying to separate the fitting from the copper line at 2,000 psi is about 81 pounds. Anyway, I'll re-install that on Monday and then the oxygen system will be well and truly done.
The next step will be to determine whether the unpressurized Bendix mags will work at 17,500 feet -- they will probably start arcing -- and then to decide whether to get pressurization kits for them or to install my pressurized Slicks instead.
[November 21, 2011]
I collected some data on speeds and fuel flows at very low power settings. At a density altitude of 7,000 feet and a weight of around 2,000 pounds, I set the rpm at 1,800 and did a sweep of manifold pressures from 17 to 25 in. Hg. with extremely lean mixtures. Below 24 in. Hg there was very little variation. At 17/1800 IAS was 90 kt for a TAS of 100.5 and fuel flow of 3.65 gph. The increase in fuel flow was more or less linear with manifold pressure up to 24 inches and 4.9 gph, where the TAS was 128 kt. Nmpg fluctuated randomly between 26 and 27, reflecting both the flatness of the mileage curve at low speeds and the difficulty of getting precise measurements. Above 5 gph the curve becomes steeper, in part because you have to increase rpm; 28/2300 gives 150 kias, 167 ktas, and 8.8 gph (18.9 nmpg).
[November 19, 2011]
The oxygen system is now working. It took me a while just to decide where to put the pressure gauge (it's in the floor between the seats, alongside the outlets), how to route the 1/8-inch aluminum line connecting it to the bottle, and where to put the pilot's end of the cord that turns the bottle valve on and off. As far as the cord was concerned, I was originally planning to put it with the outlets and the gauge. That would have involved several bends and two or three pulleys. I then experimented with various tortuous paths up the left sidewall before discovering that there is a perfectly straight line from the pulley at the bottle (see picture below) to a point on the left sidewall beside the pilot; it requires no pulleys, interferes with nothing, and is hidden by the existing armrests. Now I have to decide whether I should just put a loop in the end of the cord and bond some sort of miniature coathook to the sidewall, or whether I should go to the trouble of making an overcenter lever to turn the oxygen on and off. I will almost certainly do the latter -- eventually. The plumbing uses a mix of flare and compression fittings and a third type, whose name I don't know, that consists of a hemispherical male element brazed or silver-soldered to a copper or steel tube and a bowl-shaped female receptacle. I first tried flares on the 1/8-inch 3003 aluminum tube; they leaked at both ends. I replaced one with a brass compression fitting; it worked fine on the first try. I wanted to replace the other flare with a similar fitting, but couldn't find one; but I eventually got the flare to seal. Now the only leak, and it is very slow, is at the brazed fitting on the short 1/4-inch copper tube between the bottle and the manifold, visible in the picture below. The male fitting is visibly deformed; I need to remove it and braze on a new one.
The choice of aluminum for the pressure-gauge line was based on weight; copper or steel would be more conventional. The tubing has a wall thickness of .025 in. It is officially rated for pressures up to 2,300 psi, but the tensile strength of 3003-O aluminum is 16,000 psi. Since the bore (0.075 in.) is 1.5 times the total wall (0.025 + 0.025), the tensile stress at the maximum bottle pressure of 2,000 psi is 3,000 psi and the margin of safety is over 5. I think that the reason harder metals are usually used is to resist wear and tear; the aluminum tube does look pretty easy to damage. It is in a protected location, however, and I think I will be able to avoid dinging it. Time will tell.
[November 7, 2011]
Today I flew around for half an hour at 5,000 feet with the engine cranked back to 24/1900, which yielded 5.4 gph or about 30% power. This gave a true airspeed of 130 knots and a specific range (ie gas mileage) of 24 nmpg (around 27.7 smpg). It seems that the airplane falls short of its computed performance at high power, but exceeds it at low. This suggests that the value of e, which is essentially a way of saying what the effective aspect ratio of the wing is, is higher than the computer makes it. In other words, parasite drag is higher than the computer thinks, and induced drag is lower. But it could also mean that the engine's specific fuel consumption (pounds of fuel per horsepower per hour) at low power settings is lower than the computer thinks, or for that matter that the fuel flow instrumentation is not accurate and its errors are non-linear.
The conventional wisdom is that the real best-range speed tends to be higher than the theoretical one because engines are inefficient at low power settings. The next time I fly without a destination, I'll see if I can generate an empirical specific-range curve.
I have been working a couple of hours a day on a system for turning the oxygen on and off from the pilot's seat. The oxygen bottle is in the baggage compartment, wedged under the rear seat footrest (the rear seats face aft). Here is the apparatus, temporarily mocked up with some random twine and fittings.
The fine safety wire securing the pulley is actually not a mockup. It is the final arrangement, and is simply the lightest way I could think of to hold the pulley. It is anchored with a stainless steel cotter key whose legs have been bent outward and trapped under a phenolic disk bonded to the inner skin of the fuselage. I guess I am trying to save a gram here and there to make up for the weight of the oxygen bottle. One oddity is that the bellcrank that operates the bottle's on-off valve has to be at a certain angle, which ends up clocking the bottle so that its built-in pressure gauge faces the floor. I will have to glue a small mirror to the floor to read it. There will, however, be a second gauge in the cabin that the pilot can see.
[October 29, 2011]
The lubrication of the pitch trim mechanism on the 4th was miraculously effective. I have still not flown high enough, nor in cold enough weather, to know whether this new lubricant (which my old friend and onetime Flying Magazine editor Stephan Wilkinson, a former car buff who would get waxes and greases for his yellow Porsche from Germany, recommended and in fact caused to be shipped to me) will stiffen up unacceptably like the last one I tried. Perhaps not; when I put it into the freezer it got somewhat stiffer, but not excessively so. Anyway, now the operation of the trim is positively silky; I feel like changing speed just for an opportunity to use it.
As a first tiny step in the project of reversing the intake manifold, I rotated the vacuum pump 90 degrees in order that its outlet not interfere with the throttle body, which will be above it. I think I will do the manifold modification during November, which is when I have to do my annual inspection anyway.
Yesterday I flew around for 40 minutes just to exercise the plane a bit. When I do this I run about 25 in. Hg and 2,000 rpm with a fuel flow of 6.5 gph at about 5,000 feet d.a. I noticed that my airspeed was 20 times the fuel flow. This puzzled me at first, since that is also the case at my usual cruising setup (170 knots at 8.5 gph) and it ought not to be true at two widely different speeds. It later dawned on me that one (the faster) is true airspeed and the other is indicated. So, in car-compatible terms, it's actually 23 mpg at 195 mph and 25 mpg at 160 mph -- just like our 1986 Camry, but faster.
[October 6, 2011]
I need to remind myself, whenever I'm dreaming up exotic theories to account for electrical malfunctions, to repeat several times, "Bad ground." After taking lots of measurements, all of which checked out fine, I discovered that the fuel gauges worked when I held the piece of the panel that contains them in my hand, but stopped working when I put it back into the airplane. It turned out that moving the wire loom made the problem appear and disappear. Since it affected both gauges equally, it had to be a ground issue -- I believe that is the only wire they have in common. I didn't find the bad connection, but with a couple of tiewraps I stabilized the loom so that the problem went away. There are some malfunctions -- such as the weird noise our dryer is currently making -- that are very difficult to diagnose, but become easy once the failure is complete. I will wait for the fuel gauges (and the dryer) to fail completely.
A huge bubble turned up in the #2 flap actuator circuit yesterday, fortunately on the ground. It may have had some connection with my overhauling the #2 master cylinder in August; why it waited this long to announce itself, I can't say. The hydraulic flap actuation system has been by far the most troublesome thing on the airplane, and I still don't understand some of the things it does. Most of the time it works just fine, but it continues to be plagued with minor leaks and occasional major misbehaviors. Not ready for certification.
[October 4, 2011]
My theory that the high breakout friction in the pitch trim circuit was due to thrust on the jackscrew bushing proved to be incorrect. It was just general dirt and lack of lubrication. I had removed all lubricants a while ago, thinking that they were stiffening up at high altitude and low temperature and making the trim hard to operate. This time I tried a new type of lubricant. I then brought the trim mechanism, which I had removed from the airplane, home and put it in the freezer for a few hours. It was stiffer, but still worked smoothly. So in the end I lubricated everything and put it back together. It feels nice now, but I haven't tried it in flight yet. Another theory of mine, that the weird behavior of my fuel gauges was due to failure of some zener diodes in an interfacing circuit board, also bit the dust. I got the circuit board out and tested the diodes, and they all seemed to be regulating to 7.15 volts, just as they're supposed to do.
[October 1, 2011]
On Wednesday I flew to Santa Rosa to have a look at the participants in the NASA/Google/CAFE Green Flight Challenge. Prizes totaling more than 1.6 million dollars are offered for the most efficient airplane, the minimum standard being 200 passenger-miles per gallon over 200 miles in two hours or less. This is not a very demanding standard if no constraint is placed upon wingspan. Heck, Melmoth 2 with four aboard already gets 100 passenger miles per gallon, and it's optimized for speed, not efficiency. Participation was limited to 18 entrants, but in the event only four were ready. One of these, a powered sailplane modified by Embry-Riddle with a 75-foot-wing and a supplemental electric motor, was disqualified because the university refused to insure its participation in what passed for an "air race." Fallout from Reno. A two-seat Phoenix motorglider of 44-foot span had no realistic chance against the other two, both pure-electric designs of extremely long span and high aspect ratio. So in effect there were only two contestants. The larger of these, the Pipistrel Taurus G4, consisted of two two-seat Taurus sailplanes joined, Twin Mustang fashion, to a centersection carrying half a ton of batteries and a 195-hp electric motor. Here it is in flight:
I am inclined to think it will win, simply by dint of having four seats, not that a wingspan of nearly 70 feet hurts. As was the case in the old CAFE races, unreasonable emphasis is placed by the scoring formula on passenger capacity, even though private airplanes seldom fly with all seats full. Peter Lert, who with Gene Sheehan won the first CAFE race in a Quickie Q2, is fond of pointing out that an even better score could have been achieved by a full DC-3, and meals could have been included. The only registered entrant with more than four seats was the bio-diesel powered Synergy, but I doubt that the claims made for its very complicated arrangement of flying surfaces would have been borne out in practice. In any case, it didn't show up. What this contest is going to demonstrate, apart from the fact that most people can't finish a job in time even for a million bucks, is that 200-pmpg airplanes can't fit in taxiways, hangars or tiedowns.
Winners will be announced on Monday.
No trip would be complete without one or two things going wrong. I observed that there is a slow fuel leak where the left outboard flap track bolts to a rib. That should be easy to fix. The fuel gauges, all four of them, have stopped working, and now indicate full at all times. This has to be a problem with the circuit board that provides an interface between the float-type senders and the edgewise voltmeters that I use as gauges. Finally, there is unacceptable breakout friction in the pitch trim circuit at cruising speed. This is nothing new, but I am finally going to try to do something about it. I think it will require replacing the bronze bushing that currently serves as a thrust bearing for the trim jackscrew with a ball bearing.
[September 25, 2011]
After two and a half years or so, a buyer appeared for Ray Henning's beautiful T-18. Ray came down from Seattle for the handover, and I flew up to Tehachapi to see him. It was overcast in the Basin, and I had to hold for about half an hour waiting for a clearance to VFR on top from Burbank. The #3 (center right) CHT went to the top of the green. This is a problem: at the start of the takeoff roll, power is high but speed is low, and so CHTs rise rapidly. If a cylinder is already at the top of the green, it's going to climb out of the green before its temperature begins to drop again. I could not detect any difference in the engine after this episode, so I suppose it did no damage, but an airplane, like a car, ought to be able to idle indefinitely. I am hoping that my scheme of reversing the intake manifold will improve airflow through the cowling by removing the portion of the intake manifold that obstructs the exits. It should also eliminate the problem of rough idling after long holds, which is due to the throttle body, which is the only portion of the fuel system still on the hot side of the baffles, becoming heat-soaked.
[September 21, 2011]
Some friends brought their children over to the hangar to show them the plane. The cockpit miraculously survived having a couple of 6-year-olds sit in it for a few minutes. I then flew around the pattern to show them what it looked like in the air. I offered to take someone along with me, but all declined. The phrase "fiery crash" was uttered several times. Nevertheless, the 3-minute flight was without incident.
[September 19, 2011]
Nancy and I went to Cape Cod on August 26 and returned this last weekend. Melmoth stayed behind, so there has been nothing to report. Before we left, however, I did overhaul the #2 flap master cylinder. My impression that it was leaking through the hollow piston shaft proved to be wrong. I could not find an obvious leak, but I suspected that an insufficiently chamfered hole near the end of the shaft, where a clevis pin passes through it, may have damaged the small (3/8" I.D.) O-ring during assembly. I enlarged the chamfer and polished it vigorously, and also polished out some small scratches and dings in the piston shaft that I had evidently overlooked (or considered inconsequential) when I first installed the system. I did fly the day before we left, and the cylinder seemed no longer to be leaking. But it is too early to be sure.
There was a leak in the static plumbing after I modified it. I eventually located and repaired it, and also added a drainable trap just forward of the right static port. At present it ends with a flare cap, but I should probably replace that with a quick-drain.
I spent a good deal of idle beach time at the Cape face-down in the sand, thinking about reversing the intake manifold. I am determined to do it, even though I suspect that it may turn out to be one of those big modifications that yield no detectable benefit.
[August 17, 2011]
Something worth noticing in the photograph below is that the ridge on the back of the static port is above center. This is not just sloppy work. The hole on the other side is in the center of the disk, but it is drilled at an angle -- all part of my apparently doomed effort to keep water from getting into the static plumbing.
I tried wrapping the #1 cylinder exhaust with the thought that the insulation might keep heated air from entering the baffles. It seemed to have no effect at all. In fact, since the pipe and the head are in intimate contact, I'm not sure that making the pipe hotter is the best way to make the head cooler. I observed that the #3 cylinder is only 10 degrees C. below the #1 -- but 25 to 35 above the others -- so maybe the problem, if it really is a problem, is not related to the rearmost cylinder's baffle. This is all really academic; all temperatures are well within the green. I would just like it if they were all the same.
I decided to get serious about the hydraulic leaks in the flap synchronizer. It's not possible to properly simulate air loads on the flap while on the ground, so I took out the floor panel that normally covers the synchronizer and watched the cylinders as I cycled the flaps in flight. The first leak I found was in the #2 master cylinder; fluid seems to be seeping out through the hollow stainless steel piston shaft. That should be easy to fix by simply pressing in an aluminum plug.
One chronic annoyance has been the proneness of the static system to take on water while parked during heavy rain. I'm surprised this can happen, since the ports are so tiny and are on essentially vertical surfaces, but anyway, it happens, and happened again at Oshkosh, where it was apparent to me as I took off that I was not getting a reliable airspeed indication. On the assumption that the basic problem was that I had thoughtlessly put a downhill segment of static tube from the right-hand port, I revised the plumbing thus:
The picture shows the inside of the right-hand wall of the baggage compartment. The tubing is 3/16-inch aluminum; the joints are made by sliding a 1/4-inch o.d. sleeve over them and sealing with JB Weld. The static port is the round thing; it's about the size of a quarter.
After buying a new alternator for more than $600 a couple of weeks ago, today I found a spare alternator in my hangar -- in the box where I stored it 30 years ago.
[August 7, 2011]
In mid-July I had a visit from Francois Besse, the editor of the French magazine Piloter. We had a brief flight -- the intention was to go to Santa Paula for lunch, but we turned back when I saw that the alternator was not charging -- at the end of which he took this nice picture on short final at Whiteman.
He complained about the reflection in the windshield of the gray area above the panel. I guess he has a point. The ceiling speaker has been derided as a quaint anachronism. Indeed, I have never used it.
[August 1, 2011]
I always feel some anxiety before leaving on a long trip, not because of the dangers of flying, but because I worry that something on the airplane will break in some godforsaken place and I will spend days in a state of intense impatience and boredom getting it fixed, while having to eat at restaurants that serve you too much meat and potatoes but no vegetables. Is this some new culinary fashion in the central United States, intended, perhaps, to hasten the general trend toward grotesque obesity? Worse, this dismal experience would cost a lot of money.
Luckily, none of that came to pass. The plane did fine, except for some flaky behavior on the part of my main gear struts, which don't seem to want to stay equally inflated. I really need to overhaul them -- not a difficult job: just disassemble, replace O-rings and reassemble. The engine used one quart of oil in 20 hours, and the oil mist on the windshield ceased toward the end of the trip, making me think that when it's comparatively heavy it's because the plane has been sitting and what's ending up on the windshield is the accumulated drips of several days. And the final version of the pilot's seat was comfortable for long flights. So that was all good.
Oddly, when we flew to Japan, Europe and Chile in the old Melmoth, I never worried about anything breaking. Youth!
There were some minor glitches. The halogen flashers are working fine, but I don't dare use them on the ground because they seem to overheat the lenses. The right nav light bulb burned out. The static source was briefly unreliable after heavy rain; I need to reroute the lines to eliminate a downhill segment immediately adjacent to the starboard port (though it seems amazing that any water at all can get into those tiny holes). I suspect that the air inlet that I added to the right lower cowling to cool the battery box -- it looks like a little machine gun port -- is actually behaving as an outlet, because the ram pressure in the cowling is higher than the pressure at the inlet face, which is down in the boundary layer. I intend to eliminate that inlet and take in battery cooling air directly from the lower plenum.
I am puzzled that while with the old voltage regulator the ammeter would indicate zero once the battery was recharged after startup, with the new one it seems to indicate around +5 amps all the time. The ammeter is wired to show charging current, not bus load, so this is unexpected. It could be that it is happening because the old regulator was set for 27 volts and this one is set for 28, and the Yuasa motorcycle batteries somehow prefer a slightly lower voltage. I struggled with this problem years ago and resolved it by adjusting the system voltage downward from 28 volts; I guess I just need to do the same again.
As was the case last year, I enjoyed tailwinds eastbound and part of the return trip, and when there were headwinds -- in Wisconsin and Iowa on Saturday -- they were mild. I had to work around some big thunderstorms near Las Vegas, New Mexico, but generally didn't need to deviate much from the GPS-coupled straight line. True airspeeds conformed closely to the Melmoth 2 Rule: 20 knots per gallon per hour. I generally cruised at around 8.5 gph and 170 ktas. Early in the trip I flew a long stretch at 15,500 and found that I could maintain good oxygen saturation -- around 93 or 94% -- with the Nelson meter just barely cracked, indicating well below 1 liter per minute.
[July 31, 2011]
The new alternator and regulator having been installed, I left for Oshkosh on the 26th, a day later than planned. I refueled in Salina, Kansas after a 6+15 flight, and continued to Prairie du Chien, at the confluence of the Wisconsin and Mississippi rivers, where I RON'd. I scud-ran in marginal 1,000-and-1 conditions into OSH the next morning. I left Saturday before noon, got fuel at Prairie du Chien (I was too impatient to wait for the OSH fuel truck, even though their gas was way cheaper, and the people at PDC were nice) and flew another 6+15 leg to Gallup, NM, where I slept. Airborne at the crack of dawn, I made it almost into LA before encountering, just west of Palmdale, rain so heavy that it took the paint off the leading edges of my empennage. About 20 hours for the round trip, and almost $1,200 worth of fuel. This can't go on much longer.
[July 22, 2011]
The full field test, which consisted of disconnecting the regulator and jumping the alternator output to the field post, so that the alternator simply bootstrapped without regulation, produced no charging voltage. I removed the alternator again -- now that I knew how to do it, it took only ten minutes and drew no blood -- and opened it up. I found much of the stator winding blackened from excessive heat.
It is still not clear to me what exactly had failed, but the thing looked ugly enough that it seemed best to retire it and get a new one. It had, after all, lasted for about 1,500 hours of flying over a period of 34 years. What I think produced the heat damage was not the first thousand hours of its life in Melmoth 1. There it was cooled with a blast tube. In Melmoth 2, reasoning that it was now on the cold side of the baffles, I omitted any provision for active cooling. I should have provided it with a reverse blast tube -- that is, a vent to the low-pressure side of the baffles. The current version has a built-in fan; no blast tube is required to make air flow through it.
Mark, the foreman at Able Air, tried to locate a replacement, but the only one we could come up with was at Aero Accessories in Van Nuys, and the owner there had taken the day off and would not be back until Monday. My big worry now is that the new alternator will prove to be incompatible with the regulator I just bought. After that, I believe I will have run out of things to go wrong.
[July 21, 2011]
Quel mess. I installed the Cessna regulator -- this involved quite a lot of new wiring -- and then proceeded to damage it by stupidly attaching a ground lead to what I believed was a ground post, but was really A+. Melted some perfectly good wire. I thought I had damaged the alternator too, so I took it off -- a hideous job, even though there are only three bolts; they are in the most inaccessible locations imaginable -- and took it over to an aircraft accessory overhaul shop at Van Nuys. The guy put it on his testing machine and said it was OK, although the Woodruff key in the drive gear needed to be replaced. This he did, for a modest $20. I learned that my alternator, which I have had for around 35 years, is obsolete and no longer supported, so if it's dead I have to get a replacement. Since I do not have a core to trade for it, this could turn out to be pretty expensive.
I put the alternator back on the plane -- an even worse torment than taking it off, almost two hours, with considerable bloodshed -- and ordered a B&C regulator, which came this morning. Parenthetically, I love the amazing promptness with which stuff you order on line is delivered. This regulator had a completely different wiring hookup from either of the previous ones, plus a different mounting bolt pattern. I spent this afternoon hooking it up temporarily, only to see no charge. Tomorrow I have to do a "full field" test, which involves bypassing the regulator and letting the alternator self-regulate in response to changing rpm. There is a lot of advice on line about troubleshooting charging systems, and my system has so for been more or less within limits, except when it comes to actually putting out some voltage. Quite a puzzle.
[July 14, 2011]
On this moderately happy Bastille Day I found in one of the midden heaps in my hangar a Cessna voltage regulator.
Its wires outnumber the ones on my present regulator by three, and I do not have the pinout for it, but a local FBO offered to let me look through his old maintenance manuals to figure it out. He said this unit contains an overvoltage relay, overvoltage warning light circuitry, etc., so that is what the other wires are about. Naturally it does not have the same footprint or attachment hole spacing as the old Motorola one, but I can work around that. Of course, for all I know it is burned out or soon will be. The Motorola lasted 38 years and 2,500 hours -- not bad for a cheap non-aircraft-quality part.
Russ Hardwick, with whom I had lunch today, brought me a couple of very bright LEDs, three or four of which, in series, would do nicely for panel lights, running on the 12-volt bus, which consists of the 1-amp output from an ancient Narco voltage reducer. At present I think the only load on it is the GPS. Russ seemed to think that if I wanted more 12-volt current I could tap 12 volts off the middle of my pair of batteries; he suspected that batteries work on Communist principles: from each according to his ability, to each according to his need. That might work for batteries; it certainly wouldn't for people. At any rate, the LEDs draw almost no current, so I think the Narco will handle them fine.
[July 13, 2011]
Took off for Santa Paula with Francois Besse, the visiting editor of a French aviation magazine. We hadn't gotten very far when I noticed that the alternator was not charging, and we turned back. After some troubleshooting I concluded that the voltage regulator had failed. It is a little Motorola unit that I believe was used on some trucks that have 24-volt electrical systems. I must have gotten it almost 40 years ago. Online I found physically similar ones on offer from a Chinese firm, but only if I wanted to buy 500 or more. It looks as if I may have to get a different regulator and rig up a new mount for it. Spruce has a couple that incorporate overvoltage protection, something neither Melmoth has ever had.
[July 12, 2011]
The countdown to departure for Oshkosh has begun. Or, to put it a little less portentously, I started doing a lot of deferred maintenance. I installed the small SkyTec starter, which is not that small, or light, any more, but which will clear the intake manifold when I turn the latter around. I greased the landing gear retraction joints. I found and fixed a loose Cannon plug on the oil temperature sensor; it was probably responsible for the fluctuating oil temperatures I've been seeing lately. (Fluctuating oil pressure can be a dire symptom, but fluctuating temperature is almost certainly an instrumentation problem.) I continued my still unsuccessful search for the source of a pretty sizeable hydraulic fluid leak at the right outboard actuator. I replenished the hydraulic fluid reservoir, which was significantly depleted after just ten hours of flying. There are still leaks in several places. I cleaned the windshield, which had more oil spray than usual on it, and carefully inspected the engine without finding any new oil leaks. The oil on the windshield is a nuisance, but it is actually not very much oil, since the engine is still going 15 hours or so on a quart. I now need to put the plane on jacks, swing the gear, make sure all the doors are closing properly, and regrease the wheel bearings. It's pretty clear that I won't have the remote control for the oxygen bottle valve, or the remote oxygen pressure indicator, installed before I go, because I have other things to do than work on the plane. But at least I will have oxygen.
[July 2, 2011]
A correspondent, Ryan Niederkohr, explained the apparent inconsistencies in the results of my oxygen experiments of last week. Oxygen can be dissolved in blood without being bound to hemoglobin. The "oxygen saturation" measured by the fingertip oximeter is the amount of bound oxygen in the blood; obviously, once 100% of hemoglobin molecules are carrying their baggage of oxygen, there's no room for more. But there can be extra free oxygen just floating around in the blood if you have been breathing an oxygen-rich mixture, and as hemoglobin discharges its cargo more oxygen is present to bond to it. Therefore the decline in saturation percentage does not necessarily keep pace with change in altitude or in liters-per-minute delivered from the oxygen bottle. As Niederkohr explained, I would have seen more linear results if I had started from a minimum oxygen flow rate and worked upward.
Because my planned re-orientation of the intake manifold was going to encounter interference from the full-size starter motor that is currently on the engine, I got over my annoyance with Sky-Tec and returned my old small starter, together with a gift of $250, in exchange for a new small starter. I requested the same model, but somebody called me up from the factory and strongly suggested that I get the -5 rather than the -3 model, because that is what they recommend for the "larger" Continental engines. I think of my 360 cu. in. engine as one of the smaller Continentals, or at most as a medium-sized one, but I went for the -5 even though it weighs three pounds more than the -3. One advantage it has -- I think -- is that the -5 has a solenoid-operated electric clutch; the -3 has a centrifugal clutch. Now, the engine itself has a starter clutch consisting of a coil string that tightens around a shaft when torqued by the starter. In theory -- this must have been the theory that led the Sky-Tec people to design the original starter without a freewheeling mechanism -- the coil spring would completely disengage the engine from the starter, which did not want to rotate at all when it was not energized. But it turned out that the spring clutch would drag slightly, and tighten, and drag some more, until the whole assembly wore out and had to be replaced at a cost of over $800. For some reason I feel as if the solenoid clutch is more likely to resolve this problem completely than a centrifugal clutch is.
[June 24, 2011]
The oxygen system worked, but I can't make much sense of the pulse oximeter readings. I climbed to 12,500 feet and checked saturation; it was 83-86 (it tends to jump around a bit) and pulse was 106. (My resting pulse is usually around 60-65, but when oxygen is in short supply your pulse goes up.) I then put on the oxygen mask (which seems to be as good as new despite being more than 30 years old, but I haven't checked the built-in mic yet) and set 1.5 liters per minute on the flowmeter. Saturation percentage (hereinafter Sp) immediately went to 98 and pulse to 99. I kept reducing the flow rate with the following results (the first item is flow rate in liters per minute, the second Sp, the third pulse rate):
1.25:
98-99 / 90-92
1.00: 98 / 88-92
0.75: 96 / 90
So far so good. But this is where it gets weird. The flowmeter actually isn't marked below 1.0, but I thought I could extrapolate where 0.75 probably is. If I kept turning the knob the little ball became still. So maybe that's zero. But zero is about as far below 1.0 as 1.5 is above it, so maybe the thing is nonlinear at low flow rates, and that's probably why it isn't marked below 1.0.
With the knob screwed in all the way and the ball dead, I get 92-93 / 92-93. Then I disconnect the mask from the oxygen supply, and it goes to 90-91 / 91-94. So it looks as if oxygen remains bound to the blood for some time, because this is the same amount of oxygen as gave 83-86 / 106 before. Finally I connected the mask again and just cracked the valve, so that the ball gave a tiny movement: now I got 92-93 / 93.
I tentatively concluded that it's possible that the valve on the flowmeter doesn't close entirely. It would be interesting to know, if this is the case, what the flow rate is when the valve is ostensibly closed. Anyway, all this is of somewhat academic interest, since the value would be different higher up and in any case I would be adjusting the flow to get an Sp of 90 or so, which corresponds to about 9,000 feet without oxygen. I think I will repeat the whole experiment, but rather than start with 1.5 lpm and work down, I'll start with the valve closed and work upward; that will eliminate any lag effect, and will also make clear whether there is any difference between no oxygen at all and a closed valve on the flowmeter. I will also go to a higher altitude.
The flight, which was to Paso Robles, about 140 nm, took 1.1 hours up and an hour back, and used a total of 16.4 gallons of fuel.
Today I found that the battery water was down, just on the battery closer to the positive pole; so, as planned, I swapped the position of the batteries to see whether the excessive evaporation is due to the battery itself or to the battery tender that I use on the ground.
[June 22, 2011]
The oxygen bottle is now locked down and connected in a half-baked way to the regulator and outlets. I'm making a round trip of a few hundred miles tomorrow; I'm curious to see how my blood oxygen saturation responds to various rates of oxygen flow. Also whether the microphone in my oxygen mask still works after all these years. I probably last used that mask in 1982.
[June 14, 2011]
There is something about the arrival of summer that slows me to a crawl. The first heat is enervating; later I get used to it, and am probably less bothered by August and September than a lot of other people are. At any rate, I have accomplished almost nothing in the past three weeks, even though, after a few hot days, the weather had actually turned rather chilly and I was discouraged from going to the annual barbecue at Antique Aero in Paso Robles by rain, of all things. Not quite nothing, however. I have replaced the knob on the oxygen bottle valve with a lever and spring arrangement that will allow me to open it by pulling on a cord. It will require some sort of hook to hold the cord against the spring while the bottle is in use; when the cord is released, the spring closes the bottle. It seems to work satisfactorily on the bench, at least. I still have to figure out how I'm going to hold the ox bottle in place, but that shouldn't be difficult; there's a natural cradle for it under the rear seat footrest.
[May 25, 2011]
Further study of the problem of reversing the intake manifold has led me to think that it can be done after all by sawing up the existing manifold and ducting and welding it back together differently. The throttle body would end up right above the vacuum pump, which is okay, and the manifold would clear the oil filler neck on the left side of the engine. On the right side the old starter motor still creates a slight interference; I guess I will have to bend over and pay SkyTec for a new small starter that does not suffer from the same design fault as the one I currently have lying on the floor, where I wish I had left it when I first got it.
As for the matter of opening and closing the needle valve on the oxygen bottle by remote control, several suggestions have been offered, of which the most useful was to use an automotive speedometer cable with a small jackscrew. Jackscrews sound complicated, but are actually very easy to make with a bit of threaded rod or a sawn-off bolt. In the meantime my thinking had drifted to the minimalist solution of a piece of cord pulling the valve open and a spring pulling it shut. The current handle on the valve would of course be replaced with an arm a couple of inches long to provide some leverage and length of travel. As I mentioned a few days ago, the valve does not need to turn many times; somewhere between 45 and 90 degrees of rotation would be sufficient.
Since I have been thinking quite a bit about cooling issues, I got out my charts of delta p vs cooling air mass flow -- this is an item that manufacturers provide to OEMs -- and did a curve fit to the data. For what it's worth, the cooling air flow for my engine, in pounds per second, is 1.031 times the 0.541 power of delta p, the pressure drop across the engine expressed in inches of water. For cubic feet per second, replace 1.031 with 12.13 and divide by the density ratio. This is just part of what you need to know about cooling, unfortunately; other curves, which I have not yet modeled, relate delta p to power setting, ambient temperature, and cylinder head temperature. Ultimately, these calculations drive the size of inlets and outlets. I think, however, that inlet size, in particular, receives too much attention. People are very proud of having teeny-weeny round inlets. But you can't cram more air into an inlet than can find a way to get out. It is outlet size that controls the total mass flow, along with the impedance of the engine itself. Air finds its way around an oversized inlet, provided that it is well shaped, without a lot of trouble.
[May 20, 2011]
Since I am not one of those who believe that time ends tomorrow and am not a candidate for rapture in any case, I have been thinking about various things to do next. A couple of tasks remain unfinished: the oxygen system is hanging fire until I decide how I am going to open and shut the needle valve on the bottle, and I still need to install panel lights to complete the provisions for night flying. Actually, most people would consider night flying equipment to be incomplete until a landing light is added, so I guess I'm still far off. I don't fly at night any more, however, so none of this seems very urgent.
On the other hand, I do fly at high altitudes, and so the oxygen seems more useful. Yesterday Russ Hardwick and I discussed how to open and close the oxygen bottle by remote control. I was thinking about a torque tube; he suggested solenoids. A few minutes later he retracted the solenoid suggestion because it would shut the needle valve too violently and eventually damage it. I'm not sure that objection could not be dealt with by inserting a spring between the solenoid and the valve handle. He thought it would be best to use something that gave feedback, and proposed a hydraulic circuit; I made a counteroffer of a cable loop, but then raised him with a worm gear and sector driven by a small electric motor. It too would require some sort of spring or other cushion to avoid damaging the needle valve. Obviously, the options are impractically many. One of the desiderata is ease of removing the bottle; this is what inclined me to some sort of electrical solution. In any case I am indebted to Russ for pointing out that it is not necessary to turn the needle valve very far to provide the needed flow of oxygen. 45 degrees is plenty.
While I was mulling over all these choices, I also began thinking again about reversing the intake manifold in order to put the throttle body behind the engine, in the cool air side of the cowling, and to eliminate the transverse 2-inch tubes that currently impede air flowing out of the cooling air outlets. Today I uncowled the engine and studied the various interferences that I would encounter. I came to the conclusion that it would not be possible to simply make two saw cuts, flip something over, and come out with a workable reversed manifold. The oil filler neck gets in the way on one side and the starter motor mounting on the other. The oil filter, in its new position high on the firewall, is also a problem, and complicates running a pipe from the turbocharger to the throttle body. It appears that the best way to solve all of the problems will be to mount the throttle body wherever I want it to be, and then to bend and weld tubing as needed to connect it to the manifold and the turbocharger.
[May 9, 2011]
On Saturday I flew up to Pine Mountain Lake (Groveland), which is in the Sierra foothills on roughly the latitude of San Francisco, to present a little slide show about Melmoth 1 to the pilots' association there. My host overnight was Wayne Handley, a remarkable acrobatic pilot who is currently the president of the association. Wayne took me over to see Clay Lacy, whom I knew years ago at Van Nuys, having gotten my Learjet rating at his place. This turned out to be quite a stroll down memory lane. When we found him he was driving a 1955 Chevy Bel Air, turquoise and white, identical to my mother's car when I was an early teen. Clay's has 28,000 original miles, and looks it. In his hangar -- everybody there seemed to have a hangar -- was a Linn Midget Mustang that had belonged to the father of Clay's lady friend. That was an airplane that had impressed me quite a bit when I first saw it in Jane's in 1962, but I had never seen one in real life. Powered by a 125-hp converted GPU, it was quite fast, but I don't know how it managed to land; its tailwheel is about two inches in diameter, and its reported landing speed was 80 mph. That works out to over 13,000 rpm. Span is 16 feet. Not a lot of room inside for folding and unfolding WAC charts, or even arms.
The next morning the clouds were almost on the deck; I filed IFR back down to LA, flew the ILS at Van Nuys and broke off under the overcast to go to Whiteman. The makeshift GPS/VOR tracking system worked nicely, slaving to the old Lowrance GPS, either VOR or the ILS, or holding heading, as needed. You can do a lot with a wing leveler and one of these things.
Performance for the trip continued to be 170 ktas at 8.5 gph, which implies an F of 2.35 rather than the 2.25 I calculated a while ago. Ravages of time.
Today I was buying some more hydraulic fluid -- I still leak quite a bit of it -- when the radio shop guy walked by. I asked him about the PTT switch problem, and he suggested that it might be low voltage failing to operate a relay in the radio -- old radios, like my Collins MicroLine ones, had relays in the PTT circuit. That makes perfect sense. Next time, he said, try raising the rpm a little.
[May 4, 2011]
I had lunch at Camarillo with Javier Arango to discuss his collection of World War One airplanes, about which I am doing an article for Air & Space magazine. On starting up, I found that the press-to-talk switch on the radio would not work. This has happened a couple of times before, always after startup, and always it has resolved itself spontaneously after some time passed. This time I had to call the tower by cell phone to get a takeoff clearance. That worked fine, but when I was departing downwind the controller asked me to squawk NORDO. I reached over to select 7600 and then I suddenly thought, "Wait, is that hijack?" I couldn't remember, and not wishing to trigger a security emergency I dug around in my flight bag for one of those everything-you-need-to-know books. It turned out that NORDO is 7600; hijack is 7500. Anyway, I landed NORDO at Whiteman, taxied back to the hangar, turned off the plane, then turned on the master again and clicked the press-to-talk switch. It worked.
I sent the ox regulator to C&L Aero and have been making tooling for some fiberglass parts, including a fitted funnel for draining the oil. We had a visitor for a few days and I was going to museums and stuff rather than working on the plane; so I haven't gotten much done..
[April 22, 2011]
Further inspection revealed that the problem is simply that the relief valve on the oxygen pressure regulator is missing; broken off, in fact. If I put my thumb over the hole, the oxygen flows normally to the mask. Stumbling aimlessly around the Web with search strings that I never seem able to recreate later, I found C&L Aero in Redding, in Northern California, who charge $90 to overhaul an Alar A2000 -- though they admit that there are no life-limited parts in it, and so overhauling normally means just taking it apart, putting it back together, and, I suppose, maybe hitting it with a fresh coat of black paint. A replacement relief valve -- the originals are no longer to be found -- is another $45. On Monday I'll go by Norton Sales in North Hollywood, world center of aerospace equipment unobtainable elsewhere, to see whether they can do any better, but failing that C&L seems like a pretty good deal.
Yesterday was my granddaughter's birthday. My daughter (her aunt) gave her two tutus. She turned two, so there has to be a tongue-twister in there somewhere.
[April 20, 2011]
After correcting yesterday's errors I connected my welding oxygen bottle to the regulator and the outlets. Concerned that the decades-old armored high-pressure hose might burst and whip around murderously, I put a big piece of carpet on top of it and a packed parachute on top of that. I then just cracked the valve on the bottle. It gave forth a hissing sound that did not immediately diminish, so I gather something is leaking. Most likely the regulator is frozen after all these years. I'll test this more systematically tomorrow; I had a two-year-old sleeping in the car and she woke up just as I was starting. I looked around online for who might overhaul the regulator if it needs overhauling; one company promised a price of "under $600" -- which I suppose means $599.99 before tax -- for almost any regulator. That certainly seems generous -- to themselves.
My bottle, by the way, is a 680-liter (24 cu ft) aluminum one. It ought in principle to be sufficient for 20 hours at 18,000 ft for one person, assuming the most efficient delivery rate, which I gather from this excellent report is around 0.5 liter/minute. Less optimistically, ten hours or so. The report says that the valve on the bottle should not be opened until the oxygen is to be used; otherwise the bottle will leak down through a constant-flow regulator. So much for my idea of opening the bottle valve during the preflight.
[April 19, 2011]
A couple of people had suggestions about why the oxygen fittings are steel. One was fire resistance. That makes sense, but ought to apply to fuel as well as oxygen, and fuel lines are aluminum. Another suggestion was dissimilar metals corrosion, but since the body of the regulator is aluminum, not steel, that would not seem to be an issue. Oxygen is stored in aluminum, steel or composite bottles, and the valves on the bottles are generally either brass or steel. At any rate, there are just a few fittings, so I guess I'll stick with the steel. I installed the two outlets in the floor today, but I didn't get them quite right, and I'll have to redo the installation tomorrow. I also want to hook the whole system together outside the airplane to make sure it working before I install it. Baby steps.
[April 14, 2011]
Further study of the oxygen installation today. My regulator, an Alar A2000, was last overhauled in 1979. I'll try it and see how it performs. I rethought the question of whether or not to have a gauge, and decided that it would not be much trouble to install one alongside the two oxygen outlets. As for turning the bottle on and off, I think maybe I can make the valve accessible through a small hole in the back seat footrest. I'm curious why all the fittings associated with the regulator are steel; for small-diameter tubing, aluminum fittings would be amply strong. Rummaging through my junk collection I found that I have a lifetime supply of nasal cannulas; what hospital I robbed to get them, I can't recall. I need to read up on cannulas vs masks. I don't understand how flowing oxygen out of the cannula continuously, whether you're inhaling or exhaling, can be very efficient. Perhaps the flow is retarded by exhalation. I located a second ignition harness, which I assume must belong to the Slick mags. Still haven't found out the cost of the pressurization kit for the Bendixes, if in fact it even exists.
[April 13, 2011]
I have been closing in on installing the long-delayed oxygen system. It's pretty simple: a tank, a constant-flow regulator, two outlets, and a filling port in the sill of the baggage door. I am not currently planning to have a pressure gauge that is visible to the pilot; the idea would be to check the pressure gauge on the bottle before takeoff or know the pressure from a previous flight, and to know how much time a given pressure represents. So far I have just been figuring out how to arrange the various components so that they require a minimum of modification.
In addition to the oxygen system itself, I have to deal with the magneto pressurization question. Mags need to be pressurized to prevent cross-sparking at high altitude. Melmoth 2 started life with pressurized Slick mags, but after one of them failed in 2003 (a bad coil) I replaced them with the factory-supplied Bendixes that I had put into storage back when I first turbocharged Melmoth 1. Since then I have seldom flown above 15,500 feet. I recently learned that a pressurization kit is available for the Bendixes, which are generally thought to be of superior quality; I'm undecided about whether to invest in pressurizing the Bendixes or to just return to the Slicks, having replaced the bad coil a number of years ago.
[April 3, 2011]
I had a request from a French blogger, Xavier Cotton, for some observations about Melmoth's flying qualities. Cotton, who is a private pilot and an air traffic controller and obviously passioné des avions (crazy about airplanes), has a very nice site featuring pictures and descriptions of lots of interesting planes. If you don't understand French Google will provide a surprisingly readable translation, and the pictures are worth a visit.
When I began writing something for Cotton I realized, first, that I have never given much of a description of Melmoth 2's flying qualities here, and second, that it is difficult for me to do so, in part because I take them for granted and in part because they are -- I believe -- not particularly unusual. Nevertheless, here goes -- though this is less about qualities than procedures.
Taxiing is conventional, using nosewheel steering; if the CG is far aft, however, the nose strut extends fully, nosewheel steering disappears, and I am reduced to steering with brakes. This is very easy, fortunately.
I usually use 34/2,800 for takeoff, but I have up to 41 inches available. (The engine is rated at 200 hp at at 41/2,575; it probably puts out 230 hp or so at 41/2,800.) Acceleration is rapid (about .25 G) and I rotate at around 70 kias. I retract the gear, climb initially at 85 kias, and reduce power to 30/2500. After flap retraction, which takes a while because the flap has such a long way to go, the speed automatically settles at 95 kias. I reduce power further to 27/2300 am at 1000 agl by the time I turn from crosswind to downwind; I normally use the downwind departure at Whiteman because of Burbank Class C.
Once cleaned up, I lean the mixture to 50 degrees lean of peak and trim for a cruise-climb at about 110 kias and 8.5 gph (this does not make much sense; I should climb at a higher power setting, but still lean of peak). Rate of climb at this setting is 500 fpm when I'm alone in the airplane. I set the cowl flaps as required to hold the CHTs below 200 C. I tend to cruise high, climbing to 11,500 or 12,500 for any trip of an hour or more. A typical cruise power setting is 27/2,300, or about 55%, which gives 8.4-8.8 gph and 135-140 kias for a true speed around 170-175 ktas. On a standard day, the cowl flaps are fully closed. Handling is straightforward, with little adverse yaw and somewhat heavier roll forces than you would expect from such narrow ailerons; but the sidestick is very short. Roll-yaw coupling is satisfactory, and the airplane can be steered with rudder alone in smooth air without the ball getting very far out of center. Hands-off stability in smooth air is good; in turbulence, however, the high roll forces are fatiguing.
I usually cruise with the autopilot coupled to the GPS; it can also be coupled to either VOR. Ventilation is good, and I have never felt uncomfortably hot despite the bubble canopy. When roll trim is neutral, usually quite soon after takeoff, I turn on automatic fuel tank switching. The two fuel tanks switch automatically every seven minutes. In such an automated environment, the main challenge is to stay alert.
I usually begin my descent quite far out, reducing power to 20/1900 and descending at 500 to 800 fpm. Around three miles out, I turn off the fuel tank switcher, open the cowl flaps (in case it is necessary to go around) and deploy the airbrake (if it is not already out). At 100 kias or below I lower the landing gear and set 10 degrees of flap. The airbrake produces a nose-up trim change that more or less cancels the flap's nose-down one. Approach speed is around 75 kias, but I rely on the angle of attack indicator rather than the airspeed indicator for approach attitude guidance. On half-mile final I set full flap. I carry about 17-18 in Hg on final. I reduce power and begin to flare fairly high to bleed off speed, because the airplane likes to float. In ground effect I hold it off for as long as I can; the nose gets quite high, with the stall warning bleating during the final seconds before the wheels touch at around 50-55 kias. Stick forces are light during the flare and landing. When the mains touch I pull the stick all the way back to hold the nosewheel off -- with variable success. Once the nosewheel is down I brake firmly; the 3/8-inch thick brake pads provide good energy absorption and deceleration is quite strong. The airplane stops in a few hundred feet.
So that's about it; basically, except for its range of 3,000 miles, it seems like a normal airplane.
[March 23, 2011]
I climbed to 13,500 with the oximeter, which reports "saturation" -- the percentage of the potential oxygen capacity of blood that it is actually carrying -- and pulse rate. My resting pulse is usually in the 60s, but it was a steady 85 while flying. The saturation began at 99%, dropped to 98% at 7,000 feet, 94 at 10,000, and finally 86 at 13,500. There was some fluctuation, and saturation seemed to lag behind altitude by a minute or two, since the readings were different on the way down: 94% at 6,500, 96% on final approach, and 98% as I rolled up to my hangar.
At 13,500 I tried squaring some two-digit numbers in my head, and although I felt that I was doing it as rapidly as normally, I wrote down the answers and after landing found two out of three to be wrong. Furthermore, they were wrong in ways that were immediately obvious to me on the ground. For example, for 84^2 I wrote down 9,056. Now, it is self-evident that since 80^2 is 6,400 and 90^2 is 8,100, 84^2 cannot be 9,056. (It is in fact 7,056.) I'm not sure where the 9 came from; maybe I wrote it down incorrectly after solving correctly. But in any case, I missed the obvious mistake, and this probably had to do with my oxygen saturation being 86%. Whether this has any bearing at all on being able to cruise an airplane, I don't know. Cross-country flying on autopilot is mainly a matter of remaining awake. On the other hand, coping with an emergency is a hit-or-miss business; I have not always made good decisions in emergencies even at low altitude.
Here is a page, copied -- I hope this qualifies as "fair use" -- from a textbook found online, containing a chart of saturation against altitude (the latter being defined in terms of the oxygen partial pressure, which is 21% of the atmospheric pressure). I am a 67-year-old nonsmoker; it is not clear why the values given here are so different from the ones I recorded. Perhaps the oximeter is not reliable.
One noteworthy thing about this chart is the fact that the rate of loss of saturation with altitude increases rapidly above 12,000 feet or so.
On another topic, I checked the wingtip light flasher for radio noise. There was none.
[March 21, 2011]
For more than a week I've been helping my son help his wife prepare a yoga studio for its grand opening, which took place this last weekend. No time for the plane at all. But I finally got back out there today. The nav lights and flashers are now working, so that rather basic requirement is taken care of. I still need to rig up panel lights, however.
After writing about some hypoxia-related accidents for my June Aftermath column and then discovering that pulse oximeters have become very cheap. I bought one ($38). I intend to climb tomorrow -- between rainstorms -- to some goodly height and record my oxygen saturation. I have always believed that I can cruise for quite a while at 15,500 feet without supplemental oxygen and not experience any significant indications of hypoxia. To test myself, I would periodically square two-digit numbers mentally and assess how difficult I found the task and how long it took me. (This is a simple procedure, using the a^2 + 2ab (or -2ab) + b^2 template from high school algebra; it's just a matter of remembering the results of a couple of operations and adding them.) I am of course perfectly aware that a hypoxic person is not the best judge of his own mental capacities; but I am also aware that people react to altitude in quite different ways, and so I am curious to see an objective, numerical measure of my blood oxygen saturation and to compare it with some "normal" values, if I can find them. I have done a couple of pressure chamber rides, of course, but they are not really very informative, because their whole purpose is to hit you with a dramatic demonstration of oxygen deprivation; they never just take you to 14,000, say, and keep you there for two hours so that you can develop a more refined sense of what relatively mild hypoxia actually feels like.
I donate platelets at a local hospital every two weeks, and I asked one of the phlebotomists how, or whether, one's proneness to hypoxia would be affected by donating a pint of whole blood. She passed the question on to a doctor, who said that he didn't think so; but I doubt he had any special knowledge. I'll call FAA Aeromedical and see if I can find out something more than is contained in every magazine article about hypoxia written since the dawn of aviation.
[March 2, 2011]
Between wiring, bad weather and general distractions, I had not flown since returning from Santa Fe at the end of January; so this afternoon I cruised around the outskirts of the San Fernando Valley, down to Malibu, and back over the Sepulveda Pass and alongside Van Nuys. I found on approach to Whiteman that increasing the pitch trim tab travel from 20 to 25 degrees ANU did make it possible to trim hands-off to approach speed with takeoff, but not full, flap and the most forward CG position. Since I fly most of the approach with takeoff flap -- fully shifted aft to the trailing edge of the wing, but deflected only 10 degrees -- and go to the full 30-degree deflection only on a half mile final or so, this is adequate. When there are two or more people in the plane, or any baggage to speak of, I think I will be able to trim to approach speed, or quite close to it, even with full flap.
A correspondent, Frank Shoemaker, suggested checking the voltages of the two batteries after landing. I did so, and found the one closer to the negative pole to be at 12.9 to 13.0 volts and the other to be at 12.8 to 12.9. The next time I add water I will swap the positions of the batteries in order to see whether the difference is due to the batteries themselves or to their positions in the charging circuit. I will also check the voltages when the batteries have just been removed from their respective tenders to see whether they top off to different levels.
[February 25, 2011]
A couple of people suggested swapping the positions of the batteries to see whether the difference in water consumption moves with the battery. I will do that; but if the difference stays put, it will remain uncertain whether the reason is the physical position of the battery, its position in the electrical circuit, or the associated tender.
I posted another YouTube video, this one shot during a flight from Whiteman to Santa Paula. It's not very good, but, like Everest, it's there.
[February 24, 2011]
I've been stringing wires here and there, hooking up the nav lights, pitot heat, and flashers. I also happened to check the battery fluid level and found that it needed some water. But, as is always the case, one of the two batteries -- I use two 14-volt Yuasa motorcycle batteries in series to supply a 28-volt electrical system -- required much more water than the other. It is always the one closer to the negative pole. My first thought was that this had something to do with the battery tender, which keeps the batteries at top charge; but I use two of these "smart chargers," one for each battery, and so they should not behave differently. The battery that needs more water is farther from the exhaust pipe and other sources of radiated heat, and the batteries are in an insulated box anyway, so I don't suppose the difference has to do with temperature, unless from internal causes. Does anyone reading these bottle-messages know whether there is something about the order of the batteries in the circuit that would affect the evaporation of battery fluid, or whether this is simply a matter of two batteries having slightly different personalities?
For a long time I have been putting off installing the oxygen system that was always planned and that seems like a logical requirement for a turbocharged airplane. The problem with it is that it's added weight and would get used very seldom. Once in a while you can get extra speed high up, but it's costly, since although at home you can load your system with non-aviation oxygen at minimal cost, when you're away an oxygen charge is quite expensive -- probably more than an occasional 220-knot groundspeed is worth. My present inclination is to install the plumbing, which entails a comparatively small weight penalty, and leave the bottle behind unless I really think I'm going to use it. But of course what really happens is that you get lazy and just leave it in there.
[February 11, 2011]
I was afraid that upholstering the seat would change the feel of the cushions, and it did; the cover itself tends to compress things here and there, especially around the edges. The seat pan now felt too short, so I remade the metal brackets that hinge the back to the pan -- three times, in fact, since I kept making mistakes or changing my mind about what should be where -- and now it feels pretty comfortable. I won't know for certain until I make another 4-hour flight. I also removed, cleaned, and dry-lubed (with a graphite-moly disulphide spray that a reader recommended) the pins that hold the windows shut. I'm wondering, however, whether frozen grease was really what made them so stiff on my last trip, or whether it's actually the shrinking acrylic windows pulling the window frames out of shape.
Next project is to shim the gutters around the windows and hit them with a heat gun to temporarily soften the epoxy and, I hope, increase the clearance so that the windows are not so hard to open at low temperatures (this is a different problem from the difficulty with the locking pins).
[February 3, 2011]
I did the trim cable modification that I was thinking about a couple of weeks ago. It turned out to be more complicated than I anticipated -- what doesn't? -- and netted only a five-degree gain in aircraft nose-up trim tab deflection, from 20 degrees to 25. I picked up 10 degrees of additional travel in the nose-down direction, but that's pretty useless. I also put in a positive stop for the cable, so that the end of its range will no longer be signaled by the swaged cable end trying to wrap itself around a pulley. I have not yet flown to see whether the added tab travel has any effect on the minimum speed to which I can trim with a forward CG. What ultimately limited the tab's travel was not the cable or chain but clearances among the trim components, which are pretty tightly packed up in the T-tail intersection.
I also re-centered the out-of-whack flap valve and safetied the flap cable to the sector in the flap handle on the panel, so that it can't slip off the next time I fly into a deep freeze. Also, having flown many hours in my makeshift seat -- I can't even remember when I last adjusted the shape of the foam padding -- I took it to an upholstery shop in Highland Park to make it official. It's supposed to be done tomorrow. Who knows -- one of these days I may finish painting the instrument panel.
[January 30, 2011]
Most flights are entirely uneventful. A few are all too eventful.
I went to Santa Fe on Monday, January 24, to fly an airplane called the Sunbird Seeker at Albuquerque. After cruising at 13,500 where the OAT was -16 C, I descended into Santa Fe to find that when I selected flaps down the cable that connects the handle on the panel to the valve under the seat jumped its groove. Okay; I landed with no flap. The cable loop was surprisingly slack, and I concluded that the entire airplane had shrunk because of the cold. Since epoxy shrinks much more than steel, and for that matter the steel cable was within the warm cockpit, the effect had been to loosen the cable. I made a note to safety-wire the cable to the sector rather than rely on tension to hold it in place. Other temperature-related observations were that the window gutters interfere with the frames when cold and make the windows very hard to open, and that the window locking pins need to be thoroughly cleaned and dry-lubed. My well-intentioned greasing of them was fine for Southern California, but not such a great idea for a Rocky Mountain winter.
I felt some odd vibrations during that four-hour flight, and when I took off on Wednesday to return home I thought the engine did not feel right. I turned back to Santa Fe, where a mechanic named Kermit at Aero Services found my right mag to be 5 degrees more advanced than the left and my fine wire plugs, veterans of many happy hours in both Melmoth 1 and Melmoth 2, to be worn out. He rebuilt both mags (but did not replace any parts) and installed nine new massive-electrode plugs -- all they had in stock of the appropriate type -- along with the three least heinous of my old ones. I then started west, found the engine restored to smoothness, and got to Winslow as night was falling. I spent the night there.
In the morning the temperature was 14 degrees F. and the airplane was thoroughly cold-soaked. It took me a long time to get the engine to start; when it finally caught, I was using the flooded-engine technique -- mixture leaned, throttle wide open -- which often has the effect of letting the engine race briefly while you're getting the mixture forward and the throttle back. When I ran it up, I found the right mag seemingly completely dead and the left mag showing no drop -- as would be expected if the right mag were not supplying any spark. There was no mechanic at Winslow, but the FBO, Wiseman Aviation, also has a Flagstaff base, and they put me on the phone with the mechanic there. He said to disconnect the P lead from the right mag, since evidently something was grounding the mag. This was sensible advice, but it did not work out especially well.
I took off and found the engine still quite rough, so I went to Flagstaff, just 20 minutes away, and presented myself to the mechanic with whom I had spoken. His name was Rory Goforth -- a poetic name, I thought, for someone who sends airplanes roaring out into the world. I described the problem, including the fact that both mags had just been rebuilt. I should have kept my mouth shut. My explanation had the effect of convincing both him and me that the problem, whatever it was, could not be in the mags. In retrospect, this seems puzzling to me; after all, I had just found the right mag to be not working. But I had persuaded myself that this was due to the P lead, not the mag itself. Rory spent a couple of hours going over the usual suspects -- injectors, ignition harness, plugs -- without finding anything amiss. I took off again, flew ten miles, still didn't like the feel of it, and returned to Flagstaff.
At some point I suggested that I run up the engine and he listen to it. This wasn't especially brilliant -- it was the only thing left to do -- but it turned out to be what we should have done in the first place. As I turned off the left mag, the engine died on cue. But Rory heard something I hadn't heard -- a single pop; and he understood that it meant that the mag was not dead after all -- just malfunctioning badly. I tried the mag check again, this time letting the engine spool down for a longer time, and sure enough there was a series of pops. The right mag was firing on just one cylinder. This seemed mysterious until we looked -- at last! -- into the port at the nylon timing gear. I turned the prop. The gear did not turn. Eureka!
What apparently had happened was that the nylon gear, embrittled by age and cold, had shed a mess of teeth when the engine suddenly roared to life at Winslow. The replacement gear arrived the next morning and I returned to LA that afternoon. It was a smooth, windless and vibration-free flight.
A couple of days after returning, I was making circuits at Santa Paula for pictures to accompany a Technicalities column when I noticed that any time I operated the hydraulic pump the flaps moved upward slowly. What had happened was that the center-off positions of the panel handle and the valve had gotten misaligned when I tightened the flap cable loop at Santa Fe, so that when the handle was in the "off" position the valve was actually slightly open in the "down" direction. When tensioning the cable loop one has to adjust both legs, not just one. I had encountered that issue before; but since I have never compiled everything there is to know about Melmoth 2 into a service manual, I had forgotten about it over the years.
[January 20, 2011]
A minor irritant has been the inability to trim to approach speed at extreme forward CG; the best I seem to be able to do is about 1.4 Vs. Since I fly so much alone, and therefore at forward CG, it would be nice to have a little more trim authority. Currently the trim tabs deflect 20 degrees ANU (aircraft nose up) and 5 degrees AND. It happens that the AND authority is also just enough to cruise with extreme aft CG, and so I can't rob Peter to pay Paul. What currently limits the total tab travel is the distance between the trim wheel sprocket and a pair of pulleys behind the panel that turn the trim cables 90 degrees; the chain that the sprocket drives can't get closer than about two inches to the pulleys because of the length of the swaged cable fittings that link it to the cables. So the only way -- at least the only convenient way -- to get more tab travel is to replace those fittings with shorter ones.
On the suggestion of Russ Hardwick I found small aluminum cable splices at a hardware store; these can be swaged with a pair of pliers, and while their tensile strength is not that of a proper aircraft swage, it is certainly enough for a trim system. These look as if they will increase the chain travel by 40% and the total tab travel to 35 degrees. The more I think about how to perform the surgery, however, the more problems I recognize. For example, I seem not to have kept a record of the length of the chain in the T-tail, where the motion of the trim cables rotates a jackscrew; I will have to remove the rudder to find out. At any rate I guess I would have to remove the rudder to make sure that both chains are at the center of their travels at the same time. At least once the cable circuit is working, distributing trim authority between nose up and nose down is a simple matter of disconnecting the jackscrew nut from the tab and moving it forward or back.
Rather than replace the entire trim cable loop, I figured that I would just make new cable ends with the shorter end-loops and splice these onto the existing cables. One splice can be done with the little swaged fittings, but I thought the other might require some adjustment, and so after finding that my local bicycle shop didn't have anything suitable I made a little splice fitting. One cable inserts in a blind hole in one end and is locked in place with two set screws. The other enters on the same axis at the other end, but bends and emerges from the side of the fitting so that it can be held in tension with one hand while the other two set screw are being tightened. I use similar fittings on the cables going to the gear, flap and airbrake valves under the passenger seat, and they have worked pretty well. Here are the new, shorter cable ends and the splice fitting:
[January 15, 2011]
A visitor from France has been staying with us -- Vincent Legeay, who is in a Master's program in philosophy at the Sorbonne and is currently taking classes at U Mass and teaching French at Amherst College. We spend quite a bit of time discussing the prosody of Rimbaud, a topic in which I have an inexplicable interest. We flew out to Death Valley yesterday so that his experience of California could include something other than the many wonders of Los Angeles. On the return I got pilot reports of moderate and even severe turbulence over the mountains north of L.A., and so I stayed at 12,500 until we were over the San Fernando Valley and then descended somewhat rapidly. As it turned out, either this plan worked or there was no turbulence to start with, because we didn't run into much. It was glassy, warm and calm all over the desert. Vincent, dans l'avenir quand tu chercheras ton nom avec Google, tu te souviendras de ce vol.
Vincent Legeay in Melmoth 2, above the middle of nowhere.
[January 6, 2011]
I investigated the stiffness of the trimwheel and found that it was due to the grease in two bushings and jackscrew up in the T-tail joint having dried out. I guess I could use better-quality grease -- there are certainly lubricants that don't evaporate, or leave no residue when they do, and that don't stiffen up at low temperatures -- but instead I cleaned the offending parts with acetone and reassembled them dry. Metals of dissimilar hardness, like steel and aluminum, make naturally good bearings, at least at low rotational speed, even with no lubricant, so at least the two journal bearings should be all right. Both the male and the female components of the jackscrew are hardened, so I don't know how well they will work together; they may require a lubricant. At least the trim now works freely again, but I think I may still enlarge the trimwheel just to make it more sensitive.
[January 4, 2011]
From time to time I have mentioned that Melmoth 2's parasite drag coefficient is .022 (roughly) and I have commented that this is not especially low. Nevertheless, compared with a Mooney 201 (for example), whose parasite drag coefficient is said to be .017, M2 requires less fuel to achieve a given speed. To clarify this apparent contradiction, it must be said that parasite drag coefficient, although it seems like a nice, pure, technical way of expressing drag, is really almost meaningless, because it is based on wing area, which is used as a stand-in for the complete airplane. Obviously, this makes little sense; you could shrink the wings of an airplane and its drag coefficient would go up even though its drag would have come down. M2's wing area (105.4 square feet) is much smaller than a Mooney's (175). If M2 and a Mooney had the same drag, the Mooney's parasite drag coefficient would be .013, which would be fantastically low. (On the other hand, if Melmoth 2 had more wing area, it would also have more drag.) Some aerodynamicists prefer to cite a wetted area drag coefficient, which is based on the total surface area of the aircraft and therefore is theoretically more reflective of its size than wing area alone is; but actually from the point of view of the human occupants it would make more sense to base a drag coefficient on cabin volume or useful load or number of seats or some other ingredient or combination that might reflect the utility and perhaps even the comfort of the airplane. Equivalent flat plate area, or "drag area," which is a way of expressing actual drag, is closer to reality than parasite drag coefficient is; M2's is 2.3 square feet, the Mooney 201's is (according to at least one website) either 2.8 or 2.97, depending which numbers you use.
Fuel flow is not a good basis for comparison either. The aforementioned website gives a cruising speed of 160 knots for a Mooney 201 at 10.5 gallons an hour, presumably at around 8,000 feet. M2 uses 8.2 gph at that speed. But mixture setting could account for at least part of that difference. Besides, all these numbers are highly uncertain; different airplanes are tested by different people under different circumstances and for different purposes, and there is little consistency in the results. When the data from many years of CAFE races were reduced to equivalent-flat-plate form, it was striking how much variation in drag area there was within a given type and model, even though the airplanes were all exactly the same size.
A reader commented, with regard to my previous posting, that GPS is unlikely to be accurate to one centimeter. This is true. When I said that the Appareo stores lat-long data with a precision of one centimeter, I intended to distinguish between precision, which is simply the number of decimal places presented, and accuracy, which is fidelity to reality. For the purpose of measuring groundspeed, an accuracy of one foot, or about 30 cm, is enough, and it doesn't have to be absolute accuracy, just consistency from one moment to the next. In other words, it doesn't matter if the GPS has the lat-long of the airport wrong, provided that the error remains more or less constant